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Frontier Energy
Appropriate Thchnology in Alaska, 197'9-1984
ARLIS
Alaska Resources ·
Library & .Illformabon Services
~-chorage,AJaska
11 -1 I
This book was prepared with the support of the U.S. Department of Energy (DOE) Grant No. DE-FG51-81R000680. However, any
opinions, findings, conclusions, or recommendations expressed herein are those of the author(s) and do not necessarily reflect the views
of DOE or the State of Alaska.
ii
AUG 2 1 1985
~IX A Rt~~O'Uft G~ 1 'TPW 4..Rl"
tl .l.. DEPT. OF L"iT Ji.' .n J;.
Frontier Energy
Appropriate ·Thchnology in Alaska, 1979-1984
State of Alaska
Bill Sheffield, Governor
Department of Community &
Regional Affairs .................... Emil Notti, Commissioner
Division of Community Development .............. Karen Perdue, Director
Energy Conservation Program ............................... Steve Baden, Chief
Appropriate Technol ogy Programs ............................... Norman Bair, Manager
Editorial, Design, Production Assistance by
The Alaska Group
December, 1984
lll
A cknowledgements · ·
Pre fa ce
THE PROJECTS
Table of Contents
EARTHSHELTERED BUILDINGS
Dome house w ith a difference .............. .
R. Ky le Green
Uni que co n s tr uction method : Inflatable house ......... .
Advanced, Inc.
.............. ix
... xi
. .. 1
. .. 2
Underground greenhouse a major success . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 3
Wind-N-Sun Enterprises, Inc.
']want to li ve as soft upon the earth as I can' ..................................... . . .................. 6
Jerry Brown
ATTACHED GREENHOUSES
Fuel b ill s down, vegetable crop up .................... . .. .8
Alice Grant
Greenhouse more than an indoor garden . 10
No rman Aaberg
Greenhouse first step to energy self-sufficiency .......... . . ... 11
Mark ]. Garrett
Greenhouse overcomes severe climate .................. , ...........•.................................... 13
Steven Behnke
So larium a n asse t during Alaska winter
Larry Cline
Rustic co mfort: Solar-heated log cabin.
Jack Segle
SUPER INSULATION
Bu ild in g a n airtight environment ..
Matanuska Borough School District
Home's 's hell' holds heat. . ................. .
Terence L. Duszynski
GREENPIOUSES
Chickens provide greenhouse heat supply .......... .
Elizabeth Hart
....................... 15
.17
.19
..21
. ........... 23
Waste heat increases growing season
MTNT, Ltd.
............................................................. 25
Greenhouse crop s upplements traditional lifestyle .....•...................................... .28
Kuskokwim N ative Association
Construction p lans put on hold ......... . . ..... 30
Kotzebue l.R.A. Council
Recycled tire rubber provides thermal mass ........................................................ . . .. 31
Paul Robinson
"The ground acts as a very big radiator " .
John Co llette
Community g re enhouse provides example ................ .
Alaska Federation for Community Self Reliance, Inc.
A lesson in greenhouse improvement.
SAVE I H ig h School
WINDOW INSULATION
Search for a n energy-saving window shutter
Ed McGrath
. .. 32
. .... 33
. ...................... 35
............. 37
Polystyrene bea ds to prevent heat loss ................................ . . ........................... 38
Jerry and Judy Miller
ENERG Y STORAGE, MASS
Home's wall used as giant duct
Mark S. Merrill
AIR INFILT RATION
Heat lo ss reduced with rubber gaskets
Jerolyn Wroble
PASSIVE SOLAR HEATING
Solar collector has unexpected results
Clifford Cantor
.......................... 39
...................................... 41
... 43
v
ACTIVE SOLAR SPACE HEAT
Solar water heating system falls short in Fairbanks ...................... . . ........................... 45
H. Jack Coutts
Solar heat works well in Copper Center ..... . .......................................................... u
Kenny Lake Community League
DOMESTIC SOLAR HOI WATER
A comparison: Three solar water heating systems . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . ............... 51
Municipality of Anchorage
Solar powered pump increases efficiency . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . ..... 54
Dais Dallas
Automobile radiator reduces home fuel bills . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .................... 57
Mark A. Miller
SOLAR GRAIN DRYER
Palmer's energy farm proves up ................ .
Thomas E. Williams
METHANE DIGESTER
Crab waste produces methane gas supply
R. Charles Vowell
Design allows for continuous gas production ................................. .
McKee Inc.
PHOIOVOLTAICS
Solar power helps count fish .................... .
Alaska Department of Fish and Game
Capturing energy above the Arctic Circle ............... .
James A. Schwarber
Electric lights a wilderness luxury .......................... .
Susan E. Rainey
. ...... 59
. ...................... 63
. ......... 65
. ... 67
. .. 68
Photovoltaics perform well in Alaska Bush . . ............................................................ 69
Thomas H. Vaden
THERMOELECTRIC
Electric current from wood stove heat
W Findlay Abbott
WOOD SPACE HEAT BOILERS
Gold miner tries new boiler system ..
John W Greene, Jr.
................................................................... n
. .............................................................. n
Design goal: Energy efficiency ........... .
David R. Newcombe
WOOD-FIRED STEAM BOILER AND ENGINE
Stea:rrWloat to ply the Holitna River ...................................................................... 77
Grant Fairbanks
Wood-fired boiler requires fuel supply and attention ....................................................... 79
Guy Matthews
From wood to steam to electric lights ..................................................................... 80
Warren F. Powers
Driftwood and boiler to heat home ...................................................................... 82
Kenneth Duckett
Fishing boat to be powered by steam engine .............................................................. 84
Michael Broili
WOOD HEAT STORAGE SYSTEMS
Outdoor furnace heats home ........................................................................... 85
Wilbur LaPage
Novel system provides heat and hot water ................................................................ 87
Patrick Yourkowski
WIND GENERATOR, INTERCONNECT
Wind power supplements local utility ................................................................... 89
Northwest Arctic School District
Wind generator impresses villagers ...................................................................... 90
Hooper Bay High School
Salmon hatchery aided by wind power .................................................................. 93
Sand Point School
School District harnesses wind ......................................................................... 94
Metlakatla Indian Community
Guard takes conservation to the Bush .................................................................... 95
Alaska Dept. of Military Affairs
Danes' experience adds to local know-how ............................................................... 97
Steven Smiley
vi
'i
WIND GENERATOR WITH BATTERIES
Generator hits rough weather at sea ..................................................................... 99
Jon W. Seager
Wind power practical in remote location ..... . ........................................................ 101
Richard/. Logghe
Floating wind generator a partial success ................................................................ 103
Frank Simpson
Wind-powered telephone system .........................................................•............ 105
Interior Telephone Company
Teacher, students build a wind generator ................................................................ 107
Lake and Peninsula School District
Students learn from wind project ...................................................................... 108
Lower Kuskokwim School District
WINDMILL, WATER PUMPING
Windmill pumps hatchery water .............. . . ................................................. 111
Nerka, Inc
HYDROELECTRIC OVERSHOI WHEEL
Waterwheel made more efficient ................. .
Robert Nelson
HYDROELECTRIC, PELTON
. ............................................... 113
Hydro system powers hatchery ........................................................................ 115
Eugene Richards
Micro-hydro project generates interest .................................................................. 117
Roy Lawrence '
Willie Nelson regulates power output .................................................................. 119
Chester Johnson
Water beats wind for reliability . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . ............ 120
Ken Cassell
" ... care involved when you become your own power crew" ....... .
Louis A. Butera
Hydro success requires careful planning ....................... .
]ames and Maureen Gohr
What a difference a hot bath makes ......................... .
Richard Mathews
HYDRAULIC RAM
. . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . 123
. .... 125
. .................................. 127
Hydraulic ram ensures reliable water supply ........................ . . ............................... 131
Don Chaney
RANKINE CYCLE ENGINE
Freon system propels turbine
Arthur Manning
REFRIGERATION
.................... 133
A water-powered refrigerator. . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . ..................... 137
Don Bailey
Bush refrigerator an unqualified success ........... . . .......................... 139
Perry E. Hilleary
HEAT EXCHANGER, AIR
Kenai City Hall saves energy
City of Kenai
HEAT EXCHANGER, WATER
..................................................................... 141
A wastewater heat exchange system .................................................................... 143
Mark Gudschinsky
Heat exchanger cuts fuel bills ......................................................................... 144
Richard Runser
MONITORING AND TESTING
Computer prioritizes wind energy use
Stanley A. Baltzo
........................................................... 147
Automatic stack dampers installed ........................ . . .148
·KNOMRadio
Building a fire-prooCchimney ............................ . . ... 150
David Norton
Monitoring system collects useful data ................ . . ..... 152
Jeremy and Linda Weld
Demonstration project a success ................. . . ..... 154
Stan A. Moberly
Satellite aids in cord wood inventory .............................................................. . . .. 157
Dr. William Stringer
Ethanol production requires large amounts of energy .......................................... . . .... 160
Neldon Wagner
vii
STUDIES
Energy-efficient salmon drying facility studied ........................................................... 161
Iguigig and Levelock Natives, Ltd.
Salmon waste study shows good result . . . . . . . . ..................................... . . .............. 162
Dr. Leroy C. Reid, Jr.
Wood gasification studied by timber mill .....
Mitkof Lumber Company
CURRICULUM AND MEDIA MATERIALS
Media and curriculum projects expand energy knowledge
APPENDICES
. ............ 164
.... 167
Glossary . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . ........... 171
AT grants to libraries, 1980-1982 . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . ................. 173
AT edited videotape project material ................................................................... 174
Grant awards returned or not accepted . . . . . . . . . . . . . . . . . . . . . . . . ..................................... 175
Grant projects terminated before completion . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . .......... 176
LIST OF ILLUSTRATIONS
KEY TO SYMBOLS ............................. . . .............................. xiii
MAPS
Locations of Case Studies in Alaska . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . . ................................ xv
Climate Zones of Alaska ............................................................................. xvi
Mean Annual Precipitation in Inches in Alaska .................. ~ . . . . . . . . . . . . . ........................ xvi
viii
i'
T
l
'
Acknowledgements
The State of Alaska, Department of Community and Regional Affairs, and the
editors of this report wish to thank the many AT grant recipients who made the effort
to report on their projects so that others might learn from them in this report. That
effort came in the form of laboriously lengthy hand-written letters, to printed, bound
final reports. And by telephone, once-weekly mail service, and messenger. Both the
Department and editors wished these direct communications could each be printed in
their entirety. Unfortunately, limitations of space and disparate writing styles made
this impossible.
The editors also wish to acknowledge the two principal writers for the project, Cary
Virtue, of Anchorage, and Alan Geist, of Fairbanks, for their good nature and on-
time production on short deadlines. Ralph Nichols, of Anchorage, also contributed.
A special salute is due Miki Ballard and Joyce Talley for well-managed typographical
production above and beyond. Naomi Manabe and Johnny Ellis were valuable in
managing proofreading, quality control and other minute details of a publication of
this size. And finally, state project manager Norman Bair gave unflagging support
and guidance to the project.
ix
Preface
The U.S. Department of Energy's Appropriate Tech-
nology Small Grants program was a three-year program
that gave individuals, companies and governments the
opportunity to devise and apply various appropriate
technologies, principally for energy-related projects.
'Appropriate Technology" is a term coined by Ernest
Friedrich Schumacher, of Germany: student of Oxford
University; economist with the British National Coal
board from 1950-1970; United Nations economic advisor
to Third World countries; and outspoken defender of the
poor. After observing that the introduction of modern
technologies did not always bring benefits to the poor of
underdeveloped countries, he described a new kind of
economic development, based on a technology "more
productive than the (local) technology but immensely
cheaper than the ... technology of modern industry:'
Hence, a technology "appropriate" to the local condition.
According to Schumacher, this intermediate, ("appro-
priate") technology should have four characteristics; it
should:
• create employment in rural areas to reduce out-
migration to the cities, with their high unemploy-
ment rates;
• rely more on local labor than expensive machinery
and resources
• be simple enough for local people to make and
repair, themselves
• be used mainly to produce goods or services for
local use
Alaska is among 50 states and U.S. possessions that
participated in the grants program from 1979-1981.
Ironically, with one of the nation's highest per capita
incomes, Alaska may be far from the poor nations'
plight that Schumacher envisioned improving when he
energized the movement.
Nonetheless, Alaska certainly has unique circum-
stances of local geography, climate, and custom. Some
365 million acres of land area. Four geographic time
zones. Nearly 34,000 miles of coastline, 50% more than
all other states combined. Annual temperature variations
of 140 degrees in some areas. A population density so
low that a New Yorker would be hard pressed to imagine
it. Four economically maturing Native cultures. The
nation's largest producing oilfield. And remoteness,
spawning high costs for transportation, fuel and every
other necessity.
With transportation and energy costs affecting urban,
Bush and rural Alaska alike, it was predictable that sup-
port would evolve for Alaska to participate in the federal
grant program. (Alaska was the only state providing
additional funds, allowing almost twice as many grants
to be awarded.)
During the years the program was funded, the federal
government and State of Alaska jointly awarded 205
grants with nearly 100 AT grant projects at a total grant
cost of $1.3 million, ranging from simple greenhouse
structures to complex wind generators and waste recov-
ery systems.
XI
The projects were executed by a diverse group of
Alaskans. They live along the western coast, where
winds and cold seas carve the landscape; in Southeast,
where 100 inches of rain is common; in the Interior,
where sunlight is minimal during four months of the
year. Everywhere, energy costs are high. In many areas,
roads, telephones, sewer and water, and power utility
lines have not reached remote homesites and settlements;
until the mid-1970s, television was something watched
only in larger cities, themselves with a two-week delay
from the rest of the United States.
The grantees are homesteaders, teachers, fishermen,
students, entrepreneurs, carpenters, cabinetmakers, engi-
neers, housewives, professionals-and public utilities,
libraries and government agencies. Some found new
applications for old technologies. Others converted con-
ventional materials and appliances to energy-producing
or conservation systems. Still others recycled wasted
products to create new energy sources or worked to
spread knowledge and appreciation for the potential of
any individual to be an independent energy producer.
Some are innovators, devising systems that may well
have wider applications in the future.
For some grantees, the AT program was a means for
survival; for others, the program was a catalyst to
develop less costly, more efficient ways to heat homes,
produce food, or improve safety.
The OPEC oil embargoes of the early 1970s left a last-
ing impression on a number of the Alaskans who par-
ticipated in these projects. Others recalled simpler times
when windmills dotted the Great Plains, providing a
reliable energy source long before rural electrification
took hold; or the common use of hydraulic rams to tap
abundant water resources; or the power of the captured
sun to manufacture plant life; or the capability of a sim-
ple waterwheel to heat a home and create light where
none was before. Several were optimistic that their
chosen design would improve their business, by reducing
their costs or improving their performance in the field.
Other enthusiasts produced instructional, training or
information materials to show others the way.
The program was a pioneering one, from those who
had seldom lifted a hammer to the man who devised a
new use for crab wastes in the heart of the king crab
fishery. There were projects that had high promise, and
fulfilled that promise, such as the wind system for a
remote cabinetmaker or the hydro project that operates a
fish hatchery. There were projects with great promise
that never achieved their goal, such as the (somewhat
humorous) tale of a family's bout with black flies breed-
ing in the solar collector and infesting the home.
There were several wind generator projects that exceed-
ed even their highest expectations. There was tragedy in
the grantees whose unexpected personal problems halted
projects altogether; but there was victory for some. All
of the projects were practical, planned to allow the
grantee to save money and simplify the challenge of
creating energy supply.
And it's apparent that the concept and its applications
have not died with the termination of government sup-
port three years ago. Commercial enterprises have
sprung up nationwide, like the entrepreneurial com-
panies that specialize in wind generators and small hydro
projects. Replication of the government-funded projects
may be found everywhere, from greenhouse construc-
tion, to cooperative power use in small communities. At
the same time, systems that were devised with the for-
tuitous help of the government continue to perform well
long after the last of the paperwork has been supplied to
the sponsoring government agencies.
The stories of a major portion of these projects and the
people who tried to make them work is the subject of
this final report on Alaska's partnership with the U.S.
Department of Energy Appropriate Technology Small
Grants program. Although federal and state funding of
this program ended with the 1981 funding year, final
reporting and close-out of the program continued in 1984.
This report is organized by project type (eg. solar
greenhouses, wood-fired boilers, small hydroelectric,
etc.). In some cases, projects had more than one applica-
tion; these are clearly symbolized in the beginning
of each.
Some of the project reports were highly technical and
edited for general readership; this overall report was
compiled so that newcomers to the concept would not be
overwhelmed with technical detail and jargon. Thus, for
example, temperature references became Fahrenheit
rather than Celsius; more common "brand" names were
Xll
used instead of their technical, chemical trade names;
and common building materials (such as "two-by-fours")
were written the way most people hear them.
This book is also designed for browsing, and for
learning of others' experience in specific areas. For many
of the grantees and federal! state coordinators of the proj-
ect, it was produced in the hope that others 'will take the
same road and accept a challenge of improving on cir-
cumstances that surround a chosen lifestyle-be that
lifestyle that of a remote subsistence homesteader or
commander of a military organization that must improve
its power-generating efficiency.
All the materials produced from these projects will be
archived in the Alaska Department of Community and
Regional Affairs' Division of Community Development
library, for those seeking a more detailed description of
the project described. These materials include indi-
viduals' original applications for the grants; their prog-
ress reports along the way; photos of their labors;
descriptions of costs; newspaper and newsletter articles
about various projects; video tapes filmed by the media
or by independent producers; final reports as they were
submitted by most of the grantees; and several research
reports.
But perhaps the best sources for individual projects
are the grant recipients, themselves. Many are quite
accustomed to questions from someone who has heard
of their endeavors.
The following pages tell their stories.
Key to Symbols
Primary Energy Sources
Sun Wind
Heat Exchanger
I ti.?JI Refrigeration ~~
r
I ~ I ~ I Window or Window Insulation
..
~. u Distillation
Earth -sheltered Dwelling
I ~ I Demched Greenhouse
Attached Greenhouse
X lll
Water ttJ Water Wheel
[I!] Monitoring
~ g Battery, Storage or Operation
[jliJ Documentation
'IZJ Media
~.~ ~ Woodfuel
~ Insulation
EiJ Hydro QJ Water Pump
[] Vocational and Technical Training ~ Pelton Wheel
I ~-~~ Combustion
~ Mass
10 I Recycle
Air Infiltration
~
~ Electricity
~~ Biomass
Ia Home Enhancement
"
xiv
X <
0 0~
,._ ==<!
v ...
4
•
• •
,.
Locations of Case Studies
in Alaska
;;.. ..
xvi
Climate Zones of Alaska
D -Arctic
• -Continental
D -Transition
D-Maritime
SOURCE: AE ID C
Mean Annual Precipitation
in Inches in Alaska
D 0 '-'-10 "
• 10'-'-40"
D 40'-'-160"
D 160 '-'-3 20 "
SOURCE : AEIDC
r.
Dome house with
a difference
Kyle Green has designed a geodesic dome house with
a twist. Part of it will be sheltered by the earth to boost
its heating efficiency.
In fact , Green designed his home to reduce heat loss as
much as possible . Further, the house was planned to
reduce windwash, the exterior surface area to floor area
ratio, and window and entryway heat loss. He hopes
stored solar heat will keep the geodesic dome warm and
cozy in winter.
The home is being built on a south-facing hillside in
Wasilla, which is about 40 miles north of Anchorage. A
completed module of the home serves as an office while
the main house is under construction.
House Design
The main floor is a concrete slab at grade with a 17-
foot-diameter water tank located in the center, below
grade. (Access to the tank is through a wood hatch in
the floor.) The water in the storage tank will be heated
by the fireplace and by active solar collectors behind
the house above the roof line. The egg-shaped house
will be earth-bermed along the north side.
The smaller office module similar in design to the
main house , will be connected to the main house. The
basic dome shape is accomplished by crisscrossing re-
bar in an elliptical grid. Wire lathing is attached to the
formed rebar and cement is applied in a thickness of two
to three inches. Three inches of urethane is then applied
to the outside of the cement and a protective coating is
put on the urethane to prevent ultraviolet degradation.
One small triple-paned window looks to the south from
inside the office. The office module will be heated from
the main heating system.
1
EARTHSHELTERED BUILDINGS
Construction
The office module was completed in the second half of
1979, along with the main house slab and rebar struc-
ture. Initial plans to use blown-on ferrocement were
abandoned due to limitations of supply and cost. In-
stead, the cement was troweled onto the wire lath. The
excavation for the main house removed gravel down to
sand. Plans to have an earth-formed water tank in the
gravel were modified , since this was not feasible in sand .
Instead, corrugated culvert sections were used as con-
crete forms for a seventeen-foot diameter tank that is five
feet deep.
Solaroll-brand mat tubing was placed below the con-
crete slab for distributing heat to the house from the
storage tank .
Some progress on the main house rebar structure and
storage tank has been made, but additional funds are
needed to complete the project.
Problems
It appears that total construction costs for such a
structure would exceed conventional construction costs .
The office module has a number of holes .in the insu-
lation where birds have tried to make a nest. Interim
bank financing was not available for the funding
requirements.
Funding
U.S. Department of Energy $47,900
Grant Recipient
R. Kyle Green
SRA Box 6268
Palmer, Alaska 99645
Kyle Green 's Wasilla home (/eft) being built using a steel rebar
superstructure. This arched window (above) is located in the
comp leted portion of the house that is used as an office.
Unique construction
method: Inflatable house
The economic hub of Interior Alaska-with Prudhoe
Bay oil fields to the north, mineral deposits to the west,
and regional corporations nearby-Fairbanks has
remained vital since its Gold Rush days early in the
century. Fairbanks is hardy-few have not shivered
through Robert Service's tales of what strange things the
cold can do to inhabitants of the frozen North.
Advanced, Inc. of Fairbanks received a grant in 1980
to design a dome house that could dig in against the grip
of the cold winters Service described so eloquently
decades ago.
The company proposed a unique rubber construction
approach to this earthsheltered house on the hillside.
(The project assumed 1 ~,344 heating degree days with
a minus 60 degrees winter design temperature ).
Design Cri teria
The house was designed to be highly energy efficient .
Fuel use was to be limited to 225 gallons of oil per year,
and conventional materials were used (no sophisticated
energy saving sys tem s). The project also was desig ned to
have minimum impact on surroundings and to use a
southern exposure.
House Design and Construction
The house shape is an elliptical dome with earth-
sheltering in all directions but the south. The unique
design of the house was combined with an unique
method of construction. An elliptical concrete slab was
poured at the excavated grade level over urethane insu-
lation sprayed directly on the ground two to four inches
thick.
.. ~.-
:;--,.. __
2
Solaroll-brand flat tubing was snaked over the ure-
thane before the concrete was poured. This provides for
the radiant hot water heating of the house.
A vinyl plastic balloon was fabricated and fastened to
the concrete slab. The balloon was inflated with a large
fan to take the shape of the final structure. A double-
door entry system allowed workers to enter and exit the
balloon without altering the structure. This allowed for
the majority of the activities equivalent to frame-up to be
performed out of the weather.
Window and door openings were marked on the inside
of the balloon. An initial coat of urethane insulation was
sprayed on the inside of the balloon . Eight-inch wire
rods with peel and stick bases were fastened to the
urethane in a one-foot square grid pattern. The final five
inches of urethane were sprayed on, securing the wire
rods in place. A vapor barrier also was s prayed on the
urethane.
Rebar (three-eighth-inch diameter) was curved and
fastened to each of the wire rods to form a uniform grid
pattern. Additional rebar was shaped and fastened
a round the wi ndow and door openings. An eight bag
gunite concrete mix was sprayed to a thickness of six
inches at the base, tapering to 2 1/z inches on the roof.
With all the concrete on the inside of the urethane, the
h ouse has a large thermal storage mass. This helps to
minimize the problems of freeze -up that can occ ur with a
heating or power failure.
After the concrete had cured, the reusable balloon was
peeled off the o utside of the s hell. The interior was
,
A concrete slab (ab ove left) w as pou red as a foundati o n fo r th e
dome house. The completed st ructure is abo ve right.
1
finished w ith normal stud w alls to prov ide a 2 ,200-
square-foot, three-bedroom house. A glassed-in plant
room on the north wall brings daylight into the house
from a skylight.
Performance
The house has been lived in since February, 1981.
Although it uses less oil than most for its size , the 850 to
1 ,200-gallon annual use is more than the predicted 225
gallons per year. The floor layout and high ceilings pro-
v ide open s paciousness which is very nice during the
long, cold w inters of Fairbanks.
Problems
The radiant heating sy stem does not always keep the
house at a comfortable temperature on colder days.
Some possible reasons are inadequate tubing under the
slab for the required heat transfer; or inadequate pressure
to keep the slab from flattening the tubing when the
concrete was poured, or inadequate size of the heat
exchanger on the hot water heater, or inadequate hot
water heater temperature on cold days.
The garage and front entryways are recessed about
four feet from the edge of the slab. This means that
portions of the slab are allowed to freeze and there is no
thermal break from the outside to the inside in the slab.
The slab has heaved slightly at the front door, causing
interior walls to crack and misalign entry doors.
Either shrinkage of the shell or a slight movement
inward from the earthsheltered side may have caused
sheetrock bulging in the inner plant room. The skylight
has a chronic leakage problem that is increased with
condensation buildup in the plant room.
Mildew grows on the inside sills of some south
windows from condensation buildup. An air-to-air heat
exchanger was in the plans but never installed. This
could have controlled the interior humidity.
The garage door was installed at a slope to match the
slope of the exterior walls. Gravity keeps the door from
sealing tight against the door stop and air infiltration is
evident.
Tips
It is important that a prospective contractor have a
good record of project management before a unique
project like this is undertaken. For the first-time home-
owner/builder, a homeowner/contractor pretraining
course could help decrease problems that arise between
the homeowner and contractor.
Funding
U.S. Department of Energy
State of Alaska
Grant Recipient
Advanced, Inc.
Box 2424
Fairbanks, AK 99707
$20,804
20,804
Underground greenhouse
• a maJor success
Everett Drashner is raising fresh vegetables and flowers
year-round despite frigid temperatures and little wind or
sunlight in Alaska's heartland.
His secret? An earth-sheltered commercial greenhouse
powered by wind generators and solar panels.
'Tm diversified," said Drashner, a retired construction
worker and owner of Wind-N-Sun-Enterprises. "I raise
cucumbers, tomatoes, peppers, squash, all kinds of
herbs, some flowers , greens of all kinds, lettuce, beets
and dill. The whole project is working better than our
fondest expectations."
Drashner's enterprise is on the Denali Highway some
miles east of its junction with the Parks Highway. It's
near Old Cantwell, about 210 miles north of Anchorage
and 160 miles south of Fairbanks.
"In this area you can't grow very much outside in
summer because we're 2,000 feet up and it can freeze
11 months out of the year;' Drashner said . 'That's why
the emphasis is on greenhouses. And there's no doubt
t h at it can be done in the Interior. That it's feasible. We've
already had success:'
System Design
The building-44 feet long by 40 feet wide-juts out
from the south side of a sandbank overlooking Drashner
Lake. Only the greenhouse roof and south wall protrude
3
above ground. The structure also is divided in half into a
growing area and a work area, each of which is 20-foot-
wide-by-44-foot-long.
In designing the building, Drashner took a number of
factors into consideration, including:
Conservation of electrical energy. A 10 kilowatt wind-
powered generator produces electricity for direct use
and storage in batteries. The power is used for lights,
fans, pumps and heating water in a 1,000 gallon tank;
batteries supply power when the wind is not b lowing.
Conservation of heat. The entire greenhouse was
designed as a large heat sink. Smaller heat sinks within
the building include a 1,000-gallon hot water tank; a
sauna; a three-tiered sand floor in the greenhouse
heated by pipes in the sand carrying hot water; two
plant watering tanks w i th a total capacity of 350 gal-
lons; a septic tank; an emergency battery-charging
engine; and, an emergency coal-fired furnace.
Use of new materials. Some of the products and
materials used were new to Alaska, and few had been
tested in Cantwell 's rigorous climate.
Knowledge gained through 25 years of underground
building experience in the area. Before the greenhouse
was started, the Drashners had been living in an earth-
sheltered house with two tunnels leading to out-
buildings. They a lso had developed an earth-sheltered
barn. When it was completed, the greenhouse also was
connected to the house by a tunnel.
Little sunlight. During the shortest days of the year,
between December 21 and 22, there are only three
hours and 42 minute s between sunrise and sunset at
Cantwell's latitude of 63 degrees north and 148 degrees
west.
Construction
Excavation was done in May, 1981, followed by
erection of con crete block wall s during June.
The ground under the flo or was covered with six-milli-
meter Visqueen, a la yer of sa nd, and three-inch foam-
glas. Two thousand feet of three-quarter-inch polybu-
tylene pipe was laid over the foamglas so hot water could
be pumped throughout the building . The pipes also heat
three terraced sand beds in the greenhouse.
All the walls were heavily insulated on the outside
with three-inch foamg las. Sheets of Tuffak-Twinwall , a
brand of double wall polycarbonated glazing material ,
was installed on the south wall, ceiling a nd on the top
sec tion of the end walls in the greenhouse. Nine inches of
fiberglass also were added to insulate the ceiling.
Interior surfaces were paneled with Wafer-Weld , and
painted white . An aluminum reflective material also was
installed on some of the walls to e nhance li ght reflection
for photosynthesis during low-light days.
A 1,000-gallon water tank was lowered onto its cradle
before the roof was finished and covered with a foot of
sand. A cement floor was poured in the work area before
freeze-up . And 10 tons of lignite coal was stored in the
building.
Performance and Problems
Overall, Drashner has been very pleased with his com-
mercial enterprise. He's been able to harvest two crops of
vegetables between March and December, and raise
flowers such as begonias (which require littl e light )
between December a nd March.
Drashner also has considered putting rabbits in the
greenhouse, although he says animals can cause frost
build-up on the south wall glazing.
One problem, however, has surfaced. The greenhouse
conserves heat so well that Drashner has to find new
ways to prevent the building from overheating on hot
summer days. A lthough operating at capacity, the solar
fans were not sufficient. He said opening vents, doors
and windows did not help much.
"As long as the wind is blowing, we can cool it down;'
Drashner said. "It's when there's no movement of air that
we have overheating. But we hope to have it shipshape
by the spring of 1985. Basically, the thing is done, but
we have to finish the refinements, which takes some
experimenting."
4
Modifications and Tips
Based on the greenhouse's performance, Drashner
believes s everal modifications would be beneficial. These
include plans to:
M o dify th e solar co llec tors. Redesign the system so
that extra heat can be used to warm the outside ground
adjacent to the greenhouse for planting during spring
and summer. By thermosyphoning, warm water can
be ci rculated through t he earth in pipes without using
electricit y. The sys tem will be virtually maintenance
free since it will automaticall y start operating when the
sun returns in February.
M odify the emergency coal furnace. Origi nally,
Drashner planned to build a large elaborate coal fur-
nace surrounded by sand. But he discovered that the
furnace was not needed because his pot-bellied stove
was able to keep the 16,000-cubic-foot greenhouse at a
cozy 50 degrees-even when it was minus 40 outside.
He plans to improve t he sto ve by adding a coil water
jacket which will be connected to the 1 ,000-gallon
water tank. He also will wrap half-inch copper tubing
around the stove's mid-s ection . The cold water will
thermosyphon from the bottom of the water tank
through the coil to the top of the hot water tank when
the stove is hot. It will act as a back-up to the wind
generators.
Imp ro v e tempe rature control and increase humidity.
In stall larger photovoltaic panels which will increase
the speed of ventilating fans and turbines. In addition,
Drashner is fashionin g an evaporative cooler and
equipping it with an adequate DC motor.
Bo ost power. Install two more four-kilowatt w ind
generators to supplement the 10-kilowatt generator.
The additional power will be used to heat the 1 ,000
gallon water tank.
Funding
State of Alaska
U.S . Department of Energy
Grant Recipient
Wind-N-Sun Enterprises, Inc.
Everett Drashner
Mile 131 Denali Highway
Cantwell, Alaska 99729
$ 24,760
24 ,760
5
The greenhouse roof (above) before backfilling. A view of the
interior of the Drashners' greenhouse (middle). A so la r-
powered rotary turbine w as used in the design (bottom).
1 want to live as soft I O I
upon the earth as I can' V
(Editor's note: At press time, this project was still
under construction.)
Jerry Brown, seeking to live as se lf-sufficiently as
possible, is building a solar-energy-heated, earth-
she ltered home in Southcentral Alaska.
"I've had a specific five-year plan during which I
wanted to see how self-sufficiently I could live," says
Brown, a former junior high school music teacher. "I
wanted to see how much an individual could divorce
himself from the economic sys tem. I was wondering how
much I could cut down on what I spent and on what I
made:·
Brown's solar-heated home is four miles north of
Palmer on Soapstone Road, about 45 miles north of
Anchorage in the Matanuska Va lley.
The home, which he hopes to complete by the fall of
1984, is on top of a wooded, five -acre gravel hill about
300 feet above the valley floor. It has good southern
exposure.
Brown hopes that the knowledge he gains from his
project w ill be of some assis t ance in developing low cost
housin g for people living in rural A laska.
"''m interested in developing those things that will
actually help and are low tech," he said.
More importantly, Brown wants to make as little
impact on the environment as possible . "I want to live as
soft upon t he ear th as I can," he said.
Design
The two-bedroom concrete b lock home, which has a
sleeping loft, is 32 feet wide and 40 feet long. It also has
a bath and a four-foot by six-foot fireplace in the center.
The front of the house, which protrudes from the
ground and faces south, is made of vertical thermo pane
glazing. A south-facing clerestory with three by four feet
of glazing will be installed below the roof.
Underground, the concrete block is insulated on the
outside with two inches of polystyrene . The south side
(40 feet ) is a ll windows. There is a clerestory with sleep-
ing lofts behind it. The bathroom and bedrooms are
across the back. Otherwise, it is all open to make it easier
to heat.
This projec t sought to answer four main questions:
• Will the thermal dynamic advantages remain the
same (a nd will it cost less to build an underground
h ouse) if the six-foo t excavation around the
structure is not backfilled, and a superinsulated
roof is extended over the excavation to a concrete
abutment? This construction method eliminated
cost of backfilling; allowed building with any
material , since it doesn't have to stand the weight
of backfilling; and enabled the excavated area
(600 squ are feet ) to be used as a dry storage and
root cellar.
• Can a concrete b lock and firebrick stove burn
trash and garbage by adding large amounts of
outside air to the c h amber? Can these tempera-
tures be stored efficiently in water tanks located
in the fireplace and in the concrete b lock walls of
6
the structure? Can a house be heated sufficiently
with this stove by firing it up once or twice a day?
Does t rash burn better loose or compacted? Can
hot air from the solar collector windows be stored
in the water tanks? These questions are still under
stud y.
• Will this type of simplified hot air co ll ector con-
tribute the greatest amount of available sola r heat
to the home? It consists of a standard double-
g lazed thermal window with a single sheet of glass
mounted two inches inside the window, open at
the top and bottom. "Space blanket" curtains are
hung between the glazing, foil side out. T hey can
be closed to prevent light and heat coming into the
structure but heat can still be co llected, tran s-
ferred to the highest point of the building and
blown down across the fireplace water tanks.
• Can reflection of light into a structure increase
heat? Can interior heat be m agnified and con-
troll ed by reflec ting light with venetian blinds
on wa ll s? To determine whether this is the case
crushed white gravel or quartz will be spread
under the windows outside the structure; a ll
interior walls will be painted dark brown to
absorb heat; Venetian blinds will be mounted over
them (lowered and angled various degrees to
reflect heat when necessary); and ground floor
windows will have homemade awnings that are
adjustable.
Construction and Modifications
Brown began building his home in May, 1981, devel-
oping and modifying designs to improve its efficiency
and to reduce costs.
The concrete blocks were poured solid to provide
more mass for heat storage. Rebar was placed every 16
inches vertica lly and every three courses horizontally.
Brown doubled the amoun t of steel he p lanned to install,
for greater protection again st earthquakes.
A steel 'T' beam was used in pl ace of a glue-lam
wooden beam because of its low cost and availability.
The beam, spanning leng thwi se across the middle of the
building, will be covered with two layers of half-inch
sheetrock for fire protection.
The fireplace also was redesigned . The chimney was
ex tended into the firebox to prevent smoke from billow-
ing up the hot-air flue. The firebox will be made of sheet-
metal and lined with firebrick . A drawer bin w ill be
added below the grate to catc h falling ashes. Brown
enlarged the outside air duct to four inches to enhance
air flow. And, the air holes in the lower fireplace were
enlarged to 18-inches-by-18-inches to boost circulation.
In the roof, Brown p lans to use two-by-twelve-foot
roof joists and to insulate with 12 inches of fiberglass and
two inches of styrofoam.
Brown a lso plans to save money by installing the
i
windows upright with a 90 degree angle instead of trying
to place them at a 77-degree tilt. Trying to s lant the
windows at the more acute angle would have cost more
for an additional heat-collection gain of o nly three
perce nt by Brown's calculati~:ms. Moreover, a two-inch
s pace will separate the :xten~r thermal ?la~s fro~ the
interior side of the glazmg to 1mprove a1r c1rcu latwn .
Floor vents beneath the windows have been enlarged to
enhance air flow.
A second wall behind the clerestory windows also was
removed and the loft extended to the windows to cut
costs and improve heating efficiency. Vents were placed
in the side walls of the loft to allow hot air to escape.
Because there was not enough space wher:e heat could
gather after the inner clerestory wall was eliminated, the
loft above the bathroom was removed. Heat that collects
there will be blown across the water tanks.
Finally, a six-foot square arctic entryway was rede-
signed to provide more room inside the home.
Tips
Brown has several suggestions from his experience,
including :
• Check on whether federal taxes apply to the grant;
these taxes can be an unexpected, unwelcome
"cost :'
7
• Don't rely on donated labor from friends . People's
li ves change, they move and th ey are busy with
their own projects. P lan on paid labor for any-
thing you can't do yourse lf. It is cheaper and
faster in the long run. But when contracting for
labor, check references.
• Consider refusing the grant if you are offered only
a portion of what you requested, unless you have
independent resources to see the project to
fruition.
• Discuss your plans with friends and people in the
building industry. They may have information
that w ill save you time and money. Building
supply houses w ill supply roof load fac tors, beam
sizes and just about anything else you need .
• When buying supplies, check all the lumber yards
and supply houses for prices. Don't buy a11 your
materials from one place. Prices vary a lot. Take
advantage of sales, but only after comparing the
sale p r ice w ith regular prices.
Funding
State of Alaska
U.S.Department of Energy
Grant Recipient
Jerry Brown
P.O. Box 374
Palmer, Alaska 99645
$ 7,032
3 ,014
These are the walls of an earthsheltered house Jerry Brown is
building near Palmer (/eft).
ATTACHED GREENHOUSES : ...
Fuel bills down,
vegetable crop up
Try planting an outdoor garden in Petersburg . It's a
drenching experien ce.
Each year more than a 100 inches of rain pelts this
small Southeast Alaskan community, which is on
Mitkof Is land between Juneau and Ketchikan.
But gardener Alice Grant has discovered a unique
solution to this perplexity. She a nd her husband,
Herbert, built a 190-square-foot, solar-heated green-
house onto their home in 1983.
"I s truggled along trying to garden outside," says
Grant. "But it was so discouraging that putting things in
a greenhouse appealed to me."
Thanks to the greenhouse, she now enjoys harve sting
strawberries, beans, peas, onions, tomatoes and other
vegetables virtually year-round w ithout having to worry
a bout getting wet outdoors. It's also a convenient place
to raise rabbits and chickens and to dry firewood.
And the Grants have been able to slash their heating
oil bills in half by recycling warm air from the green-
house into their home.
"It's been a big boost to the house," says Grant, who
also works as a gardener raising saplings for the U.S.
Forest Service. "It's already performing well:'
System Design
The Grants decided to build their greenhouse where it
could get the most sun-on the southern side of their
rectangular, 60-foot-long by 24-foot-wide h ouse.
The greenhouse, 24 feet long by eight feet wide,
encloses the front door and two bedroom windows.
"Wh enever the sun does shine we open the windows
and front door and the heat from the greenhouse wi ll
come right into the house;' says Alice . "We use half the
amount of oil we used before:'
The greenhouse roof, built of plywood and insulated
to R-30, was formed by extending the aluminum roof o n
the Grants' house by eight feet. The roof was built a lo n g
the lines of the ex isting roof to make it easy for the snow
to slide to the ground. The east wall was built of ply-
wood and two-by-fours and insulated to prevent heat
loss .
Sliding glass patio doors were used for the south and
west walls instead of the slanting glass panes, that are
usually pictured on so lar greenhouses. Research showed
t hat at Petersburg's latitude the vert ical wall would be
more efficient if it were able to capture th e maximum
amount of solar energy w he n the sun is at a low angle-
during the spring, fa ll and w inter. Daylight varies from
about six hours in December to about 21 hours in June.
Cost comparisons showed that ready-made patio
doors were cheaper than buying the glass and frames.
The sliding doors, which came with screens and locks,
were easier to install. And they also can be opened and
closed for ventilation.
Originally, the Grants intended to build a concrete
foundation, but local building codes would have re-
quired pilings to support the concrete, at a cost exceed-
ing the entire project.
8
So they built the foundation on two feet of shotrock
fill , consisting of gravel, rock and earth. Sill plates of
pressure-treated lumber six inches wide a nd 12 inches
high support the wall s.
The floor of the greenhouse was laid with polyethy-
lene over the shotrock; covered with fo ur-inch rigid
polystyrene insulation a nd half-inch plywood; and filled
with rocks up to the door-sill. A top layer of garden
earth smooths out the walkway. All seams, openin gs and
cracks were caulked and insulated to prevent heat loss .
Performance
Beginning on February 1, 1983, bedding p lants were
sown, incl uding tomatoes, lettuce, cucumbers, Brussels
sprouts, broccoli, squash, and flowers . Daytime temper-
atures inside the greenhouse were averaging SO to 60
degrees; nighttime temperatures were averaging 35 to 40
degrees. Outdoor temperatures averaged 35 to 40 degrees,
and many nights were below freezing. The hours of day-
light began getting long, gaining fi ve minutes per day.
The crops grew nicely and were transplanted outside
in late April and early May. The tomatoes, kept in the
greenhou se for the full season, flourished. Lettuce, gree n
onions and radishes, which were grown in flats, kept the
Grants furnished with fresh sa lads daily from April until
October.
"We don't get a big bountiful harvest, but we get
enough to munch on and keep us s upplied with salads,"
says Alice.
Flowers grown in hanging baskets provided fresh
blossoms for Thanksgiving. There were even fuch sias
blooming on Christmas day in spite of three weeks of 10
to 20-degree weather.
The greenhouse also has been used as a place to brood
baby chicks, which the Grants used to do in their living
room. Pet ducks acted as slug control until the birds
outgrew the g reenhouse space and began munching on
the salad greens.
Pet cats , dogs and rabbits have been shel tered in the
greenhouse during bad weather. The greenhouse a lso is a
great p lace to dry firewood and store pet food.
Heat recycled from the greenhouse is saving the
Grants money. Before building the greenhouse, they
were spending about $1,232 (1984 prices) on 1,200
gallons of oil per year, and about $210 for six cords of
wood.
But now the Grants use only about 600 gallons of oil
annually, because of the solar greenhouse and a more
efficient woodstove that only uses four cords of wood.
That's a savings of $613 on oil and $70 on wood.
Another s urprising feature about the greenhouse is
that it never overheats. During summer, its aluminum
roof shades the plants from the hot sun. The highest
recorded temperature was 86 degrees. On the same day
that conventional plastic greenhouses needed to be
cooled by electrical fans and vents, the Grants' solar
greenhouse required no electricity.
I Problems and Modifica tions
There have been some minor p roblems with the roof
leaking and insulation getting soaked, but these were
easily fi xed.
Originally, the Grants planned to place bl ack, painted
water drums in the greenhouse to provide thermal mass
by absorbing heat and releasing it as the temperature
dropped. However, the drums leaked and took up so
much space that they decided to use just six 30-gallon
drums. In addition, they also placed 100 one-gallon,
plastic milk containers (eac h filled with water tinted
black) around the potted p lants for thermal mass.
Tips
The sliding doors a ll ow various degrees of ven tilati on
as well as four different exits from the greenhouse into
the garden. The sliding feature eliminates the problems
of swingin g doors .
Plan ti n g in buckets makes plants portable. They can
be turned toward the sun, tall ones move d behind s h orter
ones, and dise ased plants removed. It is m uch neater
than permanently ins talled beds.
9
Hooks on the cei lin g are convenient for hanging
baskets of flower s or t ying up tall p lants.
Water and fertili zer are mixed in a garbage can, and
heated by the sun before being appli ed to the p lants.
Different mixtures of fertil izer are put in different cans
and labeled.
Pegboards on the house wall a re handy for hanging
tools, etc.
Recycled wire book racks for paperback books can
be fitted with small pots to use vertical space. The racks
rotate to give a ll the p lants exposure to the sun.
Some sort of thermal curtain or shutters might be
made for ni ghttime use. This greenhouse has none to
date, but they would prevent more heat loss at n ight.
Funding
U.S. Department of Energy $4,294
Grant Recipient
Alice Grant
P.O. Box 1143
Petersburg, A laska 99833
Sliding glass d oors (/eft) enclose the f ront of Alice Grant's
greenhouse.
Greenhouse more than
an indoor garden
Tucked away in Pedro Bay on th e north east end of
Iliamna Lake, some 150 air miles southwest of A n chor-
age, is Norman Aaberg's solar greenhouse .
The greenhouse was added o n to Aaberg's home, one
of a handful of dwellings in this Bush community of
about 50 people.
'The greenhouse was to serve as a source of heat year-
round, fo r starting a nd growing vege tables, and for
wood (fuel ) storage during the winter months," he said.
'The project has proven a real asset:'
Design and Cons tru c tion
Construction of the greenhouse (eight by 24 by seven
feet high in size ) began in mid-1981 when Aaberg started
expanding his home.
Originally, Aaberg planned to excavate a one-foot
space under the h ouse for an air space. Heated air from a
solar panel on the back wall of the green house would
flow up thro ugh the collectors into the house. Cold a ir
on the floor a t the opposite s ide of the house would drop
through vents in the fl oor and return to the greenhouse.
There is no electric utility in Pedr o Bay, so the system
was designed to work naturally with no electricity. Bu t
he abandoned this plan because the ground was too
r ocky a n d he could not excavate enough space for an air-
tig h t system under t he house.
He also used two-by-six planks to save money and
time in building the floor instead of pouring concrete. So
far, the wooden floor has worked fine.
10
T he west wall of the house, which abu ts the east wall
of the greenhouse, was covered with half-inch COX
p lywood. This d idn't work out very well because t he hot
air and moisture weathered the wood too quickly.
The lower half of the longer west wall and the short
south wall are insulated with g lazing a long the upper
half . T he greenhouse is built on the west side of the
house as a windbreak to provide protection again s t
prevailing winds from that direction .
Foam in s ulation was applied o n portions of wall s
covered with T1-11. Luci te sheets were used for the roof,
a lthough the roof was ti nned where it joined the main
h ouse.
Trim was added and the exterior was painted and
weatherized. Several 52-gallon oil dru ms pain ted b lack
and filled w ith water were installed as heat-coll ecting
thermal mass inside the greenhouse. Wall vents a ll ow
warm a ir to circulate from the greenhouse into Aaber g's
livi n g quarter s.
The p lanned solar panels were not install ed because
they were n o t needed, Aaberg said.
Performance
The g reenhouse has exceeded expectations and is
proving functiona l in all respects, according to its
builder. A nd it's saving Aaber g mon ey by reduci n g his
heating b ill s. His 2,200-square-foot home is well insu-
lated, b ut it d oes not have any o ther energy-saving
devices . Since building the greenhouse, t h ough, he's only
T h is Ped ro Ba y greenho use (/e ft ) is als o us ed as a sh op.
(
J
)
had to burn 4 1Jz cords of wood and 380 gall ons of
heating fuel.
In short , the greenhouse conserves heat in w inter. And
it has supplied a ll the heat needed for the li ving quarters
during late spring, summer and early fall.
The greenhouse also was a good place to dry out fire-
wood and it provided Aaberg w ith additional work
space in winter.
Tips
Actual use of th e greenhouse prompted Aaberg to
make a few suggestions for improvements.
• The roof should be strong and steep e nough to shed
snow. Instead of Lucite, consider using plywood and
other material for the roof. A lso, use rubber "w iggle-
board" instead of wood for e nd-sealing corrugated
Lucite.
Greenhouse first step to
energy self-sufficiency
Mark Garrett wants his home in Anchorage, Alaska,
to be as energy efficient as possible so he added a solar
greenhouse.
And he's enjoying it.
'Tm currently growin g lettuce, peas, beans, spinach,
carrots, radish es, bell peppers and onion s;' says Garrett,
adding that he's harvested several crops a lready.
The greenh ouse helps keep his h ome warm year-
round, and its garden beauty is a pleasant contrast to
Anchorage's long w inters.
"My goal is to create a small home comple te ly depend-
ent on its own design for en er gy," says Garrett. 'This
initial (greenh ouse) step is t he beginning of that project:'
Design
The south-facing solar greenhouse is 10 feet wide by
36 feet long, featu ring 280 square feet of double-paned
Filon brand glazing. It uses insula ted sh utters and 1 ,500
gallons of water as a thermal mass.
The foundation, an extension of Garret t's home, is
ma d e of concrete blocks stacked five coarse high . The
centers of the concrete blocks were filled with tightly
packed polyurethane beads. The floor was insulated
w ith two inches of Insulfoam brand polystyrene.
The north wall o f the green house a bu ts the house so
that excess heat from the greenhouse can be ventilated
into Garrett's home, helping to reduce his home heating
bills.
Both the east and west wall s are opaque and built on
two-inch by eight-inch framing. The wall s are padded
w ith six inches of fiberglass a nd covered with thermoply
for an insulation value of R-25. Sheets of T1-11 siding
were p laced on the exterior. The roof, insulated to R-30 ,
is made of wood.
The ceiling and a ll the opaque wall s were covered with
eith er white or foi l surfaces to balance the light inside the
greenhouse. At night, the insulating shu t ter s are folded
down to cover the glazed south wall. T he two-foot-wide
by four-foot-long shutters, which provide a n R-10 insu-
11
• Do not connect t he clothes dryer ve n t to the green-
house. During the winter, moisture created by the
dryer froze to the Lucite ce iling.
• Install proper ventilation to ensure that the green-
house doesn't overheat in the winter.
Funding
State of Alaska
U.S. Departmen t of Energy
Grant Recipient
Norman Aaberg
P.O. Box 8
Pedro Bay, Alaska 99647
$2,000
2,000
lation value, are hinged at the base of the wall.
Temperatures are electronically monitored. When t he
temperature rises to 75 degrees, a thermostaticall y
co n trolled blower com es on, pulling h ot air from the top
of the greenhouse ceiling into the sealed therma l storage
area. The water a b sorbs some of the heat, a n d the cooler
air is ci rculated back into the greenhouse through an
opening at fl oor level.
Heat stored in th e water is g raduall y released into the
greenhouse at night. When the temperature drops to 65
degrees, a blower is ac ti vated and fans warm air from the
thermal storage into the greenhou se.
Inside the g reenhouse, Garrett built an 18-foot-long
by three-foot-wide plant bed to a depth of two feet.
Holes were built into the bed's con c r ete retaining wall s to
a llow excess water to drain into a sump.
Tips
Garret t found t hat several procedures worked well for
his needs and recommends that others might:
• Ins tall flourescent li ghts in the greenhouse between
November and February to overcome poor w inter
sunlight.
• Use five-gallon plastic jugs filled with water for
thermal mass. The 1 116-inch thickness is sufficient
to a llow for heat exc hange.
• Use Filon 502 brand greenhouse glazin g; it transmits
li ght well even though it is not transparent. The
greenhouse plants turn only sli ghtly toward the
south glazing because of the defusing effect of the
fiberglass a nd reflecti ons of the north wall.
Funding
U.S. Department of Energy
State of Alaska
Grant Recipient
Mark J. Garrett
3636 Knik St.
Anchorage, Alaska 99503
$1 ,613
1 ,613
12
i nside Mark Garrett's greenhouse,
both vegetables and people thriv e
(above left and right). The race gets
underway (a bove) to complete con-
struction before w inter; (at left), the
g reenhouse in progress.
·'
J
J
..
J
J
)
Greenhouse overcomes
severe climate
Location
This project was designed to demonstrate the feas ibil-
ity of cons t ructing and operating a relatively low-cost
attached sola r greenhouse in a rural Alaskan commu-
nity. Dillingham, the site of this project, is a community
of about 1,700 people on Bristol Bay, a region of ver y
hi gh transportation and energy cos ts, with a relatively
severe climate and short growing season . Rising fuel,
transportation, a nd food costs hit residents of rural
A laska harder than they do people in urban areas.
Among the most cost effec tive measures for reducing
costs appear to be energy conservation; use of local
building materials; use of sun, wind , and wa ter e n ergy;
and increased production of local foods. An attached
solar greenhouse appears to co n tribute to energy eff i-
ciency and self-sufficiency in three major ways. First, it
serves as an extra "s kin" to reduce heat loss from a
portion of the house . Second, it produces ex tra h eat to
supplemen t the home's heating system; and third, it
a ll ows pr oduction of food that would o therwise not be
possi ble to g row in the climate of Southwestern Alaska .
An additional benefit , in view of th e small size of
many homes in this region, is the ex tra sp ace which an
attached greenhouse provides.
Design and Construction
Steven Behnke's greenhouse was attached to the south
wall of the basement of his new small, well -in sulated
(R 32 wall s, R 50 ceiling), two story house . A "pit"
design, in which the g reenhouse was partially sunk into
the ground, was used so that th e surro unding earth could
provide extra mass and insulation, and so that the struc-
ture would fi t beneath the south-facing windows of the
first floor of the house .
Although the original proposal ca ll ed for glazing to
be installed a t an angle of about 30 deg rees from the
vertical , the fi na l desi gn used a 45 degree angle . This
ena bled a simpler roof design, and provided more ex-
posure to the sky. The diffuse li g ht characterist ic of the
cloudy Dillingham summer climate made this greater
exposure de sirable for plant production.
The greenhou se was desig ned to cover the entire front
wa ll of the basement, which is 26 fee t long, and to
ex tend out eight feet from the basement wall. The first
floor of t he house is cantilevered two feet over the base-
ment, and so for ms part of the greenhouse roof.
The original proposal ca lled for the use of concrete for
the wall s of the greenhouse . A framed wall of t reate d
wood was substituted due to the high cost of concrete in
this area. The wall s were built of treated two-by-fours
on 24-in ch ce nters a nd half-inch all-weather plywood.
Spacers (two -by-twos) were insta!Jed horizontally on the
interior of the two end-walls to accommodate extra
insulation a nd provide a nailing surface for an interior
fi n ish of h alf-inch plywood. The wa ll s were in s ulated
with five inches of p o lystyrene, and the foundation
perimeter was insulated with two inches of polystyrene
to a depth of two feet below floor level.
13
A double laye r of reinforced fiberglass glazing .040
millimeter in thickness was install ed instead of the orig-
inall y planned inner layer of Teflon film. The 49 Vz -inch-
wide roll s of glazing were installed on two-by-four
rafters on 24-i n ch centers. Treated o ne-by-two-inch
wood battens were used as spacers between the layers.
They also hold down t he top layer. S ilicone sealant was
appli ed along all joints. This system was simple to install
a n d has worked well.
The greenhouse is normally entered through a door
from the basement of the house. This door p ermits ci r-
culation of wa rm air from the greenhouse into the base-
ment. A small , homebuilt door in sula ted with p o lyst y-
rene a ll ows access to the outside so that material s can be
brought into the greenhouse more conveniently, but in
the colder months this d oor can be sealed off to reduce
heat loss. Originally, an airlock entry to the greenho use
from outside was planned, but the d epth of the excava-
tion made thi s impractical.
The floor of the gr eenhouse consists of two feet of
gravel; the center portion of the floor is covered with
paving bricks.
Performance
T he greenhouse captures considerable heat from the
sun . In spring, 1982 (February-April) as the days length-
ened and the sun rose higher, the greenhouse made
a major contrib u tion to he ating the basement, which
is normally he a ted with a woodstove. During these
months t h ere are norma ll y a high proportion of cloud-
less days compared to late summer and fall , which are
n ormall y cloudy and wet. From l ate April through June,
woodstove fires were needed only after severa l days of
rainy weather.
The greenhouse tended to overheat on hot summer
days and h ad to be vented manually to the outsid e .
Automatic vents and fans to circulate heated air into the
basement would im prove efficiency.
The h ouse was h eated by the greenho use through the
summer and into late October on a ll sunny days. By
November 1 , the d oor between the greenhouse and the
base ment was kept closed because little heat was being
gained.
The wa ter storage t anks added to the greenh ouse rela-
tively late in the summer of 1981 appeared to decrease
daily temperature changes.
From November to February the greenhouse is used to
store and dry firewood , a nd to dry laundry. These uses
provide major benefits, si nce Dillingham has a wet
climate, and it is often difficu lt to obtain dry wood.
Clothes dryers in Dillingham cost from $8 to $40 per
month to operate . Drier wood improves the efficiency
of heating.
In March a nd April the greenhouse is used as a warm
play area for children, and planting is started at this
time . Soils are prepared for planting tomatoes and
cucumbers. Flower s, brocco li , cauliflower, lettuce, and
other plants are started in the greenhouse to be trans-
planted into the garden later. From May through Octo-
ber the greenhouse produces tomatoes and cucumbers.
Because the house is heated with wood (supplemented
by oil) it is difficult to assess the exact contribution of
the greenhouse in heating. Fuel oil bills averaged $50 per
month in winter and about $5-$10 in spring, summer,
and fall based on a noticeable contribution to heating
the house (records from September, 1982 to May, 1983).
Public Information
The project contributed to local and regio nal knowl-
edge about energy alternatives in several ways. During
construction and after completion the project was
visited by more than 30 local residents. This provided
opportunities to discuss concepts and construction
methods with a wide range of people . The project was
described on a program about local energy issues on the
Dillingham radio station, KDLG , in January, 1982. This
program briefly touched on the benefits and methods of
construction. The greenhouse was a lso discussed and
s hown on Alaska public television throughout the state.
A program produced by Alaska Review, of Independent
14
Public Television, Inc., entitled En ergy Alternatives for
Alaskans, featured both the greenhouse and the h ouse to
which it is a ttached. It showed construction techniques
and described the benefits of such structures in rural
Alaska, where fuel and construction costs are high. A
tape of the program is avail able from the State Film
Library.
Funding
U.S. Department of Energy
State of A laska
Grant Recipient
Steven Behnke
2130 Second Street
Douglas, Alaska 99824
$1,176
1 ,176
Th is greenhouse (left) is attached to Stev en Behnke's salt box
house , loca t ed in D illingham.
Plate 1 Morning light (above) hits grantee Wind-N-
Sun's greenhouse near Cantwell. A view of
the west side of the greenhouse (middle left).
Advanced Inc. of Fairbanks developed a
unique dome design that fits well with the
winter scenery (bottom left):
Plate 2 Western exposure of Norman Aabeqfs
homesite at Pedro Bay is perfect for an at-
tached greenhouse (below). (At right) Paul
Robinson of Fairbanks chose a detached
greenhouse to supplement his outside vege-
table garden. A strawberry patch hangs on
the wall of the greenhouse in McGrath built
by MTNT, Ltd. (bottom).
Plate]
A scenic view of Unalaska (top) from Charles
Vowell's methane digester. A workman inspects a
bread box solar collector sponsored by the
Municipality of Anchorage {left). Grantee Dois
Dallas added a solar collector to heat water for this
Fairbanks home (above).
Plate 4 A view of the Portage Creek fish counting
camp operated by the Alaska Department of
Fish and Game near Bristol Bay (top right).
john Greene's cabin in Eagle (middle right)
makes good use of a wood fired boiler. Steve
Smiley's wind energy system is raised near
Homer (below).
Plate 5 An overshot wheel built by Robert Nelson
generates power at Thayer Lake (left). A
collapsible pipeline transports water to
wheel (top). Chester Johnson of Valdez
performs the weekly greasing of his hydro
turbine (above).
Plate 6 A view of the hydraulic ram assembled by
Don Chaney in Petersburg. Louis Butera (at
right) of Eagle River stands beside his micro-
hydro project. A larger scale hydroelectric
project was undertaken by Richard Matthews
of Port Armstrong (bottom).
Plate 7 The Mitkof Lumber sawmill in Petersburg
studied the feasibility of wood gasification
(above). Perry Hilleary of Trapper Creek
demonstrates one of the unique features of
his Bush refrigerator (middle left). A gray
water heat recovery system was designed
and installed by Richard Runser of Wasilla
(bottom left).
Plate 8 David Newcombe mounted a Stirling engine
on his home boiler tank in Wasilla (top
right). A rankine cycle engine was used by
Arthur Manning in his hydrothermal freon
electric plant (middle right). The Kenny
Lake Community League mounted a solar
collector on their library to help reduce
energy costs (bottom).
Solarium an asset
during Alaska winter
Larry Cline is taking t he experience he learned from
building a solari u m and apply ing it to o t her homes he's
constr ucting in Anchorage, A laska.
'Tm starting to b ui ld fo ur pl exes a nd I'm incl u ding
ha ll ways on t he south sid e w ith lo ts of windows;' says
Cline, w h o owns A laska C a r pen ter and Construction
Company. "And I'm getting my me thod of' doing this
from what I've learned here (on his solarium):'
Cline says a solarium enhances the beauty of a home,
helps reduce fuel bills, and p r ovides a warm retreat
during Anchorage's cold winters. "A solarium aesthet-
ically enhances the design of a house:· he says. "It's
a warm place to be even when the sun's behind the
clouds. You have so much darkness up here in the winter,
but the solarium seems to change all that :• He's even
grown several crops of tomatoes, lots of flowers and
he's thinking about adding catfish to his solar water
containers.
Design
The solar ium was built on t he 10-foot-w ide by
26-foot-long second floor deck of C line's h ome. Pa r t of
the solarium, a 1 0-foot-wide-by-14-foot-long room, a lso
was b u ilt on t he ground fl oor.
T he so la riu m, wh ich is o n the south-faci ng side o f the
h ome, increased t he in terio r s pace of h is home to 2,637
15
square feet. It will gather the sun's wa rm th, store it and
circulate it through the rest of the home.
T he wall s, covered o n the outside with Tl-11 plywood ,
are made o f two by six inch frami ng wi t h fiberglass
insulat ion, p o lyureth ane a nd drywall for a n insulation
val u e of R-27 . A d ouble two by 10 inch b eam ac ts as a
b race w ith t he house.
T he roof , w h ich has an R-50 insulat ion, is made of
two by eigh t inch rafters with six inches of styrofoam
and a layer of polyurethane. lt was sealed with tar.
Cline also installed triple-pane windows. The outside
and inside panes of the one-and-three-eighth inch thick
windows are standard three-sixteenths-inch thick glass.
Between these two outer layers and separated from them
by two air spaces is a third center "pane:' This center pane
is not glass but a special "Heat-Mirror" made of a
visqueen-like material which is coated on one side with a
t hin copper-tin oxide film. This film allows sunl ig h t to
enter a building, b u t effectively blocks over 50 per cent of
a ny heat rays fr om leaving.
Most sola r e nergy heating systems req uire t ha t the
w ind ows be insulated w ith sh utters o r therma l c urtai n s
dur ing periods o f d a rk ness o r n o so lar ga in . These
w ind ows don't require that ex t ra ins ul a ti o n , says Cline.
M uch of t he capture d heat wi ll be s tored in t he fl o or
Larry C lin e buil t a solarium (/eft) on t he second fl oor deck of
his south-facing home.
thermal mass composed of a rockbed atop two-inch
layers of Insulfoam brand insulation capped by a layer of
concrete blocks placed sideways, so that the block cores
form a series of channels for air ducts and a cement slab.
Registers along the outside perimeter of the floor allow
heat to rise into the solarium.
Heat sensors located throughout the solarium monitor
the internal temperature and control a fan. When the
temperature of the solarium reaches a predetermined
point, the fan is activated, drawing the warm air into the
house. The fan speed increases a s the temperature of the
solarium increases.
Once inside the house, the home's furnace ducting will
be used to transport the warm air throughout the struc-
ture. One of the existing cold air return registers for
the home heating system is located near the ceiling peak
in the highest area of the house, ensuring that air is
circulated evenly throughout the structure.
16
Tips
Cline offers several suggestions in solarium-building:
• Make sure all seams around the window and walls
are caulked well . Also, it is important to caulk both
sides of each window pane.
• Do not install triple pane windows unless the center
is coated with copper tin oxide.
• Install flourescent lights to supplement poor w inter
sunlight.
• Before building a sola rium, take time to fig u re out
how the air will circulate and incorporate the air
movement in the design.
Funding
U.S. Department of Energy
State of Alaska
Grant Recipient
Larry Cline
2820 Kingfisher Dr.
Anchorage, Alaska 99502
$3 ,155
8,363
Rustic comfort:
Solar-heated log cabin
Jack Segle drives a truck most of the time. But in his
spa re time he's building himself a solar-heated log cabin
near Palmer, in Southcentral Alaska.
"I was intrigued by solar energy," says Segle, adding
that this is the first time he's built a solar heated home. "I
hope to provide a working example of the cos t effective-
ness, the simpli c it y and the immediate availability of
passive solar space heating."
So far, he's grown several crops of vegetables in the
attached greenhouse, and used it as a work space during
winter.
Segle says he still has to install a planned sod roof, a
duct to help circulate heat from the ceiling to the floor of
the house, and an earth berm around the wall s.
'1t isn't complete yet," Segle says. "But it appears to be
working just fine :'
Design
Segle's two-story log cabin is 16 feet wide by 24 feet
long. A bedroom and storage sp ace are on the top floor,
above the first-floor li v ing room and bath.
Most of the heat is provided by a solar greenhouse,
which was added onto the south wa ll. The greenhouse,
funded by the s tate grant, has 120 square feet of double-
paned glazing; the panes are spaced four inches apart.
The home also has 56 s quare feet of d o uble-paned
windows, all on the south side.
17
In addition, Segle installed a fireplace equipped w ith a
fan to supplement his heat durin g winter, when Pioneer
Peak prevents direct sunlight from shining on his home
for about 45 to 60 days.
Heat is transferred f rom the greenhouse into the home
by convection, using air as a heat transfer medium.
Natural thermosiphoning, combined with the building's
design , creates a continuous air loop within the home .
Air moves from the greenhouse up to the second story
bedroom and storage space. Eventually, Segle plans to
install a galvanized air duct to channel hot air from the
second story to a crawl space area beneath the first floor.
Segle's planned heat storage consists of 94 .8 cubic feet
of concrete in the north wall of the greenhouse, 50 cubic
feet of concrete in the greenhouse floor, a nd 226 cubic
feet of rocks contained in wire pens beneath the first
floor li ving area.
Furthermore, he plans to build an earth berm against
t he north, east and west walls of his h ome.
Funding
U.S. Department of Energy
State of Alaska
Grant Recipient
Jack Segle
SR Box 7476
Palmer, Alaska 99645
$1 ,250
1 ,250
The fron t of ja ck Segle's cabin (ab ove left) fea tures a s olarium.
This v iew of the back of the house reveals the v ario us methods
of construction which were used (above right).
Building an air
tight environment
Imagine an electrically heated home that will s tay cozy
and warm for two days w ithout power when outside
temperatures are 20 below.
Sound impossible?
Not to a group of Wasilla High School students who
spent two school years (1981-83) designing and building
an energy-efficient three-bedroom home in Wasilla, a
growing rural community in the Matanuska Valley just
north of Anchorage.
The Mat-Su Va lley is among the fastest growing
regions in Alaska . Population increased from 18,000 in
1980 to more tha n 30,000 in 1983; assessed valuation
increased from $836 million to $1.3 billion in the same
period. Demand for land, housing, basic services, and
consumer products has been fueled by a measurable
"m igrati on" from the Anchorage area to the rural, less
populated valley and its environs, especia ll y in the
Wasilla area.
For the students, home construction ski ll s could prove
invaluable as their communit y grows.
"We got to do eve ry thing ~ said Ken Smith, one of the
students who hel ped build the home. For his part, "I got
involved in the plumbing and the electrical work the
most:' he sa id .
This was the sixth house built by the high school's con-
s truction trades program. Each year about 65 studen ts
enroll in one of three courses: architecture and drafting
in terior design or carpentry. Each class contributes to
building the home.
Students who want to be in the carpentry class must
prequal if y a yea r in advance in the woodshop class.
Instructor Richard DeBusman and assistant Gary Rich-
ardson work full time with the hands-on carpentry
course, in volv ing studen ts with each facet of the home's
actual construction.
Students in the drafting class prepare an a rchitectural
design using criter ia provided by the Vocationa l Advisory
Board of local citizens. Other students design the home's
interior.
The advisory b oa rd selects the de sign a nd makes sug-
ges tions. But it 's up to the s tudents to complete the home.
Eventually, the students sold the energy-efficient, one-
story house for about $119,000. Money from the pro-
ceeds went back into the program to purchase materials
for new homes and perpetuate the program .
The all-electric heated home also is saving energy. In
February of 1984 it only used 2,180 kilowatts, for
$178 .83; and in July it averaged 576 kilowat ts, or a
$58.23 electric bi ll .
"I like the house real well~ said purchase r Arnold
Warnke, who works on the North Slope in the Arctic as
a plant operator for Sohio Alas ka Petro le um Company.
"But I think it would have been better to put in either
gas, propane o r hot-water baseboard heat. The electric
heat is real nice, it 's just real expensive to operate. I think
gas would be ideal for this type of home'.'
, SUPER INSULATION
19
Design
The 1 ,600-squa re-foot, super-insulated home has a
master bedroom with a walk-in closet and bath, a li v in g
room, kitchen , dining room, two other bedrooms, a
garage, a four-foot crawl space, and electric heating. It
doesn't have a wood stove because the home is so a ir
tight that a stove would not be able to get enough draft,
Warnke said.
The home has two, two-by-four walls spaced n ine
inches apart to provide 18 inches of fiber glass insulation
for an R-60 rating. A 10-millimeter polyethylene vapor
barrier was applied to the inside of the inne r two-by-four
wall.
Additional two-by-three furring strips were nailed
over the vapor barrier. The extra furring allows for all the
wiring to remain inside the vapor barrier without
making any holes through it except those for exterior
e lectrical outlets.
The ceiling was insu lated with 21 inches of blown-in
fiberg lass. Arkansas-type trusses were used to extend the
outside wall t wo feet above the inside ceiling to provide
the space over the outside walls for insulati on .
Extra care was taken in the crawlspace to insulate the
rim joist spaces. Seven inches of fiberglass were placed
between the joists above the p late and then a cut piece of
.5-inch urethane board insulation was caulked into
place. An aluminum surface vapor barrier was placed
over the urethane board.
Special wood shutters, in sulated to more than R-10 ,
have been built to slide in-and-out of wall pockets. The
shutters s li de out to cover the interior face of the double-
paned windows to help keep heat from escaping. When
the shutters are clo sed t hey block light from entering the
room.
An air-to-air heat exchanger, known as Metsovent, is
another house feature. It is capable of recapturing up to
60 percent of the home's heat as inside air is replaced
with fresh air from the outside; it is part of the kitchen
range hood.
Vents for carrying warm air from the two bathrooms
a re ducted through the heat exchanger. The incoming air
is warmed by natural heat convection on its way to the
li vi ng area.
"As the warm a ir leaves the house, it's warming the
incoming air;' Warnke sa id . 'The superin sulated house is
so tight that you need some type of ve ntilation or even
radon gas will build up'.'
There also is a unique arctic entryway. It is an
enclosed insulated s pace with two doors, good for
storage of boots, rain gear and winter garb.
Performance
Overa ll , Warnke ha s been satisfied with hi s superin-
s ulated home . He sa id it was built well , a nd it doesn't
lose much heat .
Warnke, however, has had some problems with the
shutters warping. Apparently, the shutters expand and
contract, making it d ifficu lt to open and shu t th em . T hey
are being replaced by t he manufacturer.
Warnke, a lso, said he wou ld have p r eferred heating t he
home w it h more inexpensive natural gas heat th an with
costly electric heat. Nat ura l gas, however, was not avail-
able when the home was being built.
When it becomes available, Warnke says he may
conver t to gas heating.
20
Funding
U.S. Dep artmen t of Ene rgy
State of A laska
Grant Re cipient
$ 4 ,886
11,402
Matanuska Bo rough School District
Construction Trades Class
P.O . BoxAB
Palmer, Alaska 99645
·~.
Ric ha rd De Busman m akes a point (/eft) about const ruction;
(above) the sou th s ide of th e house.
Home's 'shell' holds heat
Making sure that a home loses as little heat as possible
is an important concern for Alaskans living in the
Interior, where winter temperatures can plummet below
minus 40 degrees.
Terry L. Duszynski, a construction consultant from
Fairbanks, has superinsulated his home and added a
sunspace.
Moreover, the appropriate technology grants he
received also provided funds to make two half-hour
video tapes about the project. The two-part series, enti-
tled "The Great Alaska Warm-up;' has aired on public
television in Alaska.
"We have the ideal test in g climate for energy conserva-
tion techniques," said Duszynski. "We are much more
aware of the performance of our houses due to the
extreme cold winter conditions:'
Essentially, Duszynski superinsulated an older, two-
story home by adding a new roof and outer wall s. He
filled the space between the new outer wall and the old
inner wall with insulation.
"When the project was completed, a totally new super-
structure was in place around the old house and th e
whole house was wrapped with a thick layer of fiber-
glass;' Duszynski said. "It's doing what it's supposed to do:'
The new insulation has helped Duszynski slash his
electric heating bills in half to about $100 a month.
"The house definitely is warmer in the winter and
cooler in the summer," he said . "It's more comfortable to
live in. There are fewer drafts and no major temperature
swings:'
"It re a ll y is easy to retrofit an ex isting house;' said
Duszynski.
Design and Construction
Duszynski superinsulated a two-story cedar home to
R-60. The home, built in 1965, sits in a hillside so that its
basement walls are surrounded by earth on three sides.
The house only had 2.5 inches of fiberglass insulation in
the walls, rated at R-7. The ceiling was rated at R-19.
Duszynski built additional outer walls and a new roof
around the existing house. He filled the 16-inch gap
between the inner and outer walls with fiberglass insula-
tion. ''What you end up with is a s uperinsulated cavity
around the house," he said .
The new 16-foot-high walls, made of two-by-four
framing, were built on top of a new concrete footing.
The lower half of the wall was covered w ith all-weather
wood panels w ith an outer face of polyethylene for
waterproofing.
The upper half of the walls were covered with four-by-
eight sheets of half-inch-thick plywood. Wood shingles
were nailed over the plywood.
Two layers of n ine-inch-thick fiberglas s were in stalled
between the 16-inch cavity between the outer and inner
wall. One layer was p laced horizontally, like stacked
bricks and the seco nd layer was installed vertically
between the new wall studs.
The double-paned glass windows were left in their
21
original position and a box was made to meet the new
wall. The box sides were painted a creamy white to
reflect light through the w indow into the house.
A sheet of six-millimeter polyethelene was laid across
the original cathedral roof, and 12-inch truss-joists were
placed across the polyethylene and nailed to the roof .
The space between the trusses was filled w ith 12-inch
batts of fiberglass. Two-by-four purlins were n a il ed
across the truss-joists, and 18-gauge sheet metal roofing
was fastened on top of the purlins.
Suns pace
The sunspace, built on t he south side of the house, is
14 by 28 feet and two stories high .
A six-millimeter layer of polyethylene was laid over
the ground, and four inches of blue Styrofoam insula-
t ion was placed on top of the polyethylene. A four-inch-
thick slab of concrete was laid over the insulation. The
perimeter of the concrete slab, however, was raised to
eight inches with post supports for the sunspace
s tructure.
The sunspace was made by bolting together six-by-six
post and beam framing. The roof was framed with two-
by-12 boards, and planked with two-by-four purlins.
Duszynski used three-by-18-foot-long hi rib steel roofing
with some 12 inches of fiberglass insulation. Finally, h e
used tongue and groove pine siding of one by six feet to
complete the structure.
The window panes, which were 46 by 76 inches, were
made from sliding glass door replacement glass. All win-
dows were caulked on the interior to prevent heat loss.
Heat from the sunspace is vented into the house by
opening the doors and windows on both the first and
second floor of Duszynski's home.
There a lso are vents on the east and west sides a long
the top of the window panes to exhaust heat during the
summer. Eventually, Duszynski plans to install auto-
matic vents w h ich would open when the temperature
reaches 80 degrees during the summer when th e heat is
not needed in the house .
Performance
Duszynski says both the home and the sunspace are
performing as expected. The home is not drafty and he
has not had any noticeable temperature differentials
between the living room floor and t he loft area.
Better yet, his winter electric heating bills have only
averaged $100 above his typical summer bills.
Much of the project was desig ned as it went along.
Although he had a basic idea of what was to happen, the
problems encountered were not totally known, Duszyn-
ski said.
The first problem that occurred was the visqueen on
the exterior of the all-weather wood foundation. This
material began to s li de down the wall as the ground
around the house began to settle . He had to dig two feet
down all along one side of the house and add more vis-
queen to protect the wall from ground moisture. Duszyn-
ski has since found several alternatives. One is to cover
the foundation with asphalt coating prior to the visqueen
for additional protection, A second is to put another
layer of visqueen over the first, but not fasten it at the
top. This allows it to slide down along t he first one as the
ground settles. Third is to use a new superstrong, nylon
reinforced material which will not break loose from the
top and slip.
The sunspace also functioned well. But he discovered
that there was never any extra heat available for the
home between November and mid-February, months
where sunlight is limited to four hours daily.
"I am not sure yet just how much heat is able to be
produced by this sunspace, but during the next year I
hope to monitor with instruments the temperatures
throughout the sunspace;' he said. "It's doing what it was
intended to do."
Video Tape
The appropriate technology grant also provided funds
to make two half-hour video tapes, which were pro-
duced by KUAC television at the University of Alaska-
Fairbanks.
One film is a documentary of some of the steps
Duszynski took in super-insulating his home, and the
other describes how Duszynski built his sunspace. The
video tapes have been shown on public television in Fair-
banks, Juneau and Anchorage.
Among problems the film crew had were unpredicta-
ble weather, coordinating everyone's schedules for film-
ing scenes, and getting good footage.
22
'There was one day when we worked all day on just
five minutes of footage and felt that none of it was
usable;' Duszynski said. "But most of the time it was fun
as well as work:'
'The super insulation program has been aired about
five times in Fairbanks and the sunspace film once,"
Duszynski said. "So I'm happy with the result. It said
what I wanted it to say:'
Tips
Duszynski has several suggestions for similar projects.
They include:
• Put an asphalt coating over the foundation before
adding the polyethylene for additional protection
against moisture. Buy polyethylene with nylon
threads in it.
• Do not use any type of thermal storage for sun-
spaces in far north climates because it usually
decreases the available heat from the sun for the
house in early spring. A wooden, insulated floor
would allow all additional solar heat to be directed
into the house as soon as it was available.
• Be prepared to s pend more time making a video
tape than expected.
Funding
U.S. Department of Energy
State of Alaska
Grant Recipient
Terence L. Duszynski
Star Route Box 10356
Fairbanks, Alaska 99701
$ 5,759
31,277
Chickens provide
greenhouse heat supply
Chickens can keep a solar greenhouse warm when the
thermometer plummets to sub-zero temperatures in the
Interior of Alaska.
But it's a risky proposition .
Just ask Elizabeth Hart, author, photographer, mother
of three , and owner of a roadhouse in Ruby, Alaska,
about 2SO miles west of Fairbanks and SO miles east of
Galena .
She tried to heat her solar greenhouse with a flock of
13S chickens. And it worked-until ammonia from the
chicken wastes started killing the plants and sub-arctic
temperatures began freezing the hens.
The setback, however, has only temporarily post-
poned Hart's dream of someday supplying this Yukon
River community of 2SO residents with fresh eggs and
vegetables.
"I definitely plan to try it again," says Hart. "I still
think it can be done . If I had a family flock of a dozen
chickens and a small greenhouse-I think it would
work:'
Design
The two-story greenhouse was built on pilings and
insulated to about R-40. The chickens were housed on
the first floor, and the plants were placed upstairs . Heat
and carbon dioxi de from the chickens was to supply the
needs of the plants above.
The 20-foot by 24-foot building was placed on a level ,
northern-oriented site because Hart was not able to
purchase or lease a south-sloping site.
Hart and two others with carpentry experience began
construction in the summer of 1982. They hit ice at
about one foot and had to use steam drilling to dig holes
for the wooden foundation posts, which were anchored
to the building with heavy bolts .
The walls were insulated to R-40 by installing sheets of
plywood , plastic, building paper and two sheets of
Thermax-brand insulation. The roof and floor were
padded with fiberglass, yielding an R-60 value, to
prevent the chickens from getting chilled while on the
floor or in elevated roosts. And the double-paned,
acrylic plastic windows were padded with a layer of
plastic for an added air envelope.
In addition, there were 18 inches of dry sawdust
placed on the floor in the 12-foot-by-24-foot chicken
coop area. The coop was furnished with nests, floor
feeders, waterers and roosts built on the wall from the
ceiling to the floor. Sawdust was added as waste accu-
mulated on the floor, creating a compost that helped heat
the building .
Thin aluminum reflective material was placed on the
white walls of the second-floor to enhance light reflec-
tion for photosynthesis. Flourescent lights were placed
over the growing beds, which were a foot deep and 2.S
feet wide. Similar lights were placed in the coop. Start-
ing in September, the lights were automatically turned on
at 6 a.m . and switched off at 8 p .m . Thermometers also
were placed in and outside of the building to monitor the
temperature .
23
GREENHOUSES
Performance and Problems
At first everything went well, despite the gradual drop
in temperature from 70 degrees to freezing. The hens laid
about a dozen eggs daily, the chickens gained weight,
and the three roosters woke everyone in Ruby earlier
than they wished.
But then it got really cold.
Unfortunately, the coop could not be maintained more
than 40 to SO degrees above the outside temperature. So
when temperatures outside the greenhouse plummeted to
minus 40 degrees-it meant the chickens froze in zero-
degree weather. The cold killed plants and hens.
"I was hoping that the chickens would be able to keep
the temperature up above freezing," Hart said. "But I
think the ceiling was too high . If I had lowered it, there
would have been less area to heat:'
Lack of sunlight compounded Hart's heating woes.
The sun is quite low in the winter because of the latitude
(64 degrees north) and hills to the south which block the
available light. In fact, no direct sunlight hit the green-
house between November 1S and January 1S .
As a last resort, Hart installed a heater and lowered the
ceiling a few feet, which raised the temperature about 10
degrees . But it wasn't enough . More chickens died and
the rest stopped laying eggs.
"I feel that a coop has to be at least 40 to SO degrees for
egg-laying, and I could not provide this temperature and
also be cost effective ;' she said. 'The electric bill was
several hundred dollars a month and that was too much .
So I gave away the chickens for meat:'
Ammonia gases released from the chicken wastes
proved to be another handicap. Even with a foot-thick
layer of fresh sawdust, the ammonia vapors accumulated
so heavily at times that it poisoned Hart's tomatoes,
beans, lettuce and flower plants within hours.
"It was terrible," Hart said. 'They'd just turn black and
die . It was like a stab in the heart . I had gorgeous flowers
in there. Absolutely gorgeous . Some lasted a week. And
some lasted a day. But the chicken ammonia killed them:'
Hart learned from the Cooperative Extension Service
in Fairbanks that a similar ammonia problem had devel-
oped when another person tried to heat a greenhouse
with pigs . The extension service told her that a limestone
filtering system could remove the poisonous gases. But
Hart couldn't afford the system .
Instead, she installed a fan, which helped disperse the
gases, but directed excessive airflow onto the plants.
Another person suggested that she turn the compost
heap more frequently. She tried this too, but found that
turning a compost heap 12 feet wide by 24 feet long by
18 inches thick was a lot more work than she had
bargained for.
Tips
Hart says several things could be done to improve on
her experiment including:
• Lowering the chicken coop ceiling to three to four
feet except in the immediate areas of feeding /water-
ing and roosts.
• Placing dropping pans under the roosts (instead of
sawdust) so these can be emptied.
• Installing a t ight wood stove with a protective mesh
guard around it. Buy at least two cords of wood to
last seven months.
• Installing an automatic fan system in the greenhouse
and a fan in the coop. A lso, experiment with a filter-
ing system so that the heat-but not the ammonia
gas-would circulate around the plants.
/
24
She also recommends Rhode Island Red chickens as a
breed that can withstand Alaskan winters.
Funding
U.S. Department of Energy $14,260
Grant Recipient
Eli zabeth A. Hart
861-C Yak Estates
Fairbanks, Alaska 99701
A side v iew (/eft) of the two-story greenhouse. A flock of 135
chickens (bottom left) produces a fowl odor. At bottom right,
grantee Elizabeth Hart at home. Bel ow, the Yukon River flows
near the Hart homesite.
Waste heat increases
• groWing season
Two hundred miles northwest of Anchorage, near the
limits of navigation on the Kuskokwim River, lies
McGrath, a small community of about 500 year-round
residents. But more than just a Bush community,
McGrath is also the commercial and transportation hub
for the entire Middle Kuskokwim region.
Like many remote co mmunities, McGrath is plagued
with high energy costs and a lack of fresh fruits and
vegetables during the winter months. Early in 1981,
Larry Wiggins (Executive Director of MTNT, Ltd , at the
time), started a program that he hoped would reduce
both of these problems. MTNT, Ltd. is the local for-
profit Native organi za tion for the area and owner of the
local elec tric utility.
Realizing that 70% of each gallon of diesel the utility
bought was wasted up the exhaust pipe or heat s the air
from the radiator, Larry Wiggins looked at ways to cap-
t ure wasted energy. Such a waste recovery system would
benefit the community by improving the utility's
performance. Soon a heat recovery system and heat
transporting pipeline was in stalled. This system is used
to heat the buildings (residences and office s) of the
Federal Aviation Administration (FAA) in the ce ntra l
business district. The savings in heating fuel, alone, has
amou nted to almost 40,000 gallons a year.
With the heat recovery system in place, Wiggins began
the second phase of his p lan, the construction of a com-
mercial greenhouse that could grow vegetables year-
ro und. This greenhouse would be heated with recovered
waste heat and would supply both McGrath a nd the
other villages in the reg ion, bringing in additiona l
income to MTNT.
The project in volved designing and constructing the
greenho use structure , developing a way to supply and
control the recovered was te heat to the g reenhouse,
deve loping a horticultural program that ensured maxi-
mum usage of the greenhouse, and determining the over -
all economics of the project.
Design and Construction
The greenhouse is a 42-by-84 foot clear span building
situated near the McGrath power plant along an east-
west axis. This axis is due to the low sun angles experi-
enced at these latitudes, even during the summer
months. Inside, the g reenhouse is divided into five
separate growing areas, as well as a potting room, a
sales/office area, and an emergency boiler/heat
exchanger room.
One of the major problems confronting the designers
was permafrost. The greenhouse design called for
heating pipes to be implanted under the soil of the
growing benches . Heat radiating downward could
quickly destroy the entire project by melting the perma-
frost , caus ing the foundation to shift. To protect the
permafrost, a thick gravel a nd sand b ase was laid, fol-
lowed by two inches of s tyrofoam insulation. The styro-
foam is covered by another two-inch protective layer of
25
sand , and high capacity drain pipes were installed
around the perimeter.
Primary heat is throug h four, five-tube grids laid out
in the bedding soil to provide (four) separate , but
controllable, heat zones. An aquastat switch controlling
a small circulating pump keeps each zone at the set
temperature . The aquastat allows small variations in
ground temperatures for optimum growing conditions.
To avoid the risk of heat recovery system failure and to
reduce the chances of freeze burn if doors were left open
during the winter, a secondary back-up heating system
was installed. These overhead mounted units use heat
supplied by an emergency boiler and are rated high
enough to keep the greenhouse warm even with total
failure of the underground heating system .
The two-by-six framed, double-glazed structure has
two four-by-five foot ground level openings at each end
of the greenhouse which are used for summer ventila-
tion. These openings are manually operated as the need
exists. Two louvered openings and large exhaust fans are
also mounted high in the ga bles at each end of the
building to remove heat without causing drafts at the
plant growing level.
A special "cool room" was built to provide optimum
growing conditions for new sprouts and budding plants.
This r oom was in sulated so that ambient temperatures
could b e closely controlled. A propane carbon dioxide
generator is also included in the cool room design.
The small potting room has a deep sink and ample
storage shelves and work spaces for potting new plants or
repotting seedlin gs.
The emergency boiler room (i n addition to the boil er),
has a heat exchanger and stora ge tank for warming the
40-degree well water prior to use. The water is heated to
a b out 70 degrees, fertilizer is added , and the mixture is
then applied to the plants using an efficient, automatic
drip watering system. Storage space also is available in
this room.
A 10-by-20-foot office is attached to the exterior of the
north wall. This office also is used for over-the-counter
plant sales and as a convenience to local residents.
Although th e original design did not include a rtifi cial
li ght, it was quickly determined that to make the project
economically feasible some form of additional li ghting
was necessary. The three-tiered growing beds were out-
fitted with flourescent grow-lights and metal h ali de and
sodium vapor lamps were mounted overhead, increasing
the growing area by 1,000 square feet. The additional
light also a llowed the addition of four hydroponic
growing tubes on the n orth wall. These tu bes, alone,
added almost a quarter of an acre of gr owing area, for a
total of about 4 ,200 square feet of surface area plus
room for 300 hangi ng baskets.
Performance
The greenhouse has been a resounding technical
success; unfortunately, the project was cancelled because
it had not made a profit during the first year of opera-
tion. Many reasons have been presented concerning the
.\L.-l ~~A n !·~''(l\JrW~ l''I::'~A.R J'
W.&. DE~T. OF 1NT!l.h10E
26
A view (above) of the interior of the greenhouse from the
mezzanine. (Bottom left), the exterior of the greenhouse. Heat
exchange piping (middle left) is located in the powerhouse.
r
I
economic woes of the greenhouse, including unforeseen
increased operating costs, poor marketing, size, and
poor initial planning. But it seems that community
priorities and perception may have doomed the project.
From a technical point of view, the greenhouse suc-
cessfully proved that fresh fruits and vegetables could be
grown year-round in the far north using recovered waste-
heat and artificial lighting. According to Harold Pills-
bury, greenhouse manager and horticulturist, the green-
house even exceeded commercial production elsewhere.
For instance, tomatoes yielded an average 33 pounds of
fruit per plant. Normal average in similar adventures is
22 pounds per plant, he said. Other difficult-to-grow
crops, such as cucumbers and peppers, sh.owed similar
productivity. However, since the operation was never
allowed to go beyond the experimentation stage, it is
hard to determine how profitable the greenhouse could
have been.
This is not to say that there were no problems with the
greenhouse. During initial shakedown it was found that
the aquastats were not controlling the soil temperature as
accurately as required. The aquastats were temporarily
bypassed and newer ones, with a maximum setting of
120 degres versus the 90 degree type on the originals,
were ordered to solve this minor problem.
Soon after applying heat to the four heat zones, it was
discovered that there was a heat overlap at the zone
edges. A narrow trench was dug between the zones and
the trench filled with strips of styrofoam. This effec-
tively cured the heat flow problem.
One last problem was discovered during the winter.
The cold weather caused a measurable drop in carbon
dioxide production from the propane generator. Heat
tapes and a temporary covering of the propane tank
easily corrected the carbon dioxide production problem.
27
The heat retaining ability of the greenhouse worked
better than expected. In fact, the six-inch dead air space
kept so much heat in that snow refused to melt off the
roof during the winter months. Since artificial lighting
is used and the structure was designed to handle the
additional load, the snow created no problems.
Conclusions and Results
There seems to be a common consensus that the
McGrath Greenhouse was a successful application of
appropriate technology. The problems associated with
this project seem more political than technical. Due to
the fact that the greenhouse was only allowed to operate
during the trial season and shut down before a commer-
cial market could be developed, the economic success of
the concept was never proven.
Because the project did prove that recovered waste-
heat from diesel powered generating plants could be used
to increase the growing season, it may be possible to
adapt the concept to other small villages and towns with
similar power plants.
For all of its technical successes, the McGrath Green-
house did prove that unless the community actively
supports a project, it will usually fail. Public support
would have forced management to continue with subsi-
dizing operating costs and actively pursue a market for
the product. The present management of MTNT, Ltd., is
doing just this. Although the greenhouse is temporarily
placed on the back burner, the organization is searching
for alternatives. Some suggestions have been to produce
a high value cash crop such as fresh herbs, or to limit the
growing season and thus limit operating costs.
Funding
U.S. Department of Energy
State of Alaska
Grant Recipient
$ 25,000
175,000
MTNT, Ltd. (McGrath, Takotna, Nikolai, Telida, Ltd.)
P.O. Box 104
McGrath, Alaska 99627
Greenhouse crop
supplements traditional
lifestyle
Two solar greenhouses built in Aniak are helping the
Kuskokwim Native Association extend the growing
season to eight months.
Now the association is able to start seedlings in the
greenhouses in March for growing fresh vegetables, cole
and root crops on a farm the association also operates.
The area is marked by temperature extremes, perma-
frost and a short growing season from mid-May to mid-
August.
'We've been growing tomatoes and cucumbers and
starting our seeds for cold crops and flowers~ said Walter
Overton, agriculture director for the Kuskokwim N alive
Association. "About the second week of June we transfer
it to our farm':
One of the greenhouses, a 150-square-foot-structure,
was built with funding from the Bureau of Indian
Affairs. The second, larger greenhouse, which is about
1,000 square feet, was funded partially with federal
appropriate technology grant funds. The greenhouse
grant, issued in late 1979, was one of the program's early
successes, despite a delay from weather at the start of the
first building season.
The greenhouse, farm and education programs spon-
sored by the Native organization will help take pressure
off the traditional hunting and gathering lifestyle, which
has been jeopardized by a growing population.
Almost all food, including fresh vegetables, must be
shipped or barged to Aniak, which is located at the junc-
tion of the Aniak and Kuskokwim Rivers. Freight alone
can inflate the price of food dramatically.
The association, however, is hopeful that this project
will help make the village a little more self-sufficient.
System Design
The greenhouse that was funded with AT grant funds
is 20 feet wide by 53 feet long. It has a concrete
foundation, a dirt floor, and a 10-by-14-foot arctic
entryway. '
The walls, Overton said, are eight feet high with two-
by-four-studs on the west and east walls. The north wall
has two-by-six-studs. The walls and ceiling have six
inches of fiberglass for an insulation value of R-19. The
exterior is covered with sheet metal, and the interior with
three-eighths-inch plywood sheets.
The 12-foot-high, south-facing wall is made of
double-paned fiberglass glazing spaced about 10 inches
apart, Overton said. It also has a three-foot-high south
sidewall constructed the same as the other walls. The
roof is covered with roofing paper.
To increase light reflection, the interior walls were
painted white. Fifteen, 55-gallon drums in the green-
house are filled with water for thermal mass.
All interior surfaces are covered with a polyethylene
barrier to prevent moisture from rotting the wood.
28
Overton said the association plans to install an oil-
fired stove shortly.
By comparison, the smaller greenhouse funded by the
Bureau of Indian Affairs has standard two-by-four wood
framing with plywood covering the interior and exterior
walls on the north, east and west sides. Six inches of
fiberglass provide an insulation value of R-19 to the
ceiling and to the north, east and west walls. The south
walls are made of double paned glazing with translucent
fiberglass. It has an arctic entryway about seven feet by
five feet.
Performance
Overton says both greenhouses are working very well
and are helping the Native association extend its growing
season to eight months.
The AT-funded greenhouse has even stayed above
freezing even when outside temperatures plummeted to
minus 40, according to the association. In fact, the heat
collection/retention of the structure is so good, that an
exhaust fan and shutter should be installed to provide
adequate ventilation.
Although the original plan called for a completely
passive solar structure, electricity for the exhaust fans
and grow lights was brought to the site. A road also was
added recently, to enhance travel to the greenhouse and
garden.
The group also had planned to install a 480-square-
foot reflective shield made of two-by-four framing,
covered with a lightweight reflective material (Alsinite)
on the south side. The shield was to be attached to the
roof with a hinge.
But due to high costs and questionable effectiveness,
the heat reflector shield was abandoned.
Problems and Conclusions
An extremely wet summer in 1980 delayed construc-
tion so much that only the gravel pad and cement foun-
dations could be completed that year. Workers hired
for the building season under an employment training
program spent most of their time in the classroom. The
original plan to complete the structure in four weeks
stretched out to two seasons; the greenhouse was com-
pleted in 1981. ·
Another minor problem was a low estimate for the
amount of gravel needed for the building pad. The
additional gravel for the greenhouse (added to the gravel
needed for the road) significantly increased the project's
cost. However, the increase was offset by having most of
the construction materials barged to Aniak rather than
delivered by costly air freight.
The Kuskokwim Native Association has had success
farming in remote locations. The Aniak Farm leases
about 160 acres from KNA at $1 per acre per year. This
property is used to grow vegetables and farm crops for
chickens, goats, and other livestock and for forest man-
agement projects. All p rofits a re returned to the farm.
With about 30 acres cleared a nd planted, this organiza-
tion looks to a future of self-sufficiency without loss of
cultural independence.
Funding
U.S . Department of Energy $16,534
29
Grantee
Kuskokwim Native Association
Box 106
Aniak, Alaska 99557
A view of the greenhouse built by the Kuskokwim Native
Association (left).
Construction plans
put on hold
The community of Kotzebue, hoping to grow fresh
vegetables, has been trying to build a solar greenhouse
for the past several years .
But they haven't had much success so far.
In 1980, the Kotzebue IRA Council (a village govern-
ment entity) received an AT grant to build the green-
house for a future supplemented food source .
The greenhouse is still incomplete however the frame,
plywood walls and roof were built and a few windows
were installed, but further construction has ceased, and
the building sits unused on community property.
The delay stems from site relocations and the loss of
the project manager. In fact, Kotzebue IRA manager Jeff
Hadley says the entire project may be turned over to
another nonprofit Native group for completion .
System Design
The proposed, rectangular greenhouse would be 24
feet wide by 30 feet long, standing 14 feet high at the
apex of its sloping clerestory roof .
Some 18 glass panes are planned for the south side of
the building to capture the most amount of light avail-
30
able in the late winter and early spring.
Solar heat will be stored in large water tanks inside the
greenhouse. Supplementary heating will be provided by
an oil-fired heater.
The council is planning to install movable insulating
shades to cover the glazing and reduce heat loss at night.
Fiberglass insulation will be placed on the walls .
Grow-lights will be added to provide additional light-
ing when needed .
Originally, the council had proposed to install a wind
generator that would provide some 60 percent of the
greenhouse's electrical supply, but this idea has been
dropped with the stagnation of the greenhouse con-
struction.
Funding
U.S. Department of Energy $21,200
Grant Recipient
Kotzebue I.R.A. Council
P.O. Box 296
Kotzebue, Alaska 99752
This greenhouse in Kotzebue (left) awaits completion.
Recycled tire rubber
provides thermal mass
Location
This passive solar greenhouse is located in Fairbanks,
Alaska on a flat plateau in the North Star Borough bowl.
Paul Robinson's central goal in this project was to
design a structure that could make use of recycled tire
rubber-material that otherwise would have gone to
waste from a nearby tire retreading plant. The project
was designed to enable such a greenhouse to be built on
flat terrain , rather than into slopes of hills as is common
in the Alaska Interior. The original proposal under the
Appropriate Technology grant program assumed that
black tire rubber would prove to be superior in
absorbing and holding heat , and would thus serve as an
efficient heat sink.
Construction
The detached greenhouse was built with a south-
facing wall of glass . The north wall (at the back of the
structure ) was layered with shredded rubber. The floor
of the greenhouse was above ground level , with layers of
shredded rubber placed beneath. Flower boxes also were
lined with rubber, with dirt on top for planting .
A hot water tank was suspended from the ceiling, and
vents were installed for cooling as necessary.
Performance
'The greenhouse has exceeded all of my expectations
in its performance;' said Robinson . "It seems perfect for
our Alaska climate; when the sun is high in the warm
summer months, the greenhouse can be kept cool by
simply opening the vents. In the spring and fall , the
greenhouse is much warmer inside than outside. In fact ,
keeping the structure cool is more of a problem on a
31
sunny spring day than in the middle of summer. This is
due, of course, to the design and the use it makes of
direct light in the spring and fall and of diffused light in
the summer. The project was in working condition in
May of 1982, and we made good use of it. We started all
of our bedding plants, and quite a few for several neigh-
bors and friends , in the greenhouse from seed. We grew
an excellent crop of tomatoes. The greenhouse is not
only a good growing environment, but also is a very
pleasant place to be;' he said .
"I have had one technical problem with the rubber.
Basically, it worked very well ; however, on some clear
and unusually warm days it did get too hot. I removed
the rubber temporarily and designed a system that will
enable me to move the rubber forwards or backwards,
depending on need.
"We used the greenhouse the first year until October
12. With a small heater we could extend our growing
season another month in each direction, although I
do not think we need to. The greenhouse produces so
much that we still have a freezer half-full of last year's
vegetables," said Robinson in 1983.
Funding
State of Alaska
U.S. Department of Energy
Grant Recipient
Paul Robinson
P.O. Box 60904
Fairbanks, Alaska 99706
$ 1 ,783.00
1,783 .00
Paul Robinson 's detached solar greenhouse (left) is shown here
under construction .
"The ground acts as
a very big radiator''
John Collette has the biggest tomato farm in the
Alaska Interior heartlands-thanks to a specially
designed solar greenhouse that heats the ground.
His secret? Maintain soil temperatures around 75
degrees by circulating warm antifreeze through pipes
buried in the quarter-acre lot covered by his greenhouses,
a commercial enterprise.
'The ground acts as a very big radiator;' says Collette,
who owns Happy Creek Greenhouses in Fairbanks. "It
throws heat off at night'.'
The design is so efficient that he is able to keep the soil
warm enough to produce cucumbers, bedding plants and
30 to 40 tons of tomatoes annually between early March
until November. The normal growing season is about 90
days in Fairbanks.
The design has proven successful. In fact, since the
first small, prototype greenhouse was completed from
the 1979 grant funds, Collette has added two more com-
mercial greenhouses using a similar design.
"It's working very well indeed;' Collette says. "It's
reduced my operating costs by a substantial amount. My
next venture will be to pump warm air through the
ground'.'
System Design
The entire system is dependent on pumping a 50/50
mix of hot antifreeze and water through plastic pipe
buried inside the greenhouse. The antifreeze is warmed
by a solar collector, which is supplemented with a coal-
fired boiler. An oil-fired unit heater also is available for
emergency or supplemental use.
The prototype greenhouse is 20 feet by 40 feet with a
rib structure formed of one-by-twos sandwiched together.
Two layers of six-millimeter, Monsanto 602-brand poly-
ethylene are attached loosely on the outside of the rib-
bing, separated by an air space that is maintained by a
very low pressure fan . This provides insulation similar
to thermopane glass.
The polyethylene can withstand temperatures of minus
40 degrees without cracking; and the air pressure keeps
the polyethylene taut.
The heart of the system is a 35-foot-long by four-foot-
high solar collector on the ground along the south wall.
The four-inch-deep solar collector is made of aluminum
roofing, painted black, with three-quarter inch base-
board fin tubing and polyethylene glazing .
A ceiling "squirrel-cage" fan also blows warm air that
gathers under the roof into the solar collector, which
32
helps heat the antifreeze solution circulating through the
copper baseboard tubing in the solar collector.
The antifreeze is pumped through the solar collector to
a set of plastic pipes buried in trenches in the floor.
There are 15 trenches, each 14 inches apart, across the
east-west length of the greenhouse. In each trench,
Collette put four layers of pipe, which are buried at
depths of 14, 18, 22 and 26 inches.
After circulating through the buried pipes, the anti-
freeze flows back to the solar collector via a hot water
boiler. The heater is used as a supplementary heat source
in fall and spring, when there is adequate sunlight but
snow remains on the frozen ground outside.
The heater runs whenever the ground or air tempera-
tures drops below a minimum growing temperature.
Plant growth also is enhanced with a carbon dioxide
generator. The unit burns propane, which emits carbon
dioxide and water vapor. By maintaining carbon dioxide
levels at around five times normal air levels, optimum
plant growth is achieved in the greenhouse.
A similar design was used to build two commercial
greenhouses, nearly 10 times the area of the AT grant
prototype. Each of these greenhouses are some 50 by 150
feet in dimension.
Performance
Collette says he's been pleased with the performance of
his greenhouse design. The system maintains ground
temperatures at about 75 degrees during his "extended"
growing system, which is warm enough to keep his
tomato crops thriving year after year.
Moreover, his two commercial greenhouses, are also
doing well. The produce sold in Fairbanks grocery stores
and the open air market are highlights of his success .
Funding
U.S . Department of Energy $9,484
Grant Recipient
John Collette
SR 20087-A
Fairbanks, Alaska 99701
Community greenhouse
provides example
Gardeners will soon have an opportunity to plant their
seedlings in a community-owned solar greenhouse in
downtown Fairbanks, Alaska.
The greenhouse, designed by the Alaska Federation
For Community Self Reliance Inc., should be ready for
the community by spring of 1985, says federation
spokesman Dick Farris.
It would have been ready by the summer of 1984,
exce pt that the organization had to relocate the project
after the borough decided to put a building on the old
garden site. The group plans to operate the greenhouse
from mid-April until mid-September.
"We envisioned the solar greenhouse as a place for
starting plants for gardening enthusiasts in the commu-
nity;' Farris said. "We also built the greenhouse as a
demonstration project to teach people in the community
how to build one for themselves," he said.
Design
The greenhouse is 14 feet wide by 40 feet long . The
south, west and east walls are made of double-paned
Filon, a brand of hard, translucent glazing material.
The eight-foot-high north wall is made of steel
roofing, backed by 3Vz inches of fiberglass insulation,
polyethylene plastic sheets and plywood.
The sloped roof, also made of Filon , rises to a 12-foot
apex. The north side of the roof was designed so that
blocks of polystyrene eight feet long by 1 Vz feet wide
could be installed on top of its two-by-four rafters. The
roof's south side slopes at a steep angle , and has a
2 1/z -foot-high nave wall.
A solar collector also will be suspended from the
ceiling. It is to be fabricated as a 30-foot-long by three-
foot-high metal tube cut in half lengthwise (into a half-
33
circle) and painted black for heat absorption. Polyethy-
lene will be stretched across the half-circle to trap solar
heat inside the metal apparatus.
The east and west walls of the greenhouse are hollow
with a one-foot-wide space between the inner and outer
walls to allow for air circulation.
There are also a series of four-inch-wide , perforated
drain pipes buried a foot deep in the ground floor. The
pipes, spaced one foot apart from each other, will be
connected to the east and west walls of the greenhouse.
A one-third horsepower fan will blow hot air down
the solar tube into the hollow east wall; the air then will
be channeled into the buried pipes. Excess , cool air will,
be forced up the hollow west wall .
Thermostats also will be installed to reg ulate the
temperature.
Design Modifications
Originally, the group planned to circulate warm water
through pipes buried in the greenhouse floor and sur-
rounding garden plots. The water was to be warmed in
the ceiling solar collector.
But this plan was abandoned because it was compli-
cated and would have been more expensive to install.
Funding
U.S. Department of Energy
State of Alaska
Grant Recipient
$5,533
5 ,533
Alaska Federation For Community Self Reliance , Inc.
P.O. Box 73488, Federal Station
Fairbanks, Alaska 99707
Th e Fairbanks community greenhouse is located on its original
site (/eft) along the Chena River.
A lesson in greenhouse
improvement
SAVE I High School is a vocational and technical
school located in Anchorage . The project to improve an
existing greenhouse structure was undertaken by
students, who earned credit for the project as part of
their high school curriculum.
Design and Construction
The original project proposal was designed to make
the school's existing greenhouse more energy efficient.
The students were to design the project, estimate costs,
purchase materials and implement the work.
'The situation that we were faced with was a green-
house covered with a single layer of corrugated fiberglass
sheets. There was a gas-fired furnace inside for heat . We
wanted to make the structure more energy efficient and
increase our growing season," said SAVE 's Jim
Cunningham.
"We first looked at where we were losing energy;
walls, ceilings, and door. Then we opened up discussion
for ideas on how we could cut down on the energy loss.
We decided that we would put a layer of visqueen on the
inside to act as secondary, 'inexpensive' glazing. This was
put on all four sides, ceiling and floor.
"Second, we looked at all the little places where we
were getting cold air seeping in (and hot air out). We
then insulated in those places as well as caulked with a
silicone sealant," Cunningham said.
They also took a look at where they might have addi-
tional energy losses. The students took a good look at
the north wall and ceiling. They decided that since there
35
was no sunlight coming in there, the areas should be
insulated. The students measured between each of the
two-by-four wall and ceiling studs and cut the expanded
polystyrene insulation board to fit.
Expanded polystyrene can be hard to cut evenly; there-
fore one of the students came up with the idea to seal the
material. They decided that a soldering gun would melt
through the polystyrene and seal the edge. (Care must be
taken in having the area well ventilated, since the fumes
a re toxic.)
Once the insulation was in place, plastic sheeting was
stapled in place for the second glazing. Along the top, a
series of wood one-by-two strips were used to keep the
visqueen from falling or ripping from the staples .
The students also decided that there was an energy
loss through the ceiling and roof during the winter. They
installed a series of bent nails in the ceiling rafters, from
which styrofoam sheets could be set into place as a drop-
in ceiling. This retained more heat inside.
The next phase was to redesign the plant beds. Stu-
dents set the plant beds on 55-gallon steel barrels painted
black and filled with water. These acted as a storage
medium to help extend the growing season by releasing
the stored heat. "We were also hoping that the release of
this heat under the plant beds might stimulate more
growth by heating the soil and the roots;' said
Cunningham.
Instructor' Jim Cunningham (below) taught his students how to
make their greenhouse more energy efficient.
"Looking at the project overall, the students and I have
learned about insulating, vapor barriers, heat storage,
construction, solar aspect and solar charting (summer to
winter angle);' he said.
Performance
The major points of energy conservation education
have been in the following areas, Cunningham said:
• Insulating the north wall and part of the north
ceiling. These areas are energy-losers and should
be treated or built as such. The students made the
comment that as you drive around the Anchorage
area, most of the greenhouses have clear or unin-
sulated north sides. This project's lesson could
apply to these structures.
• A second layer of glazing is much better than a
single layer. This is obvious, but the point we are
making is that a second layer of glazing can be
made of visqueen plastic which is inexpensive.
Since it is behind another layer of glazing, it is
protected somewhat from the elements such as the
wind and ultraviolet rays. Our second layer of
glazing (plastic sheeting) has been in place for
three years and is still in use.
36
• The third point of interest is the 55-gallon barrels
of water. We cannot calculate exactly how much
this has saved us in energy, but in any greenhouse
you need something to set plant beds on. What
better way than through the system we used? We
do feel that there was an energy gain and storage
through this method.
We feel that our retrofit of a standard greenhouse
should be used in most greenhouses that are in this area.
Most people are interested in putting together a green-
house that will not cost them a fortune, and be passive in
energy use.
Funding
U.S. Department of Energy $650
Grant Recipient
SAVE I High School
5300 A Street
Anchorage, Alaska 99502
Search for an energy-
saving window shutter
Developing insulated window shutters is a dream that
inventor Ed McGrath has been pursuing for severa l
yea rs.
"The project still goes on;' said McGrath in mid-1984.
He is a carpenter and former alternative e n ergy teacher at
Tanana Valley Community College in Fairbanks. "I can
report that it looks hopeful, but I canno t repor t a ny
successes'.'
T he b igges t obstacles facing McGrath a re deve lo p ing a
cos t effective design and preventing the shutters from
warping after inst allation.
"In every case that I've built a s hu tter, it's cost far more
t han the (cost of) heat lost through the w ind ow (w ithout
a shutter);' McGrath said. "But I'm s till worki ng on it ,
and I intend to keep working either until I ge t someth ing,
or u ntil it is clear that it just can't be don e -at least by
me :'
Design
Originally, McGrath hoped to build a cost-effective,
slidi n g shut ter which would slide up and down over the
exteri or face of a wi ndow. His plans called for installing
an ex terior seco nd "window;' making a sa ndwich-ty p e
asse mbly.
The sh u t ter was made of a two-inch-thick panel of
rigid insulation called Thermax. The panel was covered
wi th Dacron aircraft fabric cloth and heated so the fabric
would shri n k to fit the panel.
The fabric a lso was painted to preve nt its d eterioration
by ultra violet li gh t. The edges of t he panel were lined
with al umin um.
'The shutters were tailored to the wi n dows a nd they
varied in insulation from one-and-a-half inches to three
inches;' McGrath said.
T he sh utter co ul d b e pulled with plastic coated a ircraft
37
WINDOW INSULATION
cable either manuall y o r wi th a motor. But McGrath sa id
he ha d difficu lty sealin g the hole t h at he drilled through
the wall to install the sh utter cable .
McGrath tried using electric motors to raise and lower
his shutters, but was u nable to come up with a design to
keep the shutter up when the motor was turned o ff. The
weather-stripping caused excessive resistance w hen t he
sheeting was d rawn or raised between the glass panes.
"It turns out that gettin g a two -way, reversi ng motor
wit h a break on it is a ve ry expensive proposit ion,
cos ting a couple hundred dollars for a little bitty m otor;'
he sa id. '~lso , sliding and sealing are ant ago nist ic to
each other. It was a b asic problem. Make a tight seal and
the s h utter doesn't want to slide any more:'
Experimen ts with an inexpensive hydraulic air ram
system didn't work, ei ther, because he co uld n't prevent
leakage.
McGrath, however, had some success install ing a
fou r-foot-square demonstration shu tter for an Energy
Efficie n t D emonstration exhibit at the Tanana Valley
Fair. But the demonstration project was not as energy-
eff icient as h op ed.
'Then after eig h t months, it didn't work at a ll any
more;' he says. 'The sh utter in sulation panel had warped
and there was nothing to do about that:'
Summary
Despi te failures and dead-ends, McGrath has learned
a lot about building, installing and using in sulated
window sh u tters.
"I looked at houses constantly, trying to see if my shut-
ter would fit o n their windows;' says McGrath. "In far
too many cases, t he answer was no. I became disillu-
sioned with the slid ing shutter. I found that they were
The energy demonstration building (ab ove left) at the Tanana
Valley Fairgrounds. Ed McGrath d em onstrates his window
s hutter (ab ove right).
also much more expensive than I had imagined. It wasn't
the cost of the shutter, but of the box /glass frame that
protected it from the weather:'
But he isn't giving up.
In fact, he's been working on a new concept, for which
he built a "model" out of cigarette packs, cardboard and
tape.
McGrath has had to set his invention aside, but has
predicted that, "I will build a cheap successful shutter.
And as soon as I have something to say, I'm going to
Polystyrene beads to
prevent heat loss
A special insulation system to reduce heat loss at night
is planned for a greenhouse in McCarthy, in the Interior
of Alaska.
"We are proposing to construct a passive solar, energy-
efficient, attached greenhouse with a usable growing
season of March through October," said Jerry Miller,
w ho lives with his wife Judy at May Creek, a rural
village near the Kennicott Glacier.
"We w ill incorporate a bead wall type system which
involves blowing polystyrene insulating beads between
the glazing at dusk and sucking them back out at dawn
using a hand operated pump," he said. "We want to dem-
onstrate how such a system can be energy efficient,
practical and inexpensive to build and maintain:'
Unfortunately, the Millers had not completed their
greenhouse by mid-1984 due to several unforeseen set-
backs. The couple, for example, had to move to May
Creek after the original project site at McCarthy was
threatened by flooding three times within six months.
Health problems further delayed construction of the
greenhouse. And, by spring 1984, only the rough ground
work and initial foundation had been completed.
"Site preparation has begun and foundation work is
currently underway," said Judy Miller.
System Design
The proposed greenhouse is 14 by 36 feet and will be
attached to the Millers' cabin. The south-facing wall w ill
have nine four-foot-wide, double-paned bay windows.
The windows will be installed at a 77 degree angle to
take advantage of the low s un in the spring and fall.
During nights when there is heat loss danger, the small
polystyrene beads will be placed in between the double
paned windows.
The Millers plan to draw the beads out of the windows
with a hand operated pump each morning.
38
write a little book telling how to build these shutters, and
then my work will be done':
Funding
U.S. Department of'Energy $2,375
Grant Recipient
Ed McGrath
P.O. Box 73876
Fairbanks, Alaska 99707
Rocks stacked as plant bedding support will store heat
collected by the passive solar greenhouse. Exces s heat
gathered by the greenhouse also will be vented into the
M iller home.
Two automatic vents, on the east and west walls,
would be used to remove excess heat. They will begin
operating when the temperature reaches 65 degrees.
A wood stove will provide backup heating for the
greenhouse in the early spring and late fall.
To supplement the carbon dioxide le vel in the green-
house, rabbits will be kept in s ide; and chickens a lso
could be quartered in the greenhouse during the coldest,
darkest winter periods. This would eliminate the need for
additional heating for the chickens, and light from the
house could stim ulate year-round egg production.
"Instead of wintering our chickens, 10 to 15 birds, in a
separ ate hen house, we plan on sectioning off a part of
the attached greenhouse," Judy Miller says. "Right now,
we compost leaves and fireweed with nitrogen-rich
chicken manure to build our soil humus and nutrient
lev~. This process always stops in winter. But we will
continue this in our greenhouse."
The couple also may plant some dwarf fruit trees and
such crops as tomatoes, cucumbers, squash, peppers,
beans, lettuce, carrots and spinach.
"We hope to develop a year-round system of opera-
tion;' says Judy Miller. "We hope to start our garden
crops and plant starts for the cool weather vegetables
requiring a long season-Brussels sprouts, cabbage, and
ca uliflower:'
Funding
U.S. Department o f Energy $2,882
Grant Recipients
Jerry and Judy Miller
May Creek, Alaska 99588
Home's wall used
as giant duct
In 1981, Mark Merrill of Willow was in the process of
planning and building a new home designed around
maximum efficiency of energy use. He chose to use
quality insulation materials, take advantage of passive
solar energy, and use abundant wood in a centrally
located heating system. .
He applied for an AT grant to add one more energy-
efficient feature to his home, and in the doing has
applied the feature to other homes, as well.
'My project is to fit this house with a device that will
recycle heat which would otherwise dissipate ... and to
warm well water in a preheating tank;' he said at the
time. Very simply, Merrill turned one wall cavity in his
house into an air duct that circulates warm air at the
ceiling to a crawl space beneath the house, where it
warms a rock energy mass.
The air warms the rocks, w hich in turn pre-heat a
water tank. In summer, the rock mass he lp s cool the
house by storing heat. But at ni ght, heat emitted from the
rocks help s keep the home warm.
The design is called a residential waste heat recovery
system.
"I t's working extremely welt' said Merrill, a carpenter
and builder who lives in Willow, about 70 miles north of
Anchorage. In fact, he's so impressed with it that he's
installed it in other homes he's built in Willow.
'Tve probably built 13 homes with this system in it;'
Merrill said, including his own home. "''m real happy
with it:'
39
ENERGY STORAGE , MASS
System Design
Merrill built a two-story, 1,208-square-foot home with
a cathedral ceiling over the living and dining room, and a
clerestory window wall above the stairwell to the second
floor.
There is a wood stove in the living-dining room. Sun
shining through the clerestory windows heats the
opposite wall in the stairwell which is painted a dark
color. Electric baseboard heating provides back-up
heating.
System components include a fan with a variable
speed control, two thermostats, and six tons of three-to-
six-inch rock in a wood box surrounding the 42-gallon
tank for the well pump.
The unique link of the syste m is a wall cavity, which is
32 inches wide by 3 .5 inches deep. The cavity ex tends
from the top of the wall opposite the clerestory to the
rock pen in the 4 1/z-foot-high crawl space.
The rocks surrounding the water tank are in a wood
box measuring four by four by eight feet insulated w ith
urethane.
The fan, built into the bottom of the r ock pile, is rated
at 650 cubic feet p er minute. It is a 12-inch round duct
fan, which can draw 75 watts at full speed . The fan is
controlled by a reverse acting thermostat on the wall
opposite the clerestory.
When the temperature rises above a specific level in
the clerestory, the pre-set thermostat automatically turns
on the fan in the crawl space. The fan pulls air through
The south fac e o f Mark Merrill's house (below) makes use of
clerestory windows.
an opening at the top of the wall into the wall cavity and
through the rock pile. An opening at the bottom of the
rock bin allows the air to continue into the crawl space
and back to the living room through a floor register
located under the woodstove.
The thermostat turns on the fan to draw the hot air
which warms the rocks and the water in the tank when-
ever the sun is shining or the woodstove is used.
A second thermostat in the living room is set to turn
on the fan when the temperature drops to a pre-set level.
The fan blows air through the rocks bringing the heat
stored in the rocks back into the house through the
register under the woodstove in the living room.
40
Performance
The residential waste heat recovery system has con-
sistently worked very well, Merrill said. In fact, it's
helped him slash his electric heating bills in half. The
system has been virtually maintenance-free.
Funding
U.S. Department of Energy $1,100
Grant Recipient
MarkS. Merrill
P.O. Box 103
Willow, Alaska 99688
Heat loss reduced
with rubber gaskets
Jerolyn Wroble, of Anchorage, was persuaded to
undertake the distribution of gadgets that would save on
the homeowner's heating bills.
She proposed to give away foam gaskets that seal off
drafts from wall plugs.
According to the Texas Power & Light C9mpany, the
second greatest source of air infiltration into the home
is through outside-wall electric outlets and switches.
Eliminating drafts from this source would significantly
reduce total air infiltration. The Texas findings were
adapted to Alaska in Wroble's pilot project aimed at
reducing both energy consumption for heating purposes
and energy expenditures by the Alaskan homeowner/
renter.
The use of foam rubber gaskets as insulation between
conventional outlet covers and the wall can eliminate
93% of this air infiltration. Although the gaskets were
already commercially available at a cost of approxi-
mately $2 a package, they were not being rapidly imple-
mented by the Alaskan public. The intent of this project
then, was both to increase consumer awareness of the
problem and also to provide a safe, inexpensive, simple
solution.
Procedure
Accomplishing this goal required three phases of
effort: purchasing, assembly, a nd distribution.
Wroble got bids from five different companies. A total
of 31,200 gaskets were ordered from the Fuel Control
Corporation, Minneapolis, Minn ., the most competitive
bidder, at a price of 4 cents each. To ensure that the
gaskets were safe, they were taken to the local fire
marshal whose review indicated they would not help to
support a fire stemming from an electrical outlet. Two-
thousand plastic bags, which explained about the
gaskets and their installation, were also ordered as dis-
tribution packaging. Each packet contained 12 outlet
gaskets, four switchplate gasket covers, and one pre-
addressed postcard.
The postcard was used as a means of obtaining con-
sumer response on the effectiveness of the gaskets.
Consumers were asked to return the card by an estab-
41
AIR INFILTRATION
lished date with any comments they might wish to make.
Western Airlines agreed to trade the cost of shipping the
gaskets to Alaska in return for being mentioned on these
postcards. Therefore, shipping the gaskets and printing
of the postcards was accomplished for $226, which was
less than half the budgeted figure of $500 for shipping
alone.
Distribution of packets was made through the follow-
ing outlets in Alaska:
Division of Energy and Power Development
Alaska Gas and Service
Matanuska Electric Association
Golden Valley Electric Association
The Energy Committee
City of Aniak
Miscellaneous (mailed or delivered in person)
Anchorage
Anchorage
Palmer
Fairbanks
Juneau
Aniak
125
500
200
250
300
50
500
Total Distributed
Performance
1,925
Judging from postcards and letters, the gaskets were
accepted very well both by individuals and agencies
receiving them.
There were several requests from consumers about the
best method of obtaining more of the gaskets. Many
commented on how effective the gaskets had been in
eliminating drafts . One consumer reported that he
noticed an immediate temperature difference around
outlets after installation .
A company that showed the sealers to all the con-
sumers it contacted for on-site verifications of residen-
tial energy audits reported their surprise at the number of
homeowners who had not been told about the electric
outlet energy sealers .
Funding
U.S. Department of Energy
State of Alaska
Grant Recipient
Jerolyn Wroble
P.O. Box 3404
Anchorage, Alaska 99510
$ 975
975
Solar collector has
unexpected results
Cliff Cantor tried to convert the southwest wall of his
arctic home into a solar heater by covering it with glass
panes.
Unfortunately, the solar collector wasn't sealed prop-
erly. Mildew and insect problems prompted Cantor to
remove it from his home in Bethel, Alaska ..
Bethel is a hub community for about 50 neighboring
Bush villages and lies on the shores of the Kuskokwim
River, one of the major transportation links in Western
Alaska. Like much of the state, the growing season here
is quite short. But in those summer months the rolling,
green, treeless tundra blossoms with hundreds of thou-
sands of wildflowers-in the planet's high latitudes,
plant life grows with an intensity not found in the
middle latitudes of the Lower 48.
And although sunlight hours are short in the winter,
the sun does shine brightly during the day. Cantor, who
is an owner of a barge company, hoped to capitalize on
this light as a partial answer to his home heating needs .
"We made a kind of jungle in there;' said Cantor of his
solar project. "I think that portion of the house might
have rotted under those conditions. That's why we took
it down~'
Moreover, Cantor also said he dismantled his experi-
ment because he feared it might have ignited his log
walls. At times, he said, the glazing caused temperatures
to soar almost to 140 degrees.
"We wanted to see if we could heat up one wall and the
answer is yes;' said Cantor. "You can do it. But some of
the other details didn't work out':
System Design
The solar collector was nine feet high by 10 feet wide,
covering the outside of the home's southwest-facing log
wall. The glass panel was comprised of several small
panes held in place by two-by-four-inch frames, set two
inches from the exterior log wall.
43
PASSIVE SOLAR HEATING
The logs behind the glass pane were stained brown to
help absorb sunlight and to protect the wood, and foam
insulation was appli ed to seal the edges of the glass frame
where the frame abutted the l og wall.
Sunlight striking the glass panes warmed the logs,
which in turn radiated heat into Cantor's living room.
Cantor anticipated that it would take most of the day to
heat the logs up, and the heat would be radiated into the
house during the night .
And it worked that way for awhile, says Cantor.
But flies multiplied and infested the house through
spaces between the logs. An algae-like mildew sprung up
in the space between the log wall and glass pane. Soon
Cantor's solar collector resembled a miniature jungle
swarming with flies.
"A lgae grew all over because we had a lot of moisture
in it;' Cantor said. "And we literally got thousands of flies
that flourished. It'd be covered with them sometimes'.'
In short, it didn't work out the way it was supposed to.
Tips
Although the collector achieved the objective of cap-
turing heat, the concept has room for improvement.
• Design a solar collector that allows air to circulate
between the log wall and the glass panes, to prevent
decay and mildew.
• Chink or caulk log walls for better indoor heat
retention and pest-proofing.
• Place a moisture barrier of heat-absorbing material
on the exterior wall surface.
• Carefully seal off all exterior cracks and fissures.
Funding
U.S. Department of Energy
State of Alaska
Grant Recipient
Clifford Cantor
P.O. Box 728
Bethel, Alaska 99559
$435
435
A ladder (top) rests on the south face of the home where a solar
collector was installed; (above) the entrance to the house. Th e
slide joint (right) between the entryway and the main house
allows the two portions of the building t o move separately
while maintaining a weather seal. The pivot is a t-<.Vo-by-four
under the floor joists.
44
' ACTIVE SOLAR SPACE HEAT
Solar water heating
system falls short in
Fairbanks
H . Jack Coutts was faced with two problems when he
built his home atop a 1 , 700-foot hill15 miles west of
Fairbanks: energy costs and water. Like most of his
neighbors, Coutts could not afford the expense of drill-
ing hundreds of feet for a well ; instead, water was trans-
ported daily from work in large container s .
Energy costs in the Far North are traditionally high,
and since (as Coutts figured) most of the domestic water
used in a typical household is heated prior to use, the
cost of heating water is a significant part of the house-
hold energy budget.
What Coutts proposed in this grant was a solar collec-
tion and storage system that would use snow melted in
the winter and rainwater in the summer to supply domes-
tic water needs. Winter snow would be melted using a
heat scavenging system constructed in an earlier project.
During warmer months, rainwater would be collected
and used . A large cistern built under his house would
collect the heated water. Coutts figured he could collect
enough water this way to supply his yearly needs . The
stored, heated water below his house would also help
heat his home, further reducing overall energy costs .
Coutts was awarded an AT grant in 1980 to build the
solar collection and storage system , monitor its perform-
ance , and determine the economics of the project.
The project involved fabricating and installing solar
collectors, constructing a 1,500-gallon cistern under his
house, and installing the necessary plumbing and moni-
toring features to control the system's operation and
automatically record performance data.
Design and Construction
Three eight-by-20-foot solar panels were designed for
the project.
Two man-made water storage tanks supply domestic
water. An outside tank is used in the winter to melt snow
and during the summer as a rainwater catch basin; it also
supplies make-up water to a large inside cistern . The
1,500-gallon inside cistern provides a large supply of
clean, treated water for everything but drinking. Coutts
still carries drinking water home daily and stores it in the
refrigerator.
The original plan of building the solar collectors on the
ground and lifting them in position was scrapped after
the first panel. The panel's weight and bulkiness proved
too much for Coutts, absenting a crane or Bunyonesque
assistance. Thus, the remaining two collectors were
assembled on the roof, using the roof itself as a struc-
tural support . This reduced materials and labor con-
siderably, but also lowered the system's overall efficiency
since the second two panels were fixed to the roof's angle
and did not directly face the sun.
In order to provide structural support for snow han-
dling and foot traffic, the four two-by-eight corrugated
aluminum roofing panels used to back each collector
were nailed to eight-foot lengths of wiggle molding. The
45
wiggle molding was in turn attached to 1 %-by-two-inch
runners set about 50 inches apart . Four-by-eight-foot by
1 1Jz-inch plastic foam insulation boards were placed
between the runners under the aluminum . Since the first
panel was constructed on the ground and lifted onto the
roof, it had an additional one-by-four and two-by-four
supporting frame.
A water inlet manifold for each collector was made
from one-half-inch PVC tubing wired to the top of each
panel. One-sixteenth-inch holes were drilled along this
pipe matching each trough in the corrugated aluminum.
After painting the upper surfaces flat black to increase
heat absorption and adding an outlet collection pipe to
two of the collectors, 20 millimeter fiberglass glazing was
applied. A caulking compound able to withstand 150
degrees in temperature was then applied to the glazing
edges.
The first solar collection panel, because it was assem-
bled differently, was covered with polyethylene sheeting
(Visqueen). Unfortunately, this panel will have to be
repainted and recovered as the polyethylene became
brittle after one year's use and there is considerable
weathering of the paint.
The outlet pipe is a 10-foot piece of 1 1Jz-inch PVC
plastic pipe with a %-inch-by-nine-foot slot cut in it that
the lower end of the collector panel rests in. This pipe
goes to the outside melting tank; panel number one is
connected directly to the inside cistern.
The inside cistern is a V-shaped depression in the
bedrock below the house. Coutts covered the rock face
with smooth cement and 10-mil Visqueen as a water-
proof liner. Bacteria control of this domestic water
supply was by batch treating with chlorine. Since there
was no way to accurately control the amount of chlorine
in this water, Coutts also installed a residential water
filter with a charcoal element to filter out the excess
chlorine before the water was used. The charcoal element
needs replacing about once a year. Water in the outside
snow melting tank does not get chlorinated because it is
used only to supply make-up water to the inside cistern.
The solar collector panels are connected so that panel
number three is connected directly to the inside cistern ;
and panel number two can be connected either in parallel
with panel number three, or between panel number one
and number three. This is done with a removable piece
of PVC tubing . When make-up water is needed, the
temporary tubing connects the output of panel number
two to the outlet of panel number three. Water from the
outside snow melting tank is pumped through an
activated carbon filter to the top of panel number two,
heated as it flows down the panel, combined with the
output of panel number three and delivered to the inside
cistern. When the cistern is full , the temporary
connection is removed and water drains into the rain
gutter, returning to the meltwater tank.
Because he'd carri ed water to his home so often, Coutts
had a lready in s talled many water-saving devices in hi s
house. These incl uded a fron t-loading wash ing m achine,
a quart-flush toilet, and low-fl ow sh owerheads.
Thermal co ntrol is through two thermostats (Snap
Discs) mounted about one third of the way down the
back of collector panels one and t hree. As the skin tem-
perature of the corrugated aluminum reaches 110
degrees, the thermostats close (turn on); they open (turn
off) when the skin te mperature drops below 90 degree s .
When the thermostat o n panel one closes, a sump pump
in the bottom of the snow melting tank is turned on.
Water flow s up to the inlet manifolds of co llector panels
o ne and t wo. Panel number one free drains back into the
snow melting tank through the rain gutterin g sys tem.
Panel two either free drains b ack in to t he snow melting
tank, or into the ou tl et pipe for collector panel num ber
three, depending on w hether or not the removable PVC
coupling is installed .
When the thermostat on panel three opens, domestic
water flows throu gh a control solenoid valve to the col-
lector's inlet manifold and then t hrough the collec tor.
Domestic water is su pplied by a pressurized shallow-well
electri c pump and a 12-gallon pressure tank.
Because t he water s upply in g collector panel number
three is straight from the pressurized domestic water
system, the t hermostat mounted on t hi s panel co ntrols
46
Th e firs t solar co ll ec to r (abov e) was co ns tructed o n the
g ro u nd.
both the inlet water supply and a s pecial drain solen oid
val ve. Whe n the temperature of the aluminum exceeds
110 degrees, the drain solenoid is closed and the supply
so lenoid is opened. Water flow s through the collector
until either the skin temperature of the aluminum drops
below 90 degrees, or unti l a 24-hour control t imer shuts
the panel off. The 24 -hour timer opens t he drain
s o lenoid at the end of each solar heatin g day-at approx-
imatel y 6 p.m . n ig htly.
The timer and therm o s tatica lly controlled so lenoids
are required for f reeze protection of the tapped pressure
sy stem supplying co ll ector panel number t hree. Since
collector panels one and two are essentia ll y fr ee draining,
freez e protecti on is provided when the temperature of the
corrugated a luminum drops below 90 degrees, openi ng
the thermostat a nd shuttin g off the sump pump. The
co llectors free-drain into the rain g utters a nd back in to
the snow melting tank.
Performance
With t he sun shi n in g, the controlling thermostats
generall y cl ose when the ambient temperature of the air
between the fiberglass gla zing and the corrugated alumi-
num exceeds 45 degrees. This is us ually suffi cient to
cause the temperature of the aluminum to get above 110
degrees. H owever , during rainy, cloudy, and cooler days
when the o utside temperature is below 60 degrees, the
ambien t temperature rise is usua lly not enough to actu-
ate the thermostat and allow hea t collection. Because of
the problems associated with the polyethylene cove red
panel, the actua l performance of panel number one is less
efficient.
A dual probe thermograph, a type of self-recording
thermometer, was used to measure water temperature at
both the s u rface and the bottom of t he inside cistern . A
minute to ta li zer was also installed to record the total tim e
water ac t u all y flowed from the inside cis tern thro ugh
s o lar pa nel three. Data was collected from both units
between july 2, 1981 and Aug us t 18, 1981. Although this
ti me peri od experienced poor solar heating co nd iti o ns, it
was found that heat was s till collected for qn average of
14.6 h o urs per day.
Since heat recovered is the product of t he flow rate ,
flow time, te mperature difference between input a nd
output water of the collector, and specific heat , the heat
captured during the te s t period was calculated to be
430,000 BTU's. Although it sounds like a lot , w hen com-
pared to system cos ts and energy cost savings, it was
determined that the solar collection system would not
pay for itself during its rated 20-year lifespan . Even
amortizing the cost of the system, assuming a 10 percent
interest rate , over 1 0 yea rs would not make the project
cost effective .
If the economi cs were figured during a warmer s um-
mer, the so lar panels would obviously perfo rm m uch
bet ter, due in part to the heat transferred to t he co o ler
47
water from a mbient ai r . A similar in stallation a t a lower
a lt itude might also tip the sca le s in favor of solar heaters,
especially if they are ti lted to fa ce directly into the face of
the sun; however, the increased cos ts of such a system
may offset any sola r gain.
Conclusion s and Problems
Based o n the data collected during the s ummer of
1981, these solar collectors in sem i-a rctic environments
are not an economically sound inves tment. H owever, for
those who can o bta in inex p ensive materials for use in an
improved design, a similar project may be worth the
effort. Cout ts recommends t h at these people design a
house with solar heating as a n integra l part of t he struc-
ture, such as optimized roof s lope a nd direction (w ith a
black painted roof) and below-foundat ion water s torage
or radiant floo r heating.
One last word of advice from the g rantee is that
ground heat s torage should not be cons idered if the
house is built on or near permafrost.
Funding
U.S. Department of Energy
State of Alaska
Grant Recipient
H . Jack Co utts
Mile 348 Nenana Highway
Ne nana, Alaska 99760
$975
687
Solar heat works well
in Copper Center
Copper Center residents no longer have to worry
about buying oil to keep their Kenny Lake Community
Library warm now that they have a solar water heater
and a wood-fired boiler.
The solar collector helps keep the library at a comfort-
able 60 degrees almost year-round in this community of
500 people, 80 miles north of Valdez in Southcentral
Alaska.
During the first winter of the solar system's operation,
the librarians supplemented the solar heat with a water
boiler. The boiler, which formerly burned oil, was con-
verted to burn wood and coal. It used three cords of
wood and a ton of coal, most of which was donated.
"We now use only wood, coal and solar;' said resident
Brad Hennspeter. 'That's saving us money, plus it's a
renewable resource:'
Specifically, the community no longer has to spend
some $1,200 annually on heating oil for the library. The
solar heater also has prevented the library from freezing
up in winter despite sub-zero temperatures of minus-60
degrees.
"It's working excellently;' said resident Sam Light-
wood, who supervised the solar construction. "Solar is
much more efficient. It's the way to go'.'
System Design
A solar collector and a wood/coal boiler are used to
warm water in a 1,000-gallon tank housed in a room of
the library. Heat radiating from the water is blown by a
fan into the main library reading room, which is 23 feet
by 31 feet.
The steel water tank is six feet high and five feet in
diameter. It was coated with epoxy inside and painted
with a dull red primer on the outside.
The lOS-square-foot solar collector, which has four
glass panes, was mounted upright on the south-facing
side of the library roof. The collector-six feet wide by
six inches deep by 16 feet long-has a series of half-inch
copper pipes sandwiched between sheet metal and ther-
mopane glass. The interior of the solar collector was
painted black to absorb sunlight.
The water, circulated by a Grundfos pump, flows from
the bottom of the water tank up to the copper tubes in the
solar collector. Electronic sensors activate the pump
whenever water in the solar collector is warmer than the
tank water.
Hot water from the solar collector, averaging 80-110
degrees, returns by gravity flow to the water tank
through a three-quarter-inch copper pipe .
On very cold days, however, the librarians have to
supplement the solar system with a wood/coal boiler.
The water flows by gravity from the water tank to the
boiler and back to the water tank via a separate,
1.25-inch copper pipe .
A snap switch located in the water tank room auto-
matically cuts off the fan when the tank room air tem-
perature drops to 75 degrees.
48
~~~
The steel water tank radiates heat as it warms up. The
heat is blown into the main library room by a 36-watt
fan which was placed inside of an 8-inch galvanized
floor duct. The fan is controlled by a thermostat, which
also has a manually-operated variable speed control.
The room housing the water tank has double-wall
construction and superinsulation . The exterior wall was
framed with two-by-fours, and was insulated with eight
inches of fiberglass. The interior has four-inch stud walls
with two inches of insulation. A six millimeter polyethy-
lene sheeting also was installed on the interior as a vapor
barrier. Sheetrock covers the vapor barrier. The roof is
made of corrugated aluminum.
Performance
Overall, the solar-heated water tank has worked very
well, keeping temperatures at around 60 degrees . More-
over, the library's fuel bill has been substantially reduced
because the facility no longer has to rely on expensive
oil. They also save money by receiving volunteer contri-
butions of wood and coal. By comparison, the library
spent more than $1,200 on oil for fuel annually before
installing the solar collector.
Inadequate air circulation between the water tank
room and the main library is the most serious problem
which has surfaced.
Lightwood said that one of the cool air ducts should
not have been placed near the same vent as the hot air
flue because the hot air tended to be diverted back into
the tank room.
Lightwood said he plans to plug the old vent and
install a new one elsewhere in the library.
Another drawback of the system is the amount of time
it takes to initially heat up 1 ,000 gallons of water.
Lightwood said it often took about six hours to heat the
library to the 60 degree range.
However, once the water heater is hot it stays warm for
a long time. In fact, since its installation in June 1983 the
library has not frozen up at all.
"Once we have the 1,000-gallon tank warm we can
leave the building for a weekend and when you come
back on Monday morning the temperature (in the build-
ing) may be in the low 30s, but it hasn't gone down to
freezing;' said Hennspeter.
"I think it's very cost effective;' Lightwood said. "I
highly recommend it for any kind of a building. We have
had plants in the library all winter. It works well:'
Solar collectors (top right) were mounted on the roof of the
Kenny Lake Community Library. (Bottom right), collector pip-
ing inside the library.
49
Tips
Several tips were offered by project participants in
thei r evaluation of the solar system:
• Install the solar collector upright. This reduces stress
on the glazing, minimizes the chance of rain leaks
and reduces snow acc umulation.
• Be su re to allow plenty of air in the boi ler when
burning coal, which requires more air than d oes
wood. Otherwise, coal, particularly soft coal , tend s
to emit a lot of smoke.
• The water tank will sweat when it is first fired up.
50
• Don't fill the water tank completely. There should be
some space for water to expand as it heats up. Also,
a heat shield is needed beneath boilers if the floor is
made of flammable materials.
Funding
U.S. Department of Energ y $2 ,242
Grant Recipie nt
Kenny Lake Community League
Kenny Lake
Star Route, Box 231
Copper Center, Alaska 99573
A comparison:
Three solar water
heating systems
The Municipalit y of Anch orage and th e Western
Building and Construction Trades Council are evaluating
the feasib ili ty of three different concepts in active solar
water heaters .
The solar water heaters are in the ce nter of the
Anchorage bowl. Two are attached to a municipal office
bui lding at 3500 Tudor Road. One is attached to the
Plumbers and Steamfitters Apprenticeship Sc hool at
610 Potter Drive.
System Design
Three separa te collector systems were designed.
Design criteria included: a) the three systems must range
from the ver y si mple to the complex a nd sophisticated;
b ) the systems m ust be appropriate to residential use in
both new a nd exis ti ng s tructures; and c) each system
must provide supplemental domestic hot water heating
for 100 gall on s per day, for domes tic hot water demand
at 120 degrees .
Ea ch system has a differen t type of solar co llecting
heater o n the building's south sid e. The heat from the
co ll ector is captured in a n antifreeze so luti on and piped
to a heat exc hanger in side the building. This heat is
stored in a tank filled with water. As there is a hot water
demand, heat is extracted from th is tank through a heat
exchanger a nd piped in to the d omestic water system. All
th ree systems must have a conventional water heater to
back-up the solar co lle ctor.
System 1. The "breadbox" system is within the sco pe
of some "do-it-yourselfers" u tiliz ing simple principles
and eq uipment, and easily un derstood and adapted by
the lay m an of average ability. So lar capture effective -
ness is less than the other two systems.
The "breadbox" has three basic parts: water tanks, a n
insulated box and the cover glass. The three water tanks
we re new e lectric hot water heaters modified by remov-
ing the metal cover and insulation. The ta n ks and inside
of the insulated b ox are painted flat black. The cover
glass in the "breadbox" (and Solaroll-brand system
descri bed b elow) is double glazed acryli te panels.
System 2. The "flat plate" system is somewhat more
co mplex than System 1 , but not highly tech n ical. The
"flat plate" has three basic parts: an absorber p late, the
cover glass, and insulation under the absorber plate .
The absorber plate is a Solaroll-brand materi a l, a p lasti c
mat, s imila r in thickness to an inner-tube, with quarter-
inch diameter tubes in the mat. The design allows the
absorber plate to be glued against the side of the build-
ing, thus eliminating the need for insulation under the
plate.
System 3 . The "concentrating tracker " is a high tech-
nology sys tem. Completing the picture of available
approaches to solar water he ating is the only ju st ification
for this design in Anchorage. Design drawbacks to
a hig h technology system include t he level of effort
51
DOMESTIC SOLAR HOf WATER
required by competent design professio na ls, and the
mechanical devices n eeded to accomplish the tracking
are expensive and failure-p r one.
The "concentrating tracker " has three b asic parts: an
absorber p ip e, a parabolic r efl ector, and a tracking
system. The absorber pipe is a fl at black metal pipe
enclosed by a glass tube. Within t he pipe is a coil which
allows cold antifreeze to circulate down to the foot of the
parabolic reflector and then back up to the collection
pipe at the top. The paraboli c reflector is a curved trough
lined w i th slices of mirror which reflect sunli ght toward
the absorber pipe.
Construction and Installation
All construction was done t hrough the Western Build-
ing a nd Construction Trades Council w ith volunteer
union labor. The majority of work occ urre d in coordina-
tion w ith their apprenti cesh ip classes, w hich occ ur
seve ral months ea c h year.
Footings for the "tracker" and "breadbox" were built in
October, 1981. Footings were fo u r cement posts for the
"tracker" and four cedar posts for the "b rea dbox'.' All the
posts were at a depth of four fee t and anchored in
ce ment.
The "breadbox" collector was star ted in December,
1981 , and finished by April. T he floor is two-inch by six-
inch jois ts ins ulated with five in ches of expanded
polystyrene. The wal ls a n d roof are t wo-i nch by four-
inch studs w ith 3 V z inches of polystyrene. A three-
quarter-inch Thermax brand (poly isocyanurate) sheet
was attached to the inside of the roof with the reflective
s urface exposed inside. Urethane from a can was used to
fill jo ints between Insulfoam and wood joists.
During the winter of 1981-82, off-site p lumbing was
started at the apprenticeship training school. The h eat
exchanger coils were made from one-inch copper pipe.
Each heat storage tank has two coils, one for h ot col-
lector fluids and o ne for co ld domestic water. The fluid in
the tank stays in t he tank, at gravity pressure, acting as
heat storage mass. An over flow /expansion t a nk was built
out of six-inc h PVC pipe. This device a ll ows for tank
fluid expansion and contraction. In the eve nt either the
hot co ll ec tor coil or co ld domestic coil leaks, then
p ressure increases in the tank would tr igger a float-valve-
activated alarm .
The heat storage tanks for the ''breadbox" a nd the
Solaroll system were fabr icated from one-eighth -inch
steel. A 40-gallon storage tank was sufficient for the
"breadbox'.' The Sola roll re quired a 150-gallon stor-
age tank, partially because it has less fluid mass in the
collector exposed to the sun.
O n-site plumbing began th e summer of 1982. The
350-pound 'Tol-Tec Tracker" co llector u nit was erected on
the groun d. This co ll ector was partia ll y assembled
by t he manufacturer and was easily erec ted in s ix hours
52
by two men. Minor problems with missing bolts and
poorly machined pieces were easily overcome using an
electric drill , files , and locally available bolts. Six men
placed the unit on the cement footing. Additional brac-
ing was bolted to the tracker frame for wind protection.
Plumbing between the collector and mechanical ro om
is one-inch copper pipe hung in the floor crawl space.
After soldering the pipe together, the plumbers insulated
the pipe with half-inch thick Armstrong armaflex.
Installation of the heat exchanger tank, collector fluid
recharge tank, expansion tanks and other equipment
used 11 square feet of floor space.
Three water tanks, connected in series, were in stalled
in the "breadbox': The tanks rested on a steel platform
and were braced and bolted in place with angle iron to
withstand earthquake vi brations.
In January, 1983, electricians began installation of
conduit, breaker boxes and meter bases for the tracker.
Wiring was not completed because of insufficient elec-
trical detail on the "tracker" control system.
The mechanical area of the Solaroll system was
installed in January and February, 1983. After instal-
lation, the Municipal Fire Marshall found the permit was
incorrectly approved by their office for this system. In
June, 1983, the plumbers removed this system for
eventual reinstallation.
The "breadbox " was also moved during this time
period. The plumbers found insufficient space available
for the "breadbox" mechanical area. Using a forklift and
trailer, the "breadbox" was moved to the Plumbers and
Pipefitters Sc hool and installed.
Current construction by the Electrical Workers
Apprenticeship School on the "tracker" was expected
to be completed by spring, 1984.
Work to complete control wiring on the "breadbox"
and to reinstall the Solaro ll mechanical was scheduled to
begin in April , 1984.
(Previous p age) Pe ter Po ray (t o p ) explains d etails of the bread
box co llecto r (right). Til e assembled co llector (b o tto n-1 left ) in
p lace. S un ligh t s t rikes the S o la roll (midd le left).
53
Problems
Problems peculiar to this project in Alaska were:
• Design data on the "tracker" was incomplete. The
"tracker" was made by a new company that folded
in 1982 after three years of business. These new
technologies have problems: parts were missing
and some electrical parts were unavailable locally;
some mirrors in the parabolic reflector were
cracked; three shipments of glass tubes, which go
around the absorber pipes, were broken in ship-
ping; electrical diagrams were incomplete; the
manufacturer disappeared, but the designing elec-
trical engineer was found after a two-state tele-
phone search.
• Getting the design approved took four months.
This was the first solar co llector building/me-
chanical permit given by the Municipality.
Modifications
Several modifications were made:
• Design specifications asked for galvanized heat
storage tanks. No firm galvanizes tanks in
Anchorage, so paint was used to rustproof the
tanks.
• The "breadbox" system was relocated to another
building, due to inadequate space in the closet
housing the existing water heater.
• Viewing access to the heat exchanger, storage
tanks, pumps, and controls was changed twice.
Less viewing access now exists because of the need
to maintain an adequate fire barrier between the
mechanical area and public areas.
Funding
U.S. Dept. of Energy
State of A laska
$16,472
15,872
Grant Recipient
Municipality of Anchorage
Municipal Energy Coordinator
Pou ch 6-650
Anchorage, Alaska 99502
,,,
ol
•:I
Solar powered pump
increases efficiency
Do is Dallas, of Dallas Engineering, completed a
project in Fairbanks, 1.2 miles from the University of
Alaska, using solar energy to heat domestic hot water.
System Design
In Phase I (1981-82), solar collectors were installed and
integrated into a heat exchanger-domestic hot water
system which was capable of being alternated (for source
energy) from solar/propane to electricity. The a lternating
cycle selected was weekly for o n e year (52 weeks).
The prior energy source was all electricity for both
domestic hot water and space heat for this residence (a
log house). In addition to purchasing and installing the
solar collectors and heat exchanger, it was necessary to
purchase and install a propane hot water heater a nd a
propane furnace. Phase I was 100 % passive, incorporat-
ing a thermosiphon system and no moving parts.
The solar collector is a serpentine design with half-
inch copper tubing soldered to a metal collector plate.
The collector is mounted at a semi-fixed angle on the
ground in front of Dallas' garage. The heat exchanger is
mounted above the height of the collector on the inside
garage wall.
Phase II (1982-83) implemented a change from 100 %
passive to semi-active by adding a pump powered by
electricity from photovoltaic cells. No external elec-
tricity and no differential controllers were required.
The photovoltaic panel, DC motor, and pump work in
tandem. Only the intensity of the sun's rays controls the
flow by producing more or le ss electricity.
Operation, Performance, and Problems
The system operated throughout Phase I and II with-
out major problems. Temperature recording charts show
that for the week of April20 to 27, 1982 significant Btu's
were transferred to the domestic hot water system. (Note
that this was during the 100% passive phase.) Other
measurements (May 11 to 18, 1983) illustrate that by
employing the circulating pump, powered by the photo-
voltaic panel, more of the potential Btu's were trans-
ferred to useable storage than was the case with the
100% passive system.
54
Some 87 college-level students have been involved
in collecting and analyzing data during operation of the
system. For most of these students, it was their first
introduction to the basic procedure for capturing Btu's
a nd e le ctricity from the sun.
C lasses for future students will be offered by Tanana
Valley Community Coll ege if there is sufficien t student
interest.
The project was featured in KIMO-TV's "Alaska's
People" and a tape of the program is available in the
Alaska State Film Library.
Modifications
Changes that are indicated from the data collected are:
• Preheat storage volume should be enlarged and
insulated better.
• Life-style changes are mandatory if full advantage
is to be taken of solar Btu's when they are avail-
able. For example, 3 p.m. is probably the opti-
mum time to take showers, wash clothes, use the
dishwasher, etc.
Tips
• Propane as a source of fuel for space heating (at
local prices) is approximately 20% cheaper than
electricity.
• Solar gain from a passive system is not attractive
in Fairbanks with a payback of 24.5 years based
upon the 1984 cost of propane.
• If there is another disruption in the supply of
crude oil w hich results in a quantum leap in price
to $60 per barrel or more, then solar energy (aug-
mented or pumped with photovoltaic energy)
would be economical for domestic h ot water in
Fairbanks.
Funding
U.S. Dept. of Energy
State of Alaska
Grant Recipient
$4,040
6,935
Dois Dallas, Dallas Engineering, Inc.
SR Box 30140
Fairbanks, Alaska 99701
55
Dais Dallas (/eft) explains Fairbanks solar applications.
(Above), a temperature recorder for the solar collector.
IIIII I
.....
Automobile radiator
reduces home fuel bills
Mark Miller has reduced his fuel bills by preheating
his home's hot water in a solar collector made of car
radiators .
Initially, he had hoped that if the novel project proved
successful it could become a springboard for building
similar systems throughout rural Alaska . ·
'The syste m also was to illustrate that it could be an
unobtrusive addition to a suburban home;' said Miller,
who works for the State Department of Commerce in
Juneau.
Unfortunately, the project did not turn out to be com-
mercially viable. But it is helping Miller save on his
home heating bills.
'The project was not a spectacular success;' Miller
said . "Nonetheless, my collector continues to function
for my home, and given the few component parts, will
probably continue to do so for years to come'.'
Design and Construction
Six radiators were set inside a wood frame box in two
rows of three each . The frame is insulated to a thickness
of six inches in the back and sides, and four inches along
the interior wood ribs. It is covered with one-quarter-
inch plexiglass and sealed with a silicone seal.
The radiators, backed by sheetmetal, are filled with
antifreeze . Hoses, held in place by stainless steel clamps,
circulate the antifreeze as it warms up through the linked
radiators.
57
Heat collected by the radiators is stored in phase
change salt in 20 polyethylene plastic tubes in a shed
below the radiators . The tubes, which are filled with
eutectic salts, are six feet long by 3.5 inches in diameter.
The salts turn to liquid as heat is absorbed . Compared
with water, the pound-for-pound storage capacity of
each tube is four-to-one , and by volume, five-to-one.
Water that needs to be preheated flows through a
separate piping system sandwiched among the thermal
salt-filled tubes. The water circulates through two sets of
"W" shaped tubing made from three-quarter-inch copper
pipe . Afterwords, the preheated water flows back to the
home's domestic hot water heater.
A small water pump, expansion tank, zone valve and
pressure relief valve also were installed in the solar loop.
Many of the final connections were made with flexible
copper fittings. A sheet metal "V" roof was placed on top
of the solar collector to prevent snow buildup.
Modifications
Miller says he could have cut the 200 hours he spent on
the project in half and slashed the project's costs through
a few modifications.
For example, he recommends using plastic pipes and
rubber hosing instead of copper pipes, and connecting
the hose to the pipe with "0" clamps.
The radiators also could be stacked on top of each
other instead of being placed in separate compartments.
Mark Miller co n s tructed a so lar collector (l eft ) us ing o ld car
rad iato rs (above).
Anot her alternat ive would be to build two separ ate
wood frames that could each hold three radiators,
in stead of housi ng them together in o ne box. The two
boxes could be connected with plastic pipes. Also, it
would be easier to install two wood frames on the house
than putting up one 700-pound unit.
Tips
When Mill er applied his design to the realities of
materials and constr uc t ion, he deve loped other usefu l
tips for future reference. In h is words:
• Do not attempt this p roject if you are afraid to
solder copper pipe, do not like metal cuts, hate fiber-
glass insulation, or have little free time.
• Build a sheet metal "V" roof over the to p of the
s yste m to prevent excessive weathering and snow
buildup.
• The system can be built with a propane torch, pipe
cutter, solderi ng brush, hammer, ti n s n ips, drill g un
and a 10-ton crane.
58
• Copper must be clean and dry. Once you cut your
pipe with a pipe cutter (don 't use a h acksaw or your
grandchildren will be finishing you r project), clean
the pipe and connections with fine steel wool. Clean
the in side joint-connector, and join the pipe and
connector toge ther.
• Do not try to solder copper feeders to radi a tors . Car
radiator connection points already have been
soldered. Thus, when you heat up the radiator intake
to solder on the feede r, t he h igh temperature
weakens all the other joints and the radiator should
be junked . Chasing weakened joints is a thankless
task.
• Seal small radiator leaks w ith "silver " seal or another
auto radiator sealer.
Funding
U.S. Depart ment of Energy
State of A laska
Grant Re cipient
Mark A. Miller
4324 Mendenhall Bl vd.
Juneau , A laska 99803
$1 ,375
1,375
Palmer's energy
farm proves up
Tom Williams is creating an energy-efficient farm.
Already, he's producing electricity with a wind gen-
e:-a tor, and drying bales of hay with a solar heater.
"''ve been doing these things all my life~ says
W illiams, an attorney and farmer. "My father was into
this when I was a boy. He was always innovating and
creating new things for the farm '.'
Williams is continuing that tradition on his family
farm in Palmer, just north of Anchorage. He's also plan-
ning alternative energy projects for a second, 640-acre
farm he's developing on nearby Point MacKenzie .
Finding the time to spend on his projects while run-
ning a law office in Eagle River and meeting the demands
of his family is an on-going challenge he faces daily. He's
also had to contend with a fire that destroyed his law
office last year, and a malfunction in his wind generator.
"But things are working out. This particular farm was
designed around a huge solar collector. Since we have the
heat I'm trying to use it in several different ways': He
conceived the project and applied for the AT grant funds
in 1980.
System Design and Performance
The 10 kwh Jacobs wind generator sits atop an 80-foot-
high tower. Its three, 11-foot-long blades are made of
laminated Sitka spruce and can withstand gusts of more
than 125 mph . The generator is designed for the blades to
feather and turn sideways to the wind when the wind
speed reaches 45 mph .
59
The generator can supply Williams' farm and house
with all the electricity it needs. Any unused power is
sold to the local electric utility, the Matanuska Electric
Association.
From installation in February, 1982 to July, 1984,
Williams' system has produced about 10,000 kwh of
power, of which 2,200 kwh were sold to the electric
utility.
Unfortunately, Williams has to replace the Jacobs
Mastermind control unit which keeps the power pro-
duced by the wind generator suitable to combine with
the utility power. Nonetheless, Williams said the wind
generator has worked well .
"I am personally pleased with its production effi-
ciency;' Williams said. "It's almost paid for the mortgage
on it:'
Another project Williams completed was constructing
a new barn that is a solar grain and hay dryer. Corru-
gated plastic roof glazing is used in place of metal
roofing to turn the whole rafter area into a large hot air
solar collector.
A Habco crop dryer powered by a four-cylinder Wis-
consin engine was suspended from the ceiling. This com-
mercial fan blows the air warmed by the solar collector
into a wood crib (four by four by 10 feet) buried under
several hundred bales of hay.
The hay dries as the warm air flows from the wood
crib through the haystack. About 400 bales were dried
Installers (left) prepare the w ind generator; (above) snow
covers the fiberglass roof o f the so lar bam.
from September t hrough October in 1982 with this solar
heater.
'When baling hay, we normally find about 10 % of the
bales to be too wet to s tore;' Williams sa id. "Those b a les
are carefully stacked in such a manner as to be mechan-
ically dried by forced air. This method, while somewhat
expensive, is extremely effective and creates a very high
quality hay:'
But, Williams said, there is a more efficient way to dry
the hay. The hay, for example, should be stored inside
the barn on top of a perforated wood floor. That way
warm air could be channeled from the ceiling to under-
neath the floorboard. The air would flow up through
openings in the barn floor and dry the bales of hay.
Williams also has a solar grain drier, which utilizes t he
warm a ir from the solar coll ector. The drier, which is 12
by 16 feet, has a perforated floor . A three-horsepower
"s quirrel-c age" fa n blows warm air from th e solar
co lle ctor th rough a pile of grain .
'This device h as n ot functioned properly because our
two-horsepower motor has not been capable of driving
the fan, except for a three-minute period before it over-
heats and cuts out;' Willi ams sa id. "We have another fan
on order and hope to demonstrate its ability~
Another unique system Williams installed was an
alcohol still. "It is a manufactured 80-gallon reflux
co lu mn still;' he wrote . "It is capable of producing eight
gallons per hour of 130 to 160 proof a lcohol ... We are
Tom Will iams ' farm (above) n ear Palm er. A gasoline fan
powers the hay dryer (right).
60
p r esently using a series of fermentation vats, using both
potatoes and grain as the basic source of vegetable
matter;' he said in 1983. Effluent (wastes) from the still
are used as cattle feed.
Performance and Tips
Wh en Williams first conceived of a farm that could be
a demonstration for various energy-saving procedures
and devices, he had no idea of the notoriety it would
receive. By 1983, he said, more than 20 reporters had
interviewed him about his experiences and plans, and
more than 200 v isitors had come to the farm to learn
more a bout the project. By 1983, the farm supported 25
head of cattle and seven horses.
Williams says h is experience. suggests several improve-
ments:
• Dry the hay inside the barn .
• Install a slotted, perforated barn floor so that warm
air can be circulated fr om the ceiling, under the fl oor
and up through the hay stack.
• Before building a wind generator, m ake sure it's cost-
effective. Chart local wind currents and determine
energy needs before making the investment.
Funding
U.S. Department of Energy
St ate of Alaska
Grant Recipient
Thomas E. W illi ams
SRB-Box 7470
Palmer, Alaska 99645
$16 ,476
33,440
Crab waste produces
methane gas supply
Charles Vowell first moved to Unalaska in 1967, em-
ployed as a plant engineer for one of the local canneries.
In those days, cannery wastes were simply dumped into
the bay. Unfortunately, the cannery wastes did not float
out to sea as expected; they immediately sank to the
bottom and formed huge deposits of decaying matter.
During this period, Vowell also noted that soon after a
dumping occurred, bubbles began rising to the surface.
He didn't think much about it until a couple of years
later when, after attending an alternative energy confer-
ence, he realized that those bubbles were methane gas.
Vowell thought that if he could somehow harness this
gas, he could help solve one of Unalaska's major prob-
lems-high energy costs.
Unalaska, an island about 800 miles southwest of
Anchorage, is the home of America's third largest fish-
ing community. This island, like many in the Aleutian
chain, is a windy, treeless bump in the ocean. Since
Unalaska and its neighbor city of Dutch Harbor are
fishing and cannery centers, work is seasonal and the
cost of living high. Everything that doesn't come from
the sea has to be shipped in.
The cannery wastes have caused problems in Unalaska
before. The Environmental Protection Agency has deter-
mined that the waste disposal method was causing harm
to the fragile ecology of Unalaska Bay and the agency
ordered the dumping in the bay stopped. The canneries
complied with this order by simply pumping the effluent
to the mouth of the bay and also barging it out to sea.
Although the immediate problem of pollution within the
bay was solved, the overall problem was not.
Vowell figured that a bio-digester could not only solve
both the waste disposal and ecological problems, but
help offset some of the high energy costs of the area, as
well.
In 1979, he received a grant to design and fabricate a
methane bio-digester at Unalaska. The project involved
the design and construction of the bio-digester, and
developing a method to clean and store the methane gas.
Design and Construction
Vowell decided to build a continuous feed bio-digester
using as much local material as possible to keep costs
down. Using primarily crab gurry (offal), the system
would consist of a 10,000-gallon digester tank, a water
pump to keep the material suspended, a hot water heater
and heating coil for thermal control, an old boiler for
low pressure gas storage, carbon dioxide and hydrogen
sulfide scrubbers, insulation, and the necessary piping
and controls to operate and monitor the system .
Vowell calculated that his system would have a rated
output of between 900 and 5,100 cubic feet of methane
gas per day, with a heat value of about 900 BTUs per
cubic foot net output after scrubbing (cleaning emis-
sions). These figures are based on an average of 1.4 to 7.8
cubic feet of solid matter per loading. The actual output
would be monitored by a standard gas meter placed
between the methane generator and the low pressure
boiler storage container.
61
METHANE DIGESTER
In keeping with the philosophy of using as much local
material as possible, the support stands for the digester
tank were made from old dock pilings. The digester
tank, hot water heater, piping, and boiler were acquired
from the local canneries. The heavy equipment required
to move the tank and other articles was rented from the
city of Unalaska. Most of the labor was provided by
Vowell himself.
One modification to the original design was the low
pressure storage system. The boiler that was to be used
became unavailable, forcing Vowell to find an alter-
native. He located 41 empty propane tanks which he
mounted upside down on a rack. A small, low-pressure
compressor was connected to them . Although this solved
the storage problem, it lowered the system's efficiency
because it added the energy consumption of the com-
pressor to operating overhead.
A mixing tank with a vacuum flush mechanism was
installed at the input to the digester. This flushing device,
which works much like the home lavatory, ensured that
sediment would not build up at the input end of the tank
and reduce system effectiveness.
At the end of a digestion cycle, the remaining sludge
was drained off into a holding tank. This sludge was
subsequently disposed of by dumping into a landfill.
The system was designed to be relatively simple to
operate. A window mounted in the digester allowed
visual observation of system operation. The window
was important to anticipate scum build-up. The scum
indicates that the anaerobic action has ceased. Recharg-
ing and monitoring would only take about an hour's
work each day.
Performance
Although the methane digester was operated for only a
short period in 1980, Vowell feels that it was a resound-
ing success. Thirty days after he first began loading the
digester, "i t was quite satisfying to sit and watch the
gurry bubble~ through the tank window. The crab
wastes supplied by the East Point Seafoods cannery
produced usable quantities of methane gas that required
almost no scrubbing. Although the system was only
filled to 10 percent capacity, it produced about 100 cubic
feet of gas daily-more than a single house could use.
Another aspect of the gas produced by this system was
the lack of odor associated with fish-charged methane
digesters. The gas had almost no odor before or after
burning. However, the crab wastes only lasted until the
end of crabbing season. After that, ground salmon waste
was tried.
Although salmon is easier to handle than crab and
digests faster, the gas output of about 600 cubic feet of
gas per barrel of salmon waste was of marginal quality.
It had a foul odor and required both carbon dioxide and
hydrogen sulfide scrubbing. Even then, so little methane
was produced that it was determined that salmon, or
other fish-only wastes, are not worth the effort.
Another problem with the experimental system was its
location in relation to supply. Moving the digester closer
to the canner ie s a nd piping the crab wastes d irec tly to the
digester would improve it s effic iency co n s iderably.
In addition, Vowell tried a couple of modifications
to hasten the digestion of t he crab wastes. Since most of
the crab wastes contain she ll pieces about a half inch
in diameter, a grinder was in stalled to chop them in-
to s maller pieces. It wasn't lo n g before that idea was
scrapped. The grinder tended to clog co nstantly, adding
labor a nd m aintenance woes to the project.
Gas storage also was a con stant p ro b lem with this
pr oject. This was partially due to the unavailability of
the large used boiler and partially due to the u nexpe cted
high quality of the gas produce d.
Conclusions and Problems
Although Vowell rated his project a technical success,
he readily admits that it was an eco n omic bust. "It's a
shame, because the digester could offset about 25 to 30
per cent of the ir fuel costs'.' Vowe ll thinks that if he had
access to a lab with hard data o n quality and qua nti ty
of gas per pound of was te, he co uld have developed the
necessary projection s. "These people (the cannerie s )
operate on a yea rl y basis, and unless yo u can prove a
quick payoff, it 's very hard to convince them to use your
ideas;' said Vowell.
Another problem facing Una la ska is its location. T he
traveling d ignitaries that could have supplied the ty pe of
support this project needed, never came to see it. "A
similar project in H omer, would have made t he fron t
p ages;' he said. Yet, Vowell feels th at it 's the remote
loca ti ons t ha t ne ed the he lp .
During the operating period, the la rge pump used to
fill the digester fr om the East Point Cannery failed. This
made Vowell b eli eve that a less exo ti c, easier to feed
batch type digester may be more economical for these
operati ons. Since the crab and other shell fi s h a re sea-
son a l, running t he digester through out the yea r didn't
make sense. Crabs and shrimp, a lthough they were not
actuall y tested , "have a shell, and that shell is the real
source of the carbon" needed to make good methane.
Salmon and bottomfish do not have the extra carbon and
therefore produce low quality gas, requiring lots of extra
scrubbing to remove excess carbon dioxide and hydrogen
sulf ide gasses.
A seco ndary market was hinted at with the sludge by-
product. An acc idental spill one yea r res ul ted in a bright
green splotch of grass the next. T he b io-digester output
co uld be package d as a high-quality fert il izer, helping
offse t operatin g costs, Vowell b elieves.
Funding
U.S. Department of Energy $11 ,800
Grant Recipient
R. Charles Vowell
801 Airport Heights #226
Anchorage, Alaska 995 04
A plastic bucket (a bove) covers the electric motor of the
digester pump.
62
Design allows for
continuous gas production
Doug McKee is recycling pig waste for new uses. He's
converting it into methane gas to heat his barn, and
spreading the leftover, nitrogen-rich sludge on his fields
for fertilizer.
"I had read in some farm journals that people (Out-
side) were using manure to make methane gas and it
seemed like it was a good concept," says McKee. "We
wanted to use the methane to heat the barn :'
Keeping the pigs warm on McKee's 300-acre farm isn't
as easy as it sounds. The McKees live at Mile 20 on the
Chena Hot Spring s Road, which is near Fairbanks, where
winter temperatures can plummet 40 degrees below zero .
During winter, Doug and his brothers used to have to
get up in the freezing cold to make sure a wood stove was
still keeping their two-story, 40-foot diameter barn
warm.
But McKee now hopes he'll be able to make enough
methane gas that his family members won't have to
worry about the old wood furnace anymore.
"It 'll be a lot more convenient ," said McKee . "So far we
haven't had any trouble. Everything's been going like it 's
supposed to:' Results from first use of the digester in
mid-1984 were not yet available at press time .
Design and Construction
Pig manure is converted to methane and nitrogen-rich
sludge inside of a specially-made methane digester tank .
It's housed in a 20-foot-by-40 foot metal building that
sits on top of a concrete slab. He bought the building
from an Alyeska Pipeline Service Company subcon-
tractor for about $6,000 and invested another $6,500 on
construction, electrical wiring and urethane insulation.
63
The methane digester is composed of several parts
including a 1 ,000 -gallon predigester, a 7,000-gallon main
digester, a methane storage tank, and a water boiler.
The system McKee built is a continuous flow digester.
This means he adds a load of about 150 gallons of pig
manure to the 6,000-g allon tank several times a week to
maintain continuous methane gas production.
'The main advantage of our design is that there is no
interruption in the production of methane gas;' said
McKee .
Pig manure flows by gravity from the barn to a pit
beneath the floor of the building that houses the digester.
The manure is then pumped from the pit into the predi-
gester tank where it is heated to 95 degrees by hot water
circulating through 125 feet of three-quarter inch poly-
butylene pipe.
Gradually the oxygen is removed by bacteria thus
yielding an anaerobic material. This is important
because methane gas will not be given off until all of the
oxygen is eliminated.
After a couple of days in the predigester tank, the
manure is pumped into the main digester, which is a
converted railroad tank car insulated with three inches of
urethane . The 95 degree temperature is regulated by a
thermostat in both digester tanks by circulating boiling
water through 150 feet of three-quarter-inch polybuty-
lene pipe. It takes about a month for the manure to pass
through the main digester.
The methane, an odorless, colorless gas, rises to be
stored in a tank on top of the methane digester. The gas is
piped from the storage tank to a boiler (housed in a
separate fireproof room) and used as fuel to he at water
for circulation through pipes that heat the methane
digester and the barn.
"I plan to put a big radiator in the center of the barn
with a fan behind it ," McKee said . 'The hot wa ter w ill
circulate through the radiator a nd the fan will blow the
heat through the barn:'
The liquid s ludge that remains in the di gester is grav-
ity-fed out of the main digester tank into a honeybucket.
McKee spreads this nitrogen-rich sludge on his fields as
an organic fertilizer. Recycling human and animal
organic wastes in this way has become common practice
across the U.S.
"One of the places I think a digester would be real
useful is on small farm s where a person only has a few
acres of land and doesn't really have a place to put the
manure;' said McKee. 'The digester would come in real
handy on a small farm :'
Problems
The only serious problem McKee has encountered
occurred shortly after he fired up his methane digester
for the first time in the fa ll of 1983.
Large barley hulls that had not been ground up
enough to be completely digested by the pigs clogged the
system and prevented the manure from flowing properly.
The hulls are made of tough cellulose which can not be
digested very well by bacteria, as well . And the hulls
stuck to the heating coils, preventing t he heating coi ls
from warming up the tank.
64
McKee, however, fixed the problem by installing a
finer sc re en for his feed grinder. Now, he doesn't have to
worry about barley hulls clogging the digester.
Tips
McKee has the following suggesti ons for those w ho
may try a system similar to his:
• Methane is a highl y flammable gas. Make sure the
system does not have any leaks before filling it with
manure. Check for leaks by pumping compressed
air into the digester and pour diluted dish soap
around each one of the welds and pipe joints.
Bubbles in the soap indicate a gas leak.
• To prevent manure from forming layers of scum,
install a bar with paddles across the center of the
predigester tank. Connect the bar to a handle out-
side the tank so it can be rotated periodically. The
apparatus works like a mixer, breaking up scum at
the tank bottom .
• Clean or wash out the s ludge pipe periodically, to
prevent s ludge from freezing solid in the pipe du rin g
wi n ter.
Funding
State of Alaska
U.S. Department of Energy
Grant Recipient
McKee Inc.
$15,000
15,000
20 Mile Chena Hot Springs Road
SR Box 50985
Fairbanks, Alaska 99701
Methane originators (previous page). A gas co llection dom e
(/eft) sits atop the digester. (above) McKee stands n ext to the
insulated digester tank.
Solar power helps count
fish
As Alaska's Bristol Bay region prepares for the
onslaught of fishermen, processors, boat tenders, and
others who follow the great salmon runs into this world-
renowned fishery each summer, a team of biologists sets
the stage for the large commercial fishing season to begin .
The rivers that are tributary to the great Bristol Bay
region along the Alaska Peninsula, together with lakes
upstream, are the spawning grounds of these millions of
salmon sought the world over.
Because the fishery is managed on a sustained-yield
basis, the season does not open until enough salmon
have escaped upstream to sustain the species. The fish-
eries biologists who count these fish struggling upstream
herald the opening of the season. Days before the first
fishing nets ply the waters of Bristol Bay, the Alaska
Department of Fish and Game has set up camp waiting
for the fish to arrive .
But until the Department of Fish and Game's success-
ful experiment with solar panels, fish tracking opera-
tions in the field were both cumbersome and costly.
None of the remote field sites in the Bristol Bay region
(the test area for the application of solar power to the
salmon counting process) is connected by roads or served
by commercial electrical power.
65
The electricity that is needed to run sonar salmon
counters, refrigeration units, radios, spotlights, and
range marker lighting systems has traditionally been
generated by portable gasoline engines .
The gasoline, along with the generation units and
replacement batteries for lighting systems, had to be
shipped to the field sites by float planes or boats. Not
only was this time-consuming, it also added to the
already high cost of fuel.
The agency's experiment with solar panels, however,
has shown the practical benefits of this alternative energy
technology for salmon tracking operations. Operational
expenses for fossil fuel consumption and transportation
were reduced, and the need for hauling around most of
the bulky power supply equipment was eliminated .
Before Fish and Game began its solar energy project,
biologists collected and analyzed power requirements
over a several year period for sonar salmon counters,
marker lighting systems, refrigeration and radios, to
match power supply with demand.
Mean solar radiation for June and July, the time of
year when migrating salmon are counted, was collected
from 1961 through 1969 at the Lake Aleknagik camp
near Dillingham, and from 1966 through 1977 at Lake
The solar panel (above left) being rotated into the sun; (above
right) the sonar fish counter is powered by the solar panel.
Iliamna.
The mean Ju ne-July air temperature recorded at camps
at Cape Newenham, Iliamna, Dillingham, King Salmon
and Intricate Bay from 1961 through 1979 was 51.6
degrees.
Ave rage daily available solar panel p ower output was
calculated at 22.4 ampere h ours or 270 watt h o urs .
Power requirements for the salmon solar co unters,
according to Bendix Corp., manufacturer of the counters,
are .038 ampere hours a day for adult salmon counters
and .25 ampere hours a day for smolt counters.
Twenty ampere hours of power a day are needed for
refrigeration , based on the operation of a cooler at a set-
ting of 35 deg rees for 10 hours a day, with an ambient air
temperature of 51.6 degrees.
Radio communication needs are 10 hours standby
daily, plus two to four transmissions a day, each averag-
ing three minutes. The tota l radio power requirement is
2.3 ampere hours a day, based on 1.3 ampere hours for
broadcasting and 1.0 ampere hours for s tandby.
The use of sol ar panels to power marker lights came as
a n afterthought to department officials, so elec trica l
requirements weren't known.
However, they have worked well when connected to a
12-volt storage battery which is connected to one solar
panel.
Solar electrical panels have been utili zed successfull y
at a number of remote field sites throughout the Bristol
Bay region:
Portage Creek Radio, adult salmon
Nuyakuk Salmon Tower
Togiak Salmon Tower
lgushik River Test Fishery
Wood River Smolt
Gechiak River Wier
Kvichak River Smolt
Naknek River Smolt
Egegik River Smolt
Ugashik River Smolt
sonar, cooler
Radio, two spotlights
Radio
Radio, cooler
Smolt sonar counter
Radio
Smolt sonar counter, radio
Smolt sonar counter, radio
Smolt sonar counter,
radio, cooler
Smolt sonar counter,
radio, cooler
Ugash ik Salm on Tower Radio, cooler
N ushagak District Range Light S trobe range light
A normal counting si te will have three people tem-
porarily livi n g at the location. Three solar panels, each
connected to its own battery, supply the power for two
sonar counters a nd the ra d io . The two sonar counters are
located on either s ide of the river ; thus, it is ver y efficient
to have the separate solar pane l/battery units located at
the point of use.
66
The radio is located in a third tent usually separated
from where the counters are located .
At N uyakuk, sonar counters are not used. In stead,
counting towers b uilt o n the edge of either side of the
river are used for visual counting with a hand counter.
At night, the spotlight using power from t he solar panel/
battery units enables the biol ogists to see the fish swim-
ming up river and count them.
At those sites which utiliz e electric coolers, two solar
panels have been used to charge batteries. H owever, these
coolers tend to us e more electricity than the 10 hours a
day originally planned.
This causes severe battery drain , si nce two solar panels
alone can not provide an adequate direct power supply.
One or two solar panels provide adequate power to
operate equipment and recharge batteries at camps with
salmon sonar counters and /or radios o nly.
The use of solar panels to recharge range marker lights
fo r fishing district boundaries was tested after thei r suc-
cessful use w ith other equipment. One test light was
maintained throughout the fishing season with solar
power alone.
Solar panels to power field camp equipment for track-
ing salmon populations are now standard equipment at
most Bristol Bay field sites.
Technical notes
The equipment u t ilized in this project is o utlined below :
Solar Panel: Arco Solar, Model AS116-2300, power
rating 2.3 amperes per hour.
Cooler: Koolatron, Model P34A t hermo electric
cooler with 24-litre capacity, 16 by 12 by 11 Vz inches,
with an adjustable temperature setting range of 25
degrees to 125 degrees with a maximum o utside tem-
perature drop of SO degrees , power re quirement of four
amperes per hour during drawdown a nd less than two
amperes per hour when cycling at holding temperatures.
Range Marker Light: Pennwalt Automatic Power,
Model PA240 Strobe li gh t at eight ampere hours
per night.
Funding
U.S . Department of Energy $9,736
Grant Recipient
Alaska Department of Fish & Game
333 Raspberry Road
Anchorage, AK 99502
Capturing energy above
the Arctic Circle
James Schwarber is converting sunlight and wind into
electrical power at his log cabin above the Arctic Circle.
In fact, he likes his photovoltaic panels so well that he's
selling similar solar products through his business,
Remote Energy Systems, when he isn't out hunting and
trapping.
"It all started when I wanted to keep batteries charged
in the woods;' says Schwarber, who lives near Kobuk,
about 350 miles northeast of Fairbanks. "I got a wind
generator and when I found it was not satisfactory, I
moved up to photovoltaics;' cells that convert sunlight
directly to electrical energy.
The combination of power sources keeps his bank of
12-volt marine deep-cycle batteries charged year-round .
The photovoltaic, for example, even produces a trickle of
power between November and February when the sun
doesn't rise above the horizon.
Schwarber says he has more than enough power at his
remote cabin for his lights, two-way radio, short-wave
radio, vacuum cleaner, water pumps and 12-volt electric
chain saw.
Design
Schwarber chose a four-foot-square , Arco Solar
ASI-16-2000 photovoltaic module panel, mounting it on
a five-inch diameter spruce pole that rises 11 feet above
his log cabin roof. The four-module solar panel, which
weighs about SO pounds, was attached to the pole with
an SPM-4-65 pole mount.
The solar panel was installed above his roof to mini-
mize shading and to keep it out of the reach of pawing
grizzly bears.
67
Schwarber used No. 10 AWG UF cable to link the
solar panels with three 105 amp-hour, 12-volt, Gould
deep-cycle marine batteries, which are connected in
parallel series .
And he ran a No.4 copper wire from the top of the
mounting pole to a ground rod driven seven feet into the
earth below the pole. He also grounded the four solar
modules to the No. 4 ground wire, and added six guy
wires to the pole for stability.
A Winco 1222H 200-watt wind generator acts as a
backup power production system .
Schwarber could have chosen other equipment for his
dual-energy-source configuration, but the project gave
him what later became the opportunity to "field test" a
new commercial product and service.
Performance
Overall, Schwarber says his photovoltaic system and
wind generator are working very well. In fact, he has
plenty of power to supply his simple electrical needs at
the trapping cabin .
Two minor problems, however, surfaced about a
month after Schwarber set up his photovoltaic panels.
Three silicon cells on one panel cracked and several solar
cells had discoloration, but there was no moisture in the
cells. It appeared that the discoloration may have been
caused by a chemical reaction of the components in the
module, and a defect in the Tedlar backing may have
contributed to the cracking.
"So far, I have found that the photovoltaic array and
wind generator complement each other well;' Schwarber
says. "Periods of peak solar energy and peak wind
James Schwarber's trapping cabin near Kobuk (abov e); a solar
collector and a wind generator (/eft) are placed out of the reach
of bears.
energy rarely coincide, which results in a more continu-
ous production of electricity than either system provides
alone:'
Good data has been collected on the system, thanks to
a 10-amp ammeter he connected to the cable linking the
solar panels with the battery bank . On occasion the out-
put from the solar panels was about 10 amps, or about
10 percent greater than the manufacturer's rated output.
The solar panels can produce approximately 60 amp-
h ours of electricity on a clear summer day. When the
batteries reach 15 .1 volts, the Arco battery protector
relay is tripped and the charging current is lowered to .5
amps or less and the voltage is dropped to 13.8 volts.
During heavy overcast days, the system's output was
minimal ranging from 0 .3 to one amp all day. Partly
cloudy, hazy or lightly foggy days resulted in moderate
to high outputs.
But the important thing, Schwarber says, is that even
in mid-winter when there is no sunlight the photovoltaic
system continued to produce power from stray night
light. This means he doesn't have to worry about his bat-
tery bank going dead and freezing up when he is away
on hunting trips.
Electric lights a
wilderness luxury
Susan Rainey got tired of relying on gas lanterns to
light her log house . So she invested in a photovoltaic
energy system.
"A nd I love it;' says Rainey, who lives at mile 326 of the
Parks Highway, 42 miles from Fairbanks in the shadow
of Mount Denali (McKinley). "I just walk in the house
and turn on the lights. I'm ecstatic with it."
Rainey, a former alternative energy newsletter editor,
became interested in solar energy through volunteer
work she did at the University of Alaska-Fairbanks.
But it wasn't until she discovered that the nearest
power connection for the house they were building in
1981 and 1982 was 16 miles away that she decided to
install the solar panels at her home. With her 1981 AT
grant Rainey purchased the system. Since her home was
not finished, a neighbor used the photovoltaic panels
until Rainey's house was finished.
Now she doesn't have to rely on gas lights or electrical
hook-ups anymore.
'They've held up real well," she says. "We had no prob-
lems with it:'
Design
Ten ARCO ASI 16-2300 solar panels were mounted on
68
"I have found that I can leave the photovoltaic array
hooked up to an Arco battery protector to protect the
batteries from both overcharging and freezing," he says.
'This I find to be one of the most valuable aspects of
photovoltaics-safe, reliable , unattended charging of
batteries is possible.
"Another valuable aspect of having a photovoltaic
array is its ability during cl ear weather and low lo ad
periods to fully charge up the battery bank in a smooth
and controlled fashion," says Schwarber. 'This will
result in maximum lifespan of the batteries, which are
difficult to ship and expensive to buy:'
Funding
U.S. Department of Energy $1,850
Grantee
James A. Schwarber
P.O. Box 81997
Fairbanks, Alaska 99708
top of Rainey's roof to get the maxi mum amount of sun
exposure and to minimize shading from nearby trees .
Each panel is rated with a peak of 37 watts so that
when she uses all10 panels she has a 370-watt peak out-
put from her array, which is about four feet wide by 10
feet long.
The power is stored in eight, 82 .5 amp Gould batteries.
An inverter converts the photovoltaic alternating current
into direct current for the home's appliances.
Performance.
So far, Rainey says she's pleased with her photovoltaic
se tup. She says it produces electricity even on cloudy
and rainy days.
Better yet, she says the system has not broken down or
malfunctioned.
'They work fine," she said of the panels. "''m ecstatic
about it :'
Funding
U.S . Department of Energy $5,800
Grant Recipient
Susan E. Rainey
P.O. Box 81182
Fairbanks, Alaska 99708
Photovoltaics perform
well in Alaska Bush
The high cost of shipping oil and gas to his remote
cabin prompted Thomas Vaden to install solar panels.
He also wanted to show that solar power is practical
for isolated cabins in the Interior, such as his wilderness
survival Solo Creek School at White River southwest of
Tok.
"We've been very satisfied with the solar panels;' says
Vaden, an Anchorage elementary school teacher.
'They're efficient and there's no maintenance.
"If you were looking at summer recreation cabins
where you were gone a lot, you could put in one panel
and a couple of batteries and you'd have all the power
you'd want for weekends'.'
But he's had his share of obstacles to overcome .
Bush pilots were reluctant to transport his batteries for
fear that the battery acid might spill and ruin their plane .
A fire also destroyed one of the two solar panels he
installed.
Vaden also learned that it's better to purchase more
solar panels and fewer batteries . He said he didn't need 17
batteries for his two solar panels. Buying more than five
batteries creates a storage problem because the batteries
must be stored outside of the cabin because of hydrogen
gas emissions.
"One can't store a lot of batteries in the house because
they produce an explosive gas and they will freeze
(outside) after minus 60 degrees;' he says . "I would
recommend having four solar panels and four batteries .
That's more than enough for a two-room dwelling with
50 and 75 watt lights:'
69
Susan Rain ey 's solar collectors are temporarily mounted on a
n eighbo r's house (left ).
System Design
Vaden installed two commercially built Solarex brand
solar panels on top of two cabins. The two 12-volt
panels, 17 inches by 42 inches, can each produce 3 .5
amps when the sun is shining.
The panels are connected to a bank of 225-amp, deep-
cycle batteries. Power from the batteries provides elec-
tricity for operating the lights and radios .
Initially, Vaden planned to store his bank of 17 bat-
teries in a separate building heated by a wood stove.
But he abandoned this plan because of the possibility
that flames from the wood stove would ignite the gas
emitted by the batteries.
Vaden says he's considering putting his batteries in an
underground pit with foam insulation. The ground,
while cool, will not get so cold that the batteries will
freeze and crack .
A gasoline generator and charger for the battery bank
provide emergency backup.
Performance
The solar panels have operated well for the past several
years, producing more than enough electricity for lights
and radios.
Unfortunately, a fire destroyed one of the cabins with
the solar panels early in the summer of 1984. Vaden does
not know what caused the blaze.
The second solar panel, however, is still producing
electricity at another cabin. He said the solar panels also
have not required much maintenance .
Tips
Vaden says he's learned several things from his expe-
rience including:
• To avoid storage problems, consider using less than
five batteries so that they can be stored inside the
home.
• If more than five batteries are used, store them in an
insulated pit outside the cabin as a safety precaution
against explosive gas produced by the batteries.
• Consider purchasing battery seals which will
contain any gas produced by the batteries.
70
Funding
U.S. Department of Energy $5,705
Grant Recipient.
Thomas H. Vaden
Solo Creek Wilderness School
5827 S. Tahiti Loop
Anchorage, Alaska 99507
tl
Electric current from
wood stove heat
W. Findlay Abbott is experimenting with making
electricity from heat by using thermoelectric generators
on his woodstove .
"It's right in the same class as solar cells ;' says Abbott,
an Anchorage resident who makes architectural models
for engineering firms, "the same technology as semi-
conductor materials '.'
"I knew ·about it because my father was a scientist who
had a research lab and studied thermoelectric. I've
known about it for most of my life:'
So far, he's still experimenting with different thermo-
electric generators and has used them to recharge flash-
light batteries. The units, which use waste heat , can be
installed in many places including heating stacks, stove
pipes and exhaust pipes .
'The thermoelectric generator is silent, maintenance-
free and produces electric current as heat is radiated
from the stove to the room;' he says. "A remote house-
hold could be virtually energy independent; fire hazards
of candle and kerosene lighting also could be eliminated;'
he said.
A thermoelectric generator is essentially an extension
of the thermocouple , a device found in gas heating
systems . It was discovered long ago that when two
dissimilar-metals are fused at one end, a small electric
current can be measured at the other. This is because
each element on earth has a different electrical property,
much like humans have different blood types. When
making thermocouples, materials are chosen to produce
a stable and predictable current value over a specific
temperature range. By monitoring the current with a
precision meter, it is possible to accurately control
processes that use both extremely high and extremely
low temperatures.
Thermoelectric devices use the same principle as a
thermocouple except that they exploit the ability to
produce electricity and not the stability of the electricity
produced. In thermoelectric generators, the two dissim-
ilar materials are chosen to produce a maximum amount
of electricity over a certain temperature range . The
chosen materials can be either metal or semiconductor
alloys, depending on the temperature range at which the
thermoelectric generator will operate.
The generators are formed by layering flat plates of
71
THERMOELECTRIC
these materials with some form of insulation between
each layer, usually ceramic. Wire leads fused to the outer
surfaces of each layer are tied together so that output of
the device is the combined output of all the wafer layers.
System Design
Abbott's thermoelectric generator is comprised of a set
of solid-state, semi-conductors sandwiched between
ceramic and steel plates . Steel plates are used in this
design because it is virtually impossible to attach out-
put leads directly to semiconductor materials. Other
materials that can be used include platinum and radium,
copper and constantan (an alloy of copper and nickel),
and iron and constantan .
The six-inch-by-10-inch thermoelectric unit needs to
be placed against a hot surface, such as a wood stove .
These units, however, can withstand temperatures only
up to 400 degrees .
As heat flows through the unit, the temperature dif-
ference between the stove side and the room side of the
device causes current flow. This power is then stored in
nickel-cadmium batteries.
'Thermoelectric generators are solid-state devices
which convert heat to electricity without moving parts,
when the heat flows through certain dissimilar conductor
materials in junction;' says Abbott. The thermogener-
ative properties of the materials cause current flow
(electricity) to be produced.
"A small percentage of heat produced by a normal
wood stove could generate enough electricity for several
light bulbs and a radio;' he says.
Performance
Abbott says the thermoelectric units appear to work
quite well for recharging small batteries.
"It works. I produced a trickle charge for a battery;' he
said, but added that he's still experimenting with larger
applications .
Funding
U.S. Department of Energy $805
Grant Recipient
W. Findlay Abbott
538 M Street
Anchorage, Alaska 99501
Gold miner tries
new boiler system
Keeping a home warm in the Alaska Interior where
one has to live without such modern amenities as heating
and plumbing is a tough proposition.
But innovator John W. Greene, Jr. has developed a
baseboard heating system that keeps his home a snug 74
degrees-even when outside temperatures. plummet to
minus 42 degrees.
"In fact, I believe we have the most comfortable house
in the Interior and it is all done without electricity-no
pumps-just a wood-fired boiler," says Greene, an
engineer and gold miner who lives in Eagle.
"It's working pretty well;' he said. "But I'm still trying
different things. I'm an engineer and I have to tinker with
things:'
Design
Greene keeps his house warm by circulating a hot
water and antifreeze solution in a continuous loop
between his furnace and baseboard heating units that are
placed along the floor of each room .
The heart of the system is an eighth-inch, steel-plated
boiler he put on the concrete floor in his basement. The
boiler, which uses three-foot-long logs, has a two-inch
layer of sand in place of a grate. The sand holds the heat
and directs it back into the fire, making it easier to burn
"green" wood. There also is a one inch thick water jacket
on top of the stove .
The water and antifreeze flow into the bottom of the
boiler through a three-inch-diameter steel intake pipe,
which has a series of welded nipples. Each nipple pro-
vides for connecting three-quarter-inch copper pipe,
which links the colder-water return pipe with a similar
heated-water supply pipe at the top of the firebox. There
are twelve separate copper pipes inside the firebox.
73
The antifreeze heats up as it flows through the copper
pipes leading from the bottom to the top of the firebox,
traversing the flames.
At the top of the firebox, the heated water and
antifreeze rises up a three-inch-diameter steel pipe,
which passes through the water jacket. The steel pipe
ends in a T-section with welded steel nipples connected
to three-quarter-inch copper pipe.
Each branching copper pipe makes a loop through a
different section of Greene's home, channeling hot water
through fin type baseboard heaters .
Greene also installed a valve at each nipple-copper
pipe junction to control the amount of hot water cir-
culating through each loop, enabling him to regulate
room temperatures .
The hot water/antifreeze solution bubbles upward
from the boiler to the first-floor and moves horizontally
through the heating baseboards before flowing back into
the furnace .
"It is really important that the hot water line coming
out of the furnace rises to the first floor baseboards, and
when the antifreeze gets to the end of the heating loop it
must go down to the furnace," Greene said . 'To avoid
water or air traps (that don't allow the water to circulate),
you don't want to have ups and downs in the pipes:'
The building codes that apply to boilers do not nor-
mally allow an individual to construct a boiler with-
out going to the major expense of having the unit rated
by the American Society of Mechanical Engineers
(A.S.M.E .).
But Greene doesn't have to worry about the issue
because he built an atmospheric heating system . The
furnace creates no pressure when the antifreeze is heated
An early version of the boiler (left) before a refractory liner
was replaced with sand. (Above), winter sets in at Greene's
cabin in Eagle .
because it is open to the air via an expansion tank
located above all the piping in a bedroom closet. The
tank is a small garbage pail with a loose-fitting,
removable lid that was welded atop a three-quarter-inch
copper pipe connected to the heating system. The tank
maintains pressure on the system, while making it easy
to repleni sh the water and antifreeze .
Performance
Overall, Greene says his heating system has performed
very well. It keeps the house evenly heated and has not
required much maintenance.
'The coldest outside temperature that I have been able
to test the system in has been minus 42 degrees;' Greene
says. "The temperature inside the house was held at 74
degrees over a 24-hour period . No e lectricity was used in
the system either in the control or in the pumping of the
hot water (antifreeze).
"I had to f ill the furnace with wood once every eight
hours;' he says. 'The house was even more comfortable
than a normal c ity home with baseboard heat because
with this system the hot water flows through the base-
board units continuously at a lower temperature than
with a gas or oil fired system, thereby giving you a very
stable temperature in the house ."
Greene also tried building a heat storage, but it didn't
work out very well. He dug an e ight-foot square hole in
his cellar floor, placed three-quarter-inch copper tubes in
74
it , and filled it with sand. He had hoped to pump hot
antifreeze through the h eat storage so that whe n he was
not at home, the heat storage would keep the cabin warm
after the boiler fire stopped.
U nfortunately, the pipes leaked and he had to abandon
the project. But he sa id he doesn't need the heat storage
b ecause his log walls reta in heat well.
Tips
Greene has several suggestions to make from his
experience:
• Don't u se fire bric k in the furnace . The fire burns
longer-and better-without it.
• Don't use a grate in the fireplace . A couple of inches
of sand inside the furnace works a lot better. The
san d holds the heat and reflects it back into the
flames, in creasing combustion efficiency, especially
for g reen wood.
• Make sure the copper tubing does not have any
unnecessary bends or traps which can prevent the
antifreeze from flowing.
Funding
U.S. Department of Energy
State of Alaska
Grant Recipient
Jo hn W. Greene, Jr.
Box62
Eagle , Alaska 99738
$2,300
2,300
Design goal:
Energy efficiency
David Newcombe doesn't believe the oil supply is
going to last forever.
That's why he 's busy experimenting with alternative
energy. Recently, he built a wood-fired boiler to provide
heat for his home in Wasilla , about 45 milies north of
Anchorage.
"''ve also built wind generators and I'm playing with
solar voltaics;' says Newcombe, a heavy equipment
operator and maintenance welder. ''I'm interested in
alternate energy in general:'
So far, his wood-fired boiler is successful. Another
boiler he built for a neighbor has been operating
smoothly for the past four years .
"I see so many inefficient wood burning systems
around that I thought that there must be a better way to
go ;' says Newcombe. "It seems to be working real well. It
heats a whole house'.'
System Design
A 1,000-gallon-water tank that's six feet high and five
feet in diameter is fitted with a firebox . The tank is made
of 118-inch steel plate.
The boiler unit, which was placed on top of two
inches of styrofoam, is in his basement.
The firebox, also made of 1 /8-inch steel plate , is two
feet by three feet in size. An eight-inch-diameter steel
pipe with 1/4-inch wall extends through the water tank,
to a chimney above.
The firebox , which is lined with 1.5-inch thick fire-
brick, is divided into two combustion chambers by a
steel plate that slides in and out o f a sidewall. The divider
helps create a downdraft to make the fire burn hotter.
The water tank is insulated with nine inches of fiber-
glass so that the water temperature drop during warm
periods is less than two degrees a day.
Domestic water is heated through a 60-foot-long coil
of half-inch tubing suspended near the top of the water
tank . The drinking water circulates through the copper
tubing and is warmed as the water is flowing to a faucet
through the pipe .
Eventually, Newco mbe also plans to circulate hot
water from the tank through a baseboard heating unit to
help heat his home.
Performance
"Smoke and creosote are almost nonexistent;' says
Newcombe . "Heat storage lasts two to seven days
depending on demand, and the wood consumption is
lower than that of the Earth Stove used previously'.'
Funding
U.S. Department of Energy $2,547
Grant Recipient
David R . Newcombe
Box 871663
Wasilla, Alaska 99687
The hand-made Stirlin g engine David Newcomb e added to his
boiler.
75
WOOD-FIRED STEAM BOILER AND ENGINE
Steamboat to ply the
Holitna River
Long before Grant Fairbanks m·oved to his 40-acre
homestead near Sleetmute on the Holitna River, steam-
boats were the major form of summer transportation. By
Fairbanks' time, steam had given way to faster gasoline
and diesel engines and the airplane. Cheap petroleum
had put the old, slow, wood-burning paddlewheelers out
of business.
Then came the oil crisis with its dramatic rise in
petroleum-based fuel prices. Every penny added to a
gallon of gasoline brought a corresponding jump in
transportation costs. By the late 70s, transportation
charges were about to put supplies and fuel out of the
reach of the homesteaders along the river. Fairbanks felt
that the time was ripe for a return to steam power.
Sleetmute and the Holitna River area are surrounded
by thousands of acres of natural renewable resources-
fast growing birch and spruce forests. Furthermore,
Fairbanks knew where he could get a boiler. He figured
that by bartering, many homesteaders who were priced
out of the petroleum-based transportation system could
use a small steamboat service, paying transportation
charges with goods or cash. In an area where wood is
more plentiful than cash, this type of system could bring
a return on investment.
Fairbanks began to build his wood /waste-oil fired
steamboat for use on the Holitna River in late 1980 . The
project involved constructing and outfitting a flat-
bottomed, steam-p owered riverboat and maintaining
records to help illustrate the usefulness and economics of
the project.
77
Design and Construction
The pro ject was divided into four parts: building the
boat; obtaining a boiler and steam engines and moving
them to Sleetmute; designing and building a transmis-
sion to transmit the power from the steam engines to a
rear-mounted paddlewheel; and installing all the
mechanical hardware on the boat.
The 38-foot boat (includin g paddlewheel) is made of
three-quarter-inch marine plywood and local spruce
donated by an area sawmill. The boat's skeleton is made
of 1 1/z-inch bottom planks with two-by-six ribs. Over
this skeleton is a skin of plywood. With a beam of seven
feet and three-foot sides, the boat could safely tote an
eight-ton load while drawing only 10 inches of water.
The boat design itself borrowed heavily from the river-
boats that plied the Upper Mississippi River near the turn
of the century. The Holitna is the same type of shallow,
winding river with shifting gravel and sand bars. One
modern innovation was added however; the bottom
would be covered with fiberglass and resin. All other
surfaces are covered with wood sealer and painted.
Although the hull design and steam engines could
push the boat at speeds up to 10 miles per hour, river cur-
rent would reduce this to about four or five miles per
hour traveling upstream.
Power for the boat is from a wood /waste-oil fired low
pressure steam boiler, two 10-horsepower Sturtevant
steam engines, and a large stern-mounted paddlewheel.
A small but strong transmission transfers power from
the s team engines to the paddlewheel. The steam engines
A recycled steam engine (left ) is to be used to power the steam-
boat. (Above), work on the steamboat proceeds on the banks
of the Holitna River.
have a "square" bore and stroke of five inches and pro-
duce their rated horsepower at 325 rpm.
Fairbanks got the engines from a Minnesota firm that
had been using them for almost 40 years. They still have
an estimated 20 years of life left in them. Simplicity, rug-
gedness, and the 20-year life make them an excellent
choice for use in Bush Alaska.
The boiler was to serve a double life; Fairbanks is also
a master woodworker and during the long cold winters,
he spends much of his time in his shop. During the times
when ice on the Holitna makes riverboat travel impossi-
ble, Fairbanks figured to muscle the boiler to his shop to
power his tools. When the river cleared each spring, he'd
move the boiler back to the boat. Unfortunately, the
boiler Fairbanks intended to use for this project was not
ASME stamped to meet state regulations and he was left
with the problem of getting a new boiler; although the
original boiler was already in Sleetmute.
A company in California was chosen to make the new
boiler. It would have the same basic characteristics as the
original (52 boiler tubes of two inches by four feet) and
an operating range from 100 to 150 pounds per square
inch pressure (psi). The original firebox for the first
boiler would be used with the new one.
As of mid-1984 the boat was nearing completion.
The nearly complete steamboat w ith paddlewheel,
boiler and steam engine mounted (top left). The
paddlewheel assembly waits to hit the water
and Debbie Fairbanks ' washing machine
shows that a home-style water tower can serve
both household and steam engine uses.
78
Problems and Conclusions
Fairbanks encountered many small p roblems d uring
this project; most of all with government certification
requirements for his boiler. The need for a new boiler
delayed the project a full year and increased costs about
$2,000.
Other problems included normal communication
problems encountered in the Bush and an abnormally
wet summer. The wet summer kept the spruce for the
boat's skeleto n from drying to a maximum -of 15% water
content.
Communication problems stranded the new boiler in
Bethel for a couple of months, causing another season
delay. But even with the delays, there still seems to be a
lot of enthusiasm for this project to ensure its ultimate
success.
Funding
U.S. Department of Energy
State of Alaska
Grantee
Grant Fairbanks
General Delivery
Sleetmute, Alaska 99688
$9,145
9,145
Wood-fired boiler requires
fuel supply and attention
A wood-fired b o iler a nd steam e n g ine produces
most of the heat , hot water and electricity that Guy
A. Matthews needs for his home.
It 's also a cost effective way to ge nerate power since
most of the fuel supply-wood-is readily available near
h is home at Tok, the principal road entry to Alaska and
Canada's Yukon Territory.
"It works good," says Matthews, a road construction
worker, referring to his system. "Running a small steam
plant for power is ridiculously expensive . But if it 's your
power and your heat then it 's pretty reasonable:'
Steam from the boiler runs a small , five-horsepower
engine to produce electricity, which is stored in a bank
of 12-volt, deep-cy cle batteries . The power is used for
li ghting, operating power tools, a television and radio.
But the system has its drawbacks. Until Matthews
installs automatic controls, he has to be around when the
boiler is fired so he can monitor its operation constantly.
"It's not a continuous running system," Matthews said.
"It's not something you can throw a lot of wood into and
walk away."
System Design
A three-foot-high, 20-inch-diameter boiler sits atop a
one-quarter-inch , s teel-plated firebox that is 32 by 32 by
24 inches .
79
The firebox also heats an adjacent, 30-gallon domestic
water tank, the garage, greenhouse and entryway. In
addition, Matthews supplements his heat with a wood-
stove.
Water in the boiler is heate d by hot gases rising from
the firebox into the boiler through 70 vertical cast iron
pipes. Matthews also installed a quarter-inch-thick steel
plate in the firebox so he can slide it under the boiler
when he wants to keep the boiler from heating and, in-
stead, direct the heat through the domestic hot water
tank.
Steam from the boiler drives a 85-pound five horse-
power, steam engine. The engine , manufactured by
Semple Engine Co., is 18 inches high by 18 inches long.
Operational pressures range from 90 psi to 150 psi.
"Once steam is up to pressure, I can maintain the
pressure of 100 to 150 psi by throwing in an armload of
dry mill wood, giving me about one hour running time,"
he says.
The alternator, turning at 2,200 RPM , will produce
enough electricity to charge a bank of four, 12-volt, 700
amp deep cycle batteries.
The batteries charge according to various settings on
the alternator. The charge rate has been varied from 15
amps to a full 65 amps, depending on the battery state of
Guy Matthews pre tes ted his steam engine (top left) in a loca l
parade. (Bottom left), an attach ed workshop nears completion.
A boiler and hot wa ter heater (above) are shown inside the
workshop.
charge .
Matthews al so connected a static converter onto the
battery bank to convert direct current into alternating
current providing up to 1,800 watts. He uses the power
to operate lights, fans, pump, radios, refrigerator and
other household appliances.
Performance
Matthews is s o pleased with his steam boiler set-up
that he plans to install a similar system in a remote log
cabin he 's building near Tok .
Eventually, he plans to expand the sys tem by using
part of the heat from the boiler for a baseboard heating
system .
And despite delays in acquiring the boiler and gover-
nors for regulating steam pressure, Matthews says the
project is worthwhile .
"For any given alternative energy set-up there are
delays and shortcomings;' Matthews says. "For certain
remote situations, such as mine, steam power for energy
From wood to steam to
electric lights
Located on the northern t ip of Prince of Wales Island ,
third largest island in America behind Kodiak and
Hawaii, Point Baker is about 150 mil es from Juneau and
a go od 45 miles from Ketchi k an . The only way in or o ut
is by boat or pla ne . This m eans that fuel to power diesel
gen erators is n ot only in sh ort supply, but al so ex pensive
to t ransport . Warren Powers fi gured that there must b e a
b e tter and cheaper way to generate ele ct r ical p ower
a n d heat.
P rince of Wales Isl a n d, like most of So utheast Alaska,
is b lessed with a n abundan ce of wood. Powers knew that
this wood could be used to make steam a nd , after all ,
steam b oilers ge n erated ele c tricity long before diesel gen-
erators . H e also k ne w t hat if a sys tem co ul d economically
produce elect ri city fr om forest wastes and reduce
dependen ce on n o nren ewa b le, ex p ens ive petroleum
product s, t hen su ch a system co u ld benefit not only
Point Baker, but sm all v ill ages in t he region, also.
Powers' project involved design ing a wood-fired
steam-powered electrical ge nerati n g sys tem . In addition
to the power plant, Warren would build a 900-square-
foot house, a 600-squ a re-foot greenhouse, and a heat
recovery system that woul d supply heat to both of them .
The heat recovery system would ensure that maximum
availa ble en ergy co ul d b e ex tracted from the system.
80
gives my family lights to read b y and running water f or
drinking and bathing.
"But the steam boiler and engine are practical only
where wood is easier to get than diesel or g as ;' he said,
because of the ex tra work and attendance required with
the wood-fired system.
Tip
Matthews says it's important to insulate the b o iler,
firebox and the domestic hot water tank to increase their
efficiency.
Funding
U.S. Department of Energy
State of Alaska
Grant Recipient
Guy A. Matthews
P.O. Box 963
Seward, Alaska 99664
Design and Construction
3 ,302
6,833
Powers planned to adapt a five -horsepower, w o o d -
fired boiler to fit the requirements of rural Alask a li v ing .
This included enlarging the fi re b ox to handle la rger
len g ths of wood (to ex tend burning time), adding a f ive-
h orsepow er steam engine, d evel o ping a governor to co n -
tro l the en gine's sp eed a t 1,800 r p m , and constructing a
m ethod of extrac ting res idual heat fr o m the spent ste am
to w arm a small , well-in s u l ated h o u se and greenhouse .
A six kilowat t 110 /220 vo lt a lternating curren t ge nerator
would b e co nnec ted to t he o utp ut sh aft of t he five-
horsepower s team engine. The result would be a re liable
source of both elec trical p ower a n d h eat.
The power ho u se enclosing t h e b oilers a n d steam
engines was planned as a 12-by-18-foot structure with a
gable roof, built on pilings 10 fee t a b ove a tidal flat . This
building also will house the hot water tank and heat
exchanger that provide heated water to the house a nd
green house. A smaller enclosed five -by-eight buildin g
housin g the s u pply water tank is also part of the project.
This structure is elevated above the level of the boilers
and water tan ks.
Two boilers and steam en gi nes will ensure constant
heat and power during maintenance periods a nd in case
of em erge n cies . An additio nal diesel powered ge nera tor is
planned in case of total failure of the steam power plant.
A 12-by-24-foot tempo rary greenhouse was originally
covered with Visqueen, but future plans are to cover it
with more durable fiberglass. Power from the generator
p lant will be used to both heat the greenhouse and
operate grow lights. These lights will effectively extend
the growi ng season to produce food year round .
Heat for the greenhouse will also be used to keep a
s mall , well-insulated house warm during the colder
months. Both the greenhouse and this small , 900-sq uare-
foo t house will have a 12 volt battery-powered back-up
pump system. This assures heat when the alternating
current generator (AC ) is not operati ng. A ll piping used
to transfer heated water and steam wi ll be insulated to
minimize heat loss.
Prob lems and Conclusions
The remoteness of Point Baker, Powers' unexpec ted
lo ng illness and difficu lties in lo cating commercially pro-
duced boilers that satisfied state safety requirements all
added long delays to thi s p roject.
81
Powers still feels that using renewable, locally avail-
able resource s to ge nerate elec tri cal power and heat
makes more sense than shipping in expensive petroleum
products. "With diesel fuel costing over a buck and a
quarter per gallon, I'd like to find an alternative," Powers
said in 1981, and he may still.
Another problem that faced this project was the lack
of roads and he avy equipment. Everything had to be
moved by small wood rafts or boats to the site location.
A block and tackle was then used to move the h eavy
equipment into final position.
By mid-1984 , the powerhouse, water storage house, a
temporary greenhouse, and most of the small house were
nearing completion.
Funding
U.S. Department of Ene rgy
State o f Alaska
Grantee
Warren F. Powers
Box 464
Po int Baker, Alaska 99927
$7,579
7,579
Driftwood and boiler
to heat home
Few ci tie s in Alaska are tied as cl osely to the timber
products industry as Ketchikan . Fo r thi s so uthernmos t
ci t y in Alaska, timber has long been a m a instay of the
economy. When the North American and Pacific Rim
eco n o mie s do well, Ketc hik a n h as a relatively
s t a bl e eco n o my, s upportedby both timber and fish.
When fuel and transportation costs climb, depressing
dema nd for pulp products, Ketchikan feels the pinch .
Ken Duckett's wood-fired b o il er sys te m , when com-
pl e ted, may fit well into the Ketchikan co ndition , saving
the costs of fuel when prices are hi gh , and making use of
ab und an t timber resource s, whatever the oil prices may
be. And as an engineer and in the construction trade,
Duckett a nd Ke tchikan residents like him must be
prepared for w hat the nex t season may bring in the
work force.
But Duckett's primary m otive for turning to a lternative
e nergy was to invest hi s expertise a nd time in de sign in g a
domestic source o f electricity that would save him money.
At the time he applied for the gra n t in 1980, Ducke tt
was ge tting r eady to build a new h ouse o n Pe nnock
Island, a b o ut one-half mil e from the ci ty of Ketchikan .
The nearest commercial e lec tri c it y was some 1,000 feet
away; co nnec tion to the syste m would b e cos tl y.
System Design and Construction
Duckett's project plan was si mple, u si n g proven (but
in many places, outmoded) tec hnology. He planned to
build a vertical, low-pressure boiler to produce 100 to
150 psi of s te am. The boiler would be f ired by driftwo od
found on tidal beaches in the area. Duckett planned to
u se the steam to drive a 10-horsepower turbine engine,
which would run a four kilowatt elec trical generator.
Power produced would be stored in a battery bank until
used in the new house or any outbuildings.
Duckett planned to r ep lace the gaso line ge nerator th at
he suppli ed with 60 to 80 ga ll o n s of fuel each month.
Duckett knew the reasons w hy this "o ld " technology
has decreased in popularity for home power ge nerat ion:
the difficulty of producing steam power at a steady pres-
sure; lack of inexpensive fu el to feed the boiler; and the
easy availa bility of inexpensive com m erc ia l power in
populated areas. The b a ttery storage components of hi s
design , coupled w ith the a bundance of driftwood in his
area, m a d e the steam boiler sys tem practical for Duckett's
particular situation, where eco n omical commercial
p ower was not really an option .
D es igning for direct current p ower, Duckett planne d
hi s system so that it would provide for a 500 kwh
m o nthly co nsumption for the h ouse. The boiler, it se lf ,
would b e use d to warm a b oath o u se, g iv in g Duckett a
heated work area .
Duckett's desig n for construction was, he said, simple
e n o ug h for any handy man to build , w ith readily avail-
a bl e materials. His plans called for a concr e te slab foun-
dation fo r the firebox , which was to b e built of standard
fireplace or barbeque brick (Duckett o rdered 532 of
them). The 20-to 40-gallon hot water tank would be
82
supported in the firebox . Driftwood would b e loaded
into the chamber thro u gh a n adequate-sized door made
of steel, heavy tin , or a n o ld wood furnace door. The flu e
could be made of a common e ig ht-in c h stove pipe, a five -
gallon bucket , or a n y large s tee l pipe th a t can accommo-
date a damper plate. The taller the flue , the better it w ill
draw to increase burning eff ic ien cy. Duckett 's plans were
not dimension-critical and ca n be used for a hot water
tank of a n y size of choice.
All the controls for the system are to be mounted o ut-
side of the water tank; Duckett plans to install a safe ty
relief va lve, a pressure ga u ge, and a ga u ge to
monitor the system. H e also plans a safety relief and
blow-off va lves to the piping connected to the eng in e; a
manual water load valve , a water shutoff val ve, and a
check va lve to the pump.
The steam w ill ru n the 10-horsepower, E-7 turb in e
Duckett bou ght from Steam Power Products, alo n g with
co ntro ls, pump a n d re g ulator equipment. H e a lso will
u se Surrette 308 amp-ho ur batteries and / or RCA bat-
teries and a four kilowatt generator.
Problems
Duckett was awarded his AT grant in 1980, and by
1983 he was still trying to complete both hi s house and
the boiler project.
Hi s troubles began w it h the w in ter after he received
the gran t . Duckett sti ll was waiting for required de sig n
appr oval by the state Boiler and Pressure Vesse l Inspec-
tor 's Office in Anchorage. With out state a pprova l,
Duckett could not order the materials he required.
By March , he had begun pl acing his equipment orders;
shortly after, a sh ipping strike delayed delivery of the
m ateri a ls he n eeded to proceed. During the process of
building his home and boiler sys tem, Ducke tt also h ad to
move b ack to Ke tc hikan for a period , a nd accepted
employment w hi ch fr equen tl y took him away from
home .
By early 1982, Duckett h ad set the pilings and scaf-
fold in g in place for t he water tank, and the house h ad
been framed. The area in side the boathouse was cleaned
a nd excavated in preparation fo r construct ion of the
foundation for the firebox and boiler. Duckett at thi s
time a lso followed advice to redesign the project for a
12-volt sys te m i n stead of the 115-volt system he
envisio ned.
As of mid-1984 Ducket t planned to in ves t a n es tim a ted
120 h o urs to complete hi s h ome a nd boiler system ; a ll
materials a nd equipment wer e on site and he was a n xious
to move into hi s new home .
Funding
U.S. D e pt. of Energy
State o f Alaska
Grant Recipient
Kenneth Duckett
P.O. Box 3178
Ketchikan, Alaska 99901
$4,169
4,169
•
A view of the shop building where t he steam engine will be located .
83
Fishing boat to be
powered by steam engine
Michael Broili hopes to install a steam engine on a
commercial fishing boat.
So far, preliminary studies indicate that a 10-horse-
power steam engine can power a 30-foot boat and gener-
ate enough electricity for operating radios and hydraulic
systems aboard the vessel.
"I wanted to find out if the steam engines would be
more efficient and effective than internal combustion
engines;' said Broili, marketing and art director for the
Alaska Fisheries Development Foundation in Anchorage .
'The steam engines are pretty reliable and pretty easy to
repair'.'
Major drawbacks are that the steam engine requires a
lot of observation while in operation, and it takes awhile
to fire up the engine.
The advantages of steam engines for commercial fish-
ing operators, who have been hit hard by rising petro-
leum costs, is a potential measurable reduction in energy
costs.
Usable steam boiler fuels include wood (wood, chips
or sawdust); coal (chunks, stoker-quality or liquified );
waste and crude oil; gas; peat; paper and cardboard .
Broili , who has worked in almost every aspect of the
fishing industry, plans to build a boat for the steam
engine .
System Design
Broili planned to use a boiler and an engine
specifically designed for marine use . The particular
system he selected, which cost about $7,000 , has been in
use for more than 100 years.
To test his idea, Broili bought a 10 horsepower, twin-
cy linder Semple engine which can operate at 400-600
rpms.
84
He also acquired a steel-plated boiler, which weighs
about 650 pounds, is six feet tall and measures 3.5 feet in
circumference. The boiler sits atop a two-foot-square
firebox.
Steam produced in the boiler is piped into the engine,
where it pushes the pistons up and down . One piston is
larger than the other because the exhaust steam from the
smaller piston is fed to the larger piston to extract as
much energy out of the steam as possible. The pistons
are connected to a crankshaft (like an automobile engine )
which turns the vessel's propeller.
Belts connected to the drive shaft also spin a separate,
12-volt alternator. Electricity generated by the alternator
is stored in a 12-volt, deep-cycle , marine battery.
Performance
Broili says he's confident that the steam engine can
produce enough power to propel a fishing vessel and
generate electricity for on-board radios and hydraulic
equipment.
And Broili said he did not ex perience any malfunc-
tions or equipment failures during test runs of the
engine.
"We think that it could power the boat, and auxiliary
equipment and radios;' Broili said. "Hopefully, down the
line, it's our intention to install it in a boat'.'
Funding
U.S . Department of Energy
State of Alaska
Grant Recipient
Michael Broili
3011 Lois Drive
Anchorage, Alaska 99503
$5 ,070
5,070
Mike Broili's steam engine (left) awaits hookup to a bo il er.
Outdoor furnace
heats home
Wilbur LaPage has slashed his oil consumption in half
by building an o utdoor furnac e to heat hi s Southcentral
Alaskan home .
The novel project is called a Heating and Heat Storage
Apparatus (HAHSA) by the manufacturer. It's a concrete
block outdoor furnace tha t burns wood, trash and coal
in a large combustion chamber.
Water heated in the furnace is piped b a ck to the house
fo r hot water and baseboard heating.
"The completed furnace works very well;' says
LaPage, a retired parks and recreation employee for
Anchorage w ho li ves on a 14-acre wooded lot in Ea gle
River.
"Last winter I don't believe I burned more than a cord
and a half of wood all winter. But I also burned paper,
boxes and other burnable material. And I can hold the
furnace heat at approximately 180 degrees for 48 hours:'
LaPage, who spent three years building the furnace,
says he's been pleased with its performance . He said he
purchased the HAHSA system from a Pennsylvania
manufacturer after he saw an advertisement about it in a
magazine .
The biggest problem he still faces , however, is getting
rid of creosote build-up in the furnace's chimney. He has
to clean it about every three months.
"If we lick that I think we'll have it made;' he said.
"When the chimney's clean , it works beautifully. It's an
economical system . We 've cut our oil consumption by
more than 40 percent :'
85
System Design
The outdoor furnace is about 10 feet wide, 12 feet
long and 8 feet high. It is h o used in a mini-building that
resembles a large wellhouse . The chimney stack is about
10 feet high to maintain a good draft in the firebox .
The concrete block furnace has three inner walls, so
that it resembles three boxes placed inside of each other.
A firebox with fire brick is the heart of the furnace. It
is encased by 21 tons of sand and crushed rock . About
200 feet of plas tic pipe are buried in the sand. The sand
absorbs the heat , which in turn, heats water circulating
through the buried plastic tubes.
The sand is encased by a concrete wall, a layer of
styrofoam and an outer shell of concrete block .
Water circulates constantly between LaPage's home
a nd the outdoor furnace throu gh two separate plastic
PVC pipes. One is a lfz -inch-diameter domestic hot
water pipe, and the other is a 3/4 -inch-diameter pipe for
baseboard heating. Both lines are encased in a wood box
insulated with styrofoam and covered with Visqueen.
Performance
LaPage says he's been pleased with the HAHSA
heating system .
Two drawbacks, however, entail creosote buildup in
the chimney, and heating water in the plastic pipes.
"Extreme accumulation of creosote occurs in the chim-
ney and the firebox ;' LaPage said. 'This is one good
reason for having the unit separate from the house. The
T he HA H SA (above left) is lo cated n ea r to t he h ous e it heats.
(A bove right), Wi lb ur La Page exp lai ns th e tie-in w ith t he
boiler.
system is designed to allow for the heavy creosote build-
up, but it does have to be burned out or w ire-brushed
out of the chimney a few times through the w inter:'
LaPage also says his plastic pipes are not as good as
copper pipes. He said the water could heat faster if it
were circulated through copper pipes.
"Plastic pipe doesn't pick up heat as quickly as copper
pipe;' he said. "If I did it over, I would recommend that
they pick up the copper and forget the plastic. I think it
would be worth the additional cost :'
Tips
LaPage suggested several ways to improve his outdoor
heating system:
LaPage shows off his roo t cellar
86
• Use copper pipe in the HAHSA rather than PVC
plastic pipe to heat the water faster. [Ed. note: This
may not be economically advantageous.)
• Reduce construction costs by doing as much of the
labor by yourself.
Funding
U.S. Department of Energy
State of Alaska
Grant Recipient
Wilbur LaPage
P.O. Box 1111
Mile 3.5 Old Eagle River Road
Eagle River, Alaska 99577
$2,290
2,290
. '
. '
Novel system provides
heat and hot water
A so-called heating and storage apparatus is both a
furnace and a heat storage system, located outside and
away from the home .
In Alaska, where many homes are far from fire protec-
tion services, this type of heating system not only
reduces chances of burning down your hor;ne, it also
provides a more efficient heating system than the vener-
able wood stove. And, because the apparatus is
so large, it can supply domestic hot water at the same
time it heats your home.
Pat Yourkowski was preparing to build a large,
2,500-square-foot home in Homer and was looking for
ways to minimize his reliance on fossil fuels and electri-
city. His new house would be located on a hillside about
18 miles from town , overlooking Kachemak Bay and the
Lower Cook Inlet. This area is known for butter and
razor clams, good fishing and exposed coal seams on the
bluffs lining the inlet and bay. In fact, at one time in the
1800s, Homer was a coaling station for the Russian and
American Naval and merchant fleets serving the north-
ern Pacific. Beach coal has been traditionally used to heat
the homes in the area and even today is free for the
picking .
Yourkowski figured he could use this local coal and
some of the tons of driftwood washed up on the same
beaches to fire his furnace and heat his home; a couple of
hard-working weekends at the beach could supply
enough fuel for the entire year.
Pat's new home would be superinsulated with double
exterior walls and insulated interior walls and floors .
Yourkowski planned to isolate each room and use a
system of controls and valves to regulate heat on an indi-
vidual room basis. For instance, if an upstairs room was
not being used, the heat to that room would be turned
down to a minimum. Through interior insulation, heat
creep to that room will be minimized , leaving more heat
available to the rest of the house without increasing the
heat transfer from the system. Pat figured that this design
could extend the heat reserve of the system enough to
allow weekend winter jaunts without the fear of frozen
pipes or house plants.
Design
An apparatus such as this is characterized by its large
firebox and massive thermal heat si nk-20 tons of sand
in Yourkowski's case . Using a controlled burning envi-
ronment, it should be possible to stoke this device only
o nce or twice a day on the coldest days. Another charac-
teristic of a heating /storage system is its ability to burn
multiple fuels simultaneously. Coal, wood, paper,
almost anything combustible can be tossed into the fire-
box. Explosives (pe troleum-based products are consid-
ered explosive ) and items that give off toxic fumes should
not be burned for obvious reasons. The heat stored in the
massive heat sink of the structure will maintain its tem-
perature for up to three days without additional heat
input. Yourkowski planned to design a firebox that
would burn multiple fuels without the common draw-
87
backs associated with airtight wood stoves and coal fur-
naces. These include over consumption or waste, the
need for constant attention, and a constant danger of
overheating .
In Yourkowski's design the heat output would be con-
ducted to the house through buried, heavily insulated
pipes and transferred to individual rooms via standard
baseboard heat exchangers (radiators). Using a combina-
tion of sound engineering and good insulation, Your-
kowski figured he could heat his 2,500-square-foot house
(for three to five days) with only one stoking of fuel
(wood or coal, or both). This remains to be demonstrated .
In order to take advantage of the earth's natural insula-
tion, about 75% of the system is to be placed below
ground level. A 12-foot-deep area was to be dug from the
hillside below the house . A concrete slab, eight by ten
feet by four inches, was poured for the foundation . On
top of this foundation will be a concrete block firebox of
three by eight feet. The firebox will be set flush on the
front of the foundation and centered laterally. Firebrick
will be attached to the inner walls and a piece of one-
quarter-inch three-by-eight steel plate will cover the top.
The steel will protect both the heat sink and the heat
transfer pipes from the hottest part of the firebox and
help conduct the heat to all areas of the heat sink.
A large metal stove door will be attached to the front
and a chimney in the rear of the unit will complete the
firebox.
The thermal heat sink and heat transfer tubing go
between the inner and outer walls of the structure. Two
types of pipes will be used to transfer the heat; copper
where the heat is the greatest and PVC where tempera-
tures are much lower. The use of the two types of tubing
was based on economics . In the sides of the heat sink,
temperatures would never be greater than 180 degrees,
well below the performance characteristics used above
the steel plate , where temperatures are hottest.
A cross-grid of PVC pipe will be placed vertically
approximately eight inches from the firebox on each side
and along the rear of the heat sink. Fine sand will be
tamped around the piping for support and heat transfer.
The PVC grid will be connected so that water can flow
into the pipe , through the entire grid, and then out. The
PVC grids will be in turn connected to the copper pipe
placed above the firebox .
The copper pipe will be installed horizontally on top
of a one-inch layer of sand on the steel plate. Once the
plumbing connecting this grid to the PVC grid is in place
and pressure-tested, the rest of the 20 tons of sand will be
added . The entire structure will then be covered with an
insulated roof .
A small pump will be used to circulate the water
through the thermal mass to the house system and back.
Air flow to the firebox will be controlled by an old g as
tank modified to regulate and preheat outside air before
it enters the fire area . Two hoses will be attached to the
gas tank. One draws in outside air to be preheated. The
other regulates the a mount of preheated air allowed to
enter the fi rebox. This regulator I pre heater is designed to
extract every last ca lorie of available heat from the fuel.
Problems and Conclusions
A lthough Yourkowski has star ted both the house and
heating /heat storage apparatus, personal problems have
caused a considerable delay in completion.
During the course of const ruction, Yourkowski decided
for econ omy's sake not to bury the insulated water
delivery /return pipes. These pipes will now be
supported above ground between the furnace and the
house. Because the project is not finis h ed, other modifi-
88
cations may be made in the future .
Since this type of heating and heat storage device has
prove n it self in other northern applications, it seems
probable that once Yourkowski finishes his syste m he
will have an effective, econ omical heat source fo r hi s new
house .
Funding
U.S. Department of Energy $3,081
Grant Recipient
Patrick Yourkowski
Box 2136
H o mer, Alaska 99603
Winter in Alas ka (/eft) often slows construction. Th e unique
s ton e arch is constructed of riv er rock (above).
Windpower supplements
local utility
Kivalina is located some 80 miles northwest of Kotze-
bue on a sandspit that at its highest point is only 10 feet
a bove sea level. The town is bordered on its southeastern
side by the mouth of the Wulik River; it is bordered on
its western side by the Chukchi Sea, and to the north-
northeast, K ivalina is bordered by a shallow lagoon.
Transportation to and from Kivalina is limited to air
travel, small, locally-made boats, and snowmachines.
During the summer, transportation to and from hunting
camps is via many of the r ivers located around Ki v alina .
Because Kivalina sits north of the Arctic Circle and on
the coast just south of the protective shield of the Brooks
Range, the temperature seldom falls below minus 40
degrees for very long .
Kivalina's temperatures range in the winter from minus
30 degrees to minus 50 degrees, generally staying around
minus 10 to minus 30 degrees. During the summer, the
temperature stays around 50 to 65 degrees with a few
weeks when the temperatures range from 75 to 90
degrees .
Wind is a daily routine for Kivalina. Usually, wind
speeds are aro und 15 to 30 mph, but once or twice a
y ear, there is a big blow with winds up to 65 and 75 mph.
Under its AT grant, the Northwest Arctic School
District used wind p o wer to augment local utility power.
Kivalina's windpower plant is a simple direct intertie
system with the utility . T he district is utiliz ing a n Ener-
tech four-kilowatt synchronous system that is hooked up
directly into a circuit breaker panel.
89
Construction
The construction and installation phase of this project
turned out to be the toughest and the most time-consum-
ing aspect of the whole operation. This was due to a lack
of ex perience with tower construction, a lack of consis-
tent workers, and weather.
The project was initiated in 1979, when the school's
science teacher reflected about the local wind conditions
and applied for an energy grant in hopes of constructing
a sy stem to harness the winds-to convert the wind's
energy into electricity that would power a greenhouse
where fruit and vegetables would be raised for local
consumption .
When the new principal and science teacher arrived in
1980, the tower sections, guy wire, tower parts, dead-
man beams, plates and accessories for raising the tower
and g uy wire warning tubes were on-site .
In order to complete the project, the tower base needed
to be dug in place, one last dead-man trench needed to
be dug; and the tower raised . Further, a generator needed
to be ordered to replace the proposed wind system that
was made by the Dakota Wind company, which had
gone out of business .
Student help accomplished a good part of early stages
of t he project.
David Aldrich, who guided the project along, de-
scribed the work in detail:
"First , w e s tarted digging an ei ght-foot-deep hole to
accommodate the tower base beam. This beam, an eight-
Th e h eig ht of wind power s u ccess in Kivalina.
jl
foot by 12-inch by 12-inch timber, was to be buried
except for about one foot, which would stick out above
ground level.
"I t was necessary to dig prior to the cold months of the
year; the ground starts to freeze towards the middle of
October," said Aldrich.
"We went out every day and spent 45 minutes digging
the sandy ground. It was slow work. The ground was
hard. As we dug, the sides of the hole caved in; thus, we
ended up with a wide hole that needed shoring up to
prevent the hole from being filled up.
"When we got down to the six-foot mark, we struck
water. We dug out another two feet of ground while
standing in cold muddy water. We finally set the tower
base beam into the hole and poured concrete , sand, and
gravel around the beam to steady and strengthen our
base. But before we could raise the tower, we had to dig
one more dead-man hole. Winter had started, as had the
cold winds and snows that accompany it. It wasn't until
the late winter and early spring that we could get out and
dig the last dead-man hole .
"It was late September of 1982 before the complete
base and dead-man systems were in place. All that was
left to do was raise the tower," Aldrich said .
"We attempted to raise the tower in pieces. I bolted
to gether five of the six tower sections, secured a line to
the tower, passed the line to a nearby telephone pole, and
secured the line on the other end to the town's bulldozer.
To make a long story short, the tower was on its way up
when the bottom kicked out causing the tower to fall and
bending four of the five sections.
"We repaired three of the sections . One section was
Wind generator
impresses villagers
Building a wind generator in a small Eskimo village on
the Bering Sea coast can be a turbulent undertaking.
Just ask the students in Karl Lund's advanced science
class in Hooper Bay.
Every step of the way-from acquiring the wind gen-
erator to installing it-they encountered one problem
after another. But despite the setbacks, they successfully
completed the project.
And for a year, the generator produced electricity for
the local health center. A videotape of the project also
was produced by KYUK and is available in the state film
library.
"On September 29 , 1982, the school celebrated the
10,000th kilowatt hour of production by consuming a
commemorative cake made by the home economics
class;' said Lund . 'The city of Hooper Bay was so
impressed with the performance that they purchased a
Jacob's (wind generator) for use on their city building:'
But then another setback occurred .
The regional school board, headquartered more than
100 miles from Hooper Bay, voted to shut down the wind
90
beyond repair. It looked as if the tower wasn't goi ng to
be raised . But the manufacturer, Enertech, had changed
the tower design , requiring a stronger section to be in-
stalled. Following the arrival of the last elements of the
wind system was much-needed technical help in the form
of tools and technical ability; that winter we raised the
tower and secured the generator on top using a gin pole:;
said Aldrich of the final step.
Because the generator is synchronous, it relies on
proper voltage from the utility power. Alaska Village
Electric Co-op (AVEC) provides the school electric
power, and the voltage from their system was only 180 to
206 volts at the school, which was not adequate to
operate the wind system, which requires 220 volts.
After a step-up transformer was installed, the sys tem
was fully operational by February 19, 1983.
Performance
The wind generator has been in operation now for
a year. It has produced up to 60 and 70 kwh worth of
electricity in a day, when the wind has blown 20 mph
for a full 24 hours. The system has worked as claimed .
The only modification required on the machine was
the addition of a foam -rubber pad along the bottom edge
of the generator access door. During operation, the door
would vibrate striking the bottom cowling piece and
creating a very noisy growl; the foam made the machine
a very quiet running machine .
Funding
U.S. Department of Energy $18 ,377
Grant Recipient
Northwest Arctic ,School District
McQueen School
Kivalina , Alaska 99750
generator for fear that children could be harmed if the
blades broke . The board, acting after the wind gener-
ator's blades had broken twice already, also ruled that
the generator be moved off school grounds .
"''m very sad about it;' Lund said. 'The regional board
is afraid of the liability factor in case a blade came off . I
didn't anticipate this . Otherwise, the students wouldn't
have gone to the trouble to do the project'.'
For the past year, the wind generator has not been
functioning because the project has not been moved to a
new location . The city is seeking funding to build a road
to a site where the wind generator can be safely operated .
But despite the setbacks, Lund is optimistic about the
project .
(Nex t page). Cement and parts (top left) are moved to the
tower site. (Middle left), a village tower raising. A student
(right) prepares the generator for hoisting. Studen ts (bottom)
calculate how to raise th eir tower.
II II
91
'We showed that this particular brand of wind gener-
ator can work in Hooper Bay:' Lund said. "And I think
eventuall y it will fly. Things in the Bush never grow at a
speed you wish they would. But I think eventually it will
accomplish its goal :'
D esign
The heart of the system is a 10-kilowatt Jacobs wi nd
generator, which has three, 11-foot-long blades. The
generator sits atop a 60-foot-high Rohn self-supporting
steel tower.
The three legs of the tower are each bolted to angle
iron set in two tons of cement. The cement surrounding
the angle iron was poured into drum barrels buried six
feet deep in the tundra. The bottom barrel of each
anchor was expanded into a bottom bell shape for addi-
tional strength.
'We didn't penetrate the permafrost:' said Lund . "It's on
top of a sand dune'.'
A 26-foot-high gin pole with two block and tackle
pulleys was used to hoist the tower upright. A second
14-foot-long gin p ole attached to the tower was used to
lift the 1 ,000-pound wind generator up to the top of the
tower.
'We had to do it by hand:' said Lund , adding that they
erected the tower between September and November of
1981 . 'We didn't do anything by machine . Probably a
third of the 200 students at the school helped pull the
tower up. And because it was a learning experience,
almost everything had to be done twice before it was
correct'.'
The wind ge nerator was intertied with the local electric
company, the Alaska Village Electric Cooperative, so
that none of the electricity was stored in batteries.
The power was used for a local public health commu-
nity clinic; su rplus power was fed to the utility free .
P roble m s
Delay in obtaining necessa ry equipment was the
biggest obstacle the students had to overcome .
In fact , there were problems almost every step of the
way. The tower was lost in delivery, cement and gravel
92
weren't available locally, and other nece ss ities were
shipped to the wrong village.
"Finally, everything looked good:' Lund said of the
progress at the time . "But wait ! United Transportation's
barge broke down unable to ship material to Hooper Bay.
Part of our tower and cement arrived in Hooper Bay via
Nome instead of Bethel. The other part o f our tower was
mistakenly shipped to the neighboring village of Chevak
and arrived in Hooper Bay via barge three days later:'
Pe rformance
The generator has performed well since its installation,
providing power for the community's health clinic. The
average windspeed has been 15 mph, but it has ranged as
high as 70 mph.
But six months after installation-and after producing
12,750 kwh -the governor in the wind generator broke,
causing the three blades to splinter. Apparently, the tail
hydraulic governing mechanism froze in the cold weather.
The blades were prevented from turning out of the high
winds to reduce the pressure on the blade .
The distributor, Four Winds, replaced t he governor
and installed shorter, 11-foot-long Sitka spruce blades
free of charge since the equipment was still under
warranty.
Unfortunately, the ge nerator froze again .
'There was another freeze-up:' Lund said. "We decided
to let the wind break it loose . We had a SO to 60 mph
wind and it broke it loose, but one of the blades hit the
tower.
'We're on our third se t of blades now;· sa id Lund ,
adding that the system "worked fine" and will do so
again when it's moved .
Funding
U.S. Department of Energy
State of Alaska
Grant Re cipient
Hooper Bay Hig h School
Karl Lund , science teacher
H ooper Bay, Alaska 99604
$12 ,385
12,785
Salmon hatchery
aided by windpower
Since May 18, 1982, the aquaculture class at Sand
Point High School doesn't have to worry about buying
electricity for their salmon hatchery-thanks to a new
wind generator they installed.
Power from the wind generator is used to heat and light
the school aquaculture facility and to operate a refrig-
erator, freezer and water heating unit in this small
community in Southwest Alaska . The community's 700
residents live on Shumagin Island, near the Aleutian
Chain .
"We feel that the windmill has saved the school district
a substantial amount of money in fuel savings ;' said
school superintendent Liz Boario, adding that they used
to rely on an oil furnace.
"In addition, the windmill has allowed us to heat water
for aquacultural purposes on a scale that would have
been prohibitively expensive under other circumstances;'
she say s . "After the windmill was fully operational, our
utility bills showed a tremendous dro p '.'
Design
The students installed a 10-kilowatt Ja cobs wind
ge nerator on a small rise above the hatchery. The gen-
erator is p o wered by three wooden blades, 23-fee t in di-
a meter, and sits atop a 60 -foot self-supp orting tower. An
anemometer and FAA warning lights are mounted on the
tower and the tower's three supporting le g s are attached
to concrete anchors .
Power from the wind generator is tied to both the
hatchery and the public utility system through a control
box. This box monitors the hatchery's usage and
93
compares it with the output from the generator. Excess
power from the generator is fed to the public utility
power grid; however, during periods when power output
from the wind generator is too low, the control box
supplies additional power from the public utility system .
Performance
The wind generator has performed well, providing
more than enough energy to meet the hatchery's needs .
The average windspeed during its operation has been 11
mph, with electrical consumption around 200 kwh each
month.
It was interesting to note that make-up power usually
was required if wind speeds dropped below 11 miles per
hour, while speeds above 11 miles per hour resulted in
excess power.
There has only been one minor problem with the
system. About six months after it became operational , a
defect caused one o f the propeller blades to crack . Jacob s
r esponded with an entirely new blade assembly designed
specifically f or the Alaskan environment and there were
no further problems .
They al so installed an improved sp ring-loa d ed tail
unit which turns the b lade a ssembly out of the w in d ,
w h ic h protect s it from wind damage .
Funding
U.S. Depar tmen t of Energy
State of Alaska
Grant Recipient
Sand Point School
Liz Boario
P.O. Box 132
Sand Point, Alaska 99661
$ 4 ,734
15 ,261
School district
harnesses wind
A wind generator is helping the Annette Island School
District in Southeast Alaska reduce its monthly electric
bills .
Each month, the generator produces about 1,250
kilowatt hours of energy, which is a $50 savings at
4 cents per kwh, says school superintendent Walt
Bromenschenkel .
"It's operating well;' says Bromenschenkel. "I t runs
whenever there's wind . The electricity is being fed into
the city system.
"Then, on a monthly basis, the number of kilowatt
hours generated is calculated and the district is compen-
sated for that by the city':
The generator was installed for the school district and
the Metlakatla Indian Community on Annette Island,
about 16 miles south of Ketchikan. The community,
founded as an Indian reservation in 1887, has a popula-
tion of 1 ,1 50 residents . It remains the only reservation
form of government in Alaska, after its residents opted
out of the landmark Alaska Native Claims Settlement
Act of 1971.
Originally, the community had planned to use the
wind generator for lighting and heating one of two green-
houses funded under this grant, and as an emergency
energy supply. Some of the power was to be tapped to
operate a satellite dish.
Those plans were abandoned during the three years it
took to get a wind system chosen a nd installed. As for
the greenhouses, a 100 mph wind storm destroyed one of
the greenhouses, and crippled the se cond one .
94
System Design
A 10-kwh, Jacobs-brand wind generator :with 12-foot-
long, laminated spruce blades was mounted at the top of
an 80-foot self-supporting Rohn tower. The system was
installed by Bill Breese, who represents Four Winds of
Alaska in Ketchikan.
The power system is intertied with the community's
electric utility.
One greenhouse was installed on a cement pad by the
high school and a second greenhouse was installed on a
concrete pad near the school superintendent's residence.
The identical greenhouses, both 14 feet by 40 feet ,
were purchased as kits. They used a metal frame with
double-paned plastic glazing on all sides down to the
ground.
Performance
The wind generator went into operation in July 1983
and has performed well. As of 1984, the greenhouses
remained inoperative.
'The only trouble we've had with the wind generator is
with releasing the brakes;' says Breese. "They get a little
corroded at times from our moisture and salt wind. I use
mercury anti-corrosion grease, and it works well;' he
said .
Funding
U.S . Department of Energy
State of Alaska
Grant Recipient
Metlakatla Indian Community
P.O. Box 458
Metlakatla, Alaska 99926
$16,783
16,783
Guard takes conservation
to the Bush
.M ~ ~ ~
In 1981, the Alaska National Guard launched a major
program to build wind generators and install wood stoves
at its bases in rural communities of Alaska .
The program was part of a statewide commitment to
finding economical solutions to the unique problems of
operating a remote and dispersed military r~adiness
program.
Today, the program has been largely abandoned by the
agency. Two state-funded wind generators have been dis-
mantled, and the wood stoves are being replaced with
the original oil-burning stoves.
The reason was the difficulty in ensuring ongoing
maintenance and operation of the systems in the Bush.
The problem is not an uncommon one in Alaska's rural
areas, where a majority of more than 200 villages live a
subsistence lifestyle. With unemployment in the Bush
averaging as high as 70%, residents in these remote areas
place a high priority on subsistence hunting, fishing and
gathering that has been passed down over many genera-
tions. To ensure an adequate food supply, residents must
be prepared when the resources become available .
And although many energy-conservation techniques
are straightforward and simple in their technology, it is
only in recent years that Bush residents have benefitted
from the increased economies of bringing technology to
a remote area that supports relatively few people.
"There is nothing wrong with the concept and there is
nothing wrong with the equipment;' said Maj. Roger R.
Patch, director of facilities management division for the
State Department of Military Affairs. But when some-
thing stopped working, residents would seldom call
Anchorage to let the Guard know. In the Guard's expe-
rience, "there is a lack of utility conservation in the
outlying areas . And there's nothing we can do here in
Anchorage that has been able to overcome that'.'
System Design
A significant part of the conservation program were
two wind generators funded by a grant. The Guard
hoped the generators would reduce the reliance on
expensive, diesel-generated electricity and show that
wind power was feasible.
The Guard first planned to construct a five-kilowatt
wind generator at Savoonga armory on St. Lawrence
Island, but the site was changed to Togiak , a more acces-
sible site. A smaller 1 .5 kilowatt Aeropower generator
was mounted on a 60-foot tower which was connected to
a control panel and battery bank.
Patch said he couldn't find anyone to tend the wind
ge nerator regularly at Togiak . The machine broke down
when it got out of balance, and the batteries were
destroyed when they froze .
The Guard also discovered that the batteries could
only supply power for a day or two, not a week or more
during periods of no wind as promised by Aeropower,
which has since gone bankrupt.
'The failures could have been corrected before we had
95
structural damage, but no one thought to call us;' Patch
said.
The failure prompted the guard to dismantle the wind
generator. A 1.5 kilowatt Enertech wind generator in
Bethel was also funded by a grant.
The agency hoped that a readily accessible site with
full-time personnel would allow the successful operation
of such wind power installations. Batteries also would
not be needed because the system was tied directly into
the Bethel Electric Utility.
Bethel, with a modern, regional airport and full-time
maintenance personnel at the armory, appeared to meet
those needs. The Guard also hoped that Bethel would
provide more visibility for the experiment, since the
community is the administrative, commercial and trans-
portation center for Western Alaska.
Again, n o one tended the wind generator. So the
Guard dismantled it.
Performance
Despite the lack of local support, Patch says initial
findings indicated that wind power is very feasible for
many of the state's rural co mmunities.
'The wind generator will work in the Bush and it's
economical;' Patch said . "''d go out there every six
months or so, and find nothing in operation . I'd fix it ,
and go back six months later and find the exact same
thing':
Problems encountered included governors which mal-
functioned, failure of personnel to rotate the generator
out of stormy high-speed winds, and batteries which
froze because storage buildings weren't heated.
"The problems they had were nothing that could not
have been overcome by routine observations of the user;'
Patch said .
Miscellaneous
Local maintenance support problems also compelled
the Guard to abandon several other experiments around
the state, although these were not part of the alternative
energy program .
The Guard, for ex ample , replaced oil space heaters
with wood stoves at Federal Scout armories operated by
the Guard at Arctic Village, Delta Junction , Hoonah,
Nulato, Shaktoolik, Saint Michael, Kaltag, Huslia, Elim,
Ambler, Kiana, Noatak, Noorvik, Selawik and
Shungnak.
To help stimulate the local economy, the Guard offered
to buy wood from local residents, paying up to $200 a
cord. The Guard said it was less expensive to burn wood,
rather than the average 3 ,000 gallons of oil consumed
annually at each facility. And the Guard found that at
some treeless coastal locations, driftwood accumulations
are adequate to meet heating needs.
But local residents generally did not want to spend the
time collecting wood to sell the Guard.
Consequently, oil stove heat is replacing the wood-
stoves.
Clivus type composting toilet systems also have been
installed at Selawik and Camp Carroll on Fort Richard-
son. And t he Guard has been adding insulation to all of
its older fac ili ties, and retrofitting its armories with
double-paned windows.
Furthermore, the Guard has made a complete change
from incandescent li ghting to flu orescen t lighting, and
high sodium fixtures have replaced fluorescen t lighting
at major armory drill halls. The new light in g is more
energy-efficient.
96
Funding
U.S. Department of Energy
State of Alaska
Grant Recipient
$15,070
15,070
A laska Department of M il itary Affairs
Facilitie s Management Division
P.O. Box 5-549
Fort Richardson, A laska 99505
Danes' experience adds
to local know-how
"We're proving that a lternative energy is not inacces-
sible to small towns:· said Steve Smiley at the christening
of Homer's first commercia l wind generator. Smiley, a
group of Danish visitors, and numerous Homer residents
had just finished building a n d in stalli ng a 10-kilowatt
wind generator on the H omer Spit.
The project began when Smiley, the grantee , met
Preben Maegaard, Chairman of the Danish Organiza-
tion for Renewable Energy, at Alaska's first A lternative
Energy Conference. After seein g Homer at Smiley's
request , Preben convinced Steve that it was possible to
build a small scale commercial wind generator in Homer
using local talent and materials.
Smi ley applied for and was awarded grant funds to
apply Danish know-how in Alaska. Denmark is one of
the most experienced nations in the use of moderate-size
(10 to 20 Kw) wind generators that are tied into local
commercial power grids.
Six Danish craftsmen were brought to Homer as part
of this project to help design, build and install a
10-kilowatt wind generator. The craftsmen a lso taught
and demonstrated t he Danish method for utilizing this
renewable ener gy source.
Although the visible result of the project would be the
operating wind generator, the overall purpose of the
project was to exchange information between the local
Homer residents and the Danes, to help demystify the
building process, and to prove that a wind generator
could be built with locally available materials and skills.
97
Design and Construction
An 11-kilowatt, 230-volt three-phase alternating
current induction motor driven by a three-bl aded pro-
peller, both built at the Cook Inlet Metal Works in
Homer, were used as the main components of the wind
generator . This unit was placed on a 40-foot-tall steel
tower (recycled from a crane boom) o n a concrete foun-
dation. Homer Spit was chosen as the project location
because it is highly visible.
The project was open for public review and education
programs, and also video-taped for future reference.
A number of local craftsmen, under the direction of
Smiley, also participated in the project.
Although the project initially proposed travel for four
Danes, six actually participated: Preben Maegaard, team
organi zer; Bendy Poulsen, blacksmith-engineer; Hans
Pedersen, e lectronics engineer; Birger Kuhn, wood-
worker; John Carlsson, mechanic; and Jacob Bugge ,
design engineer.
Homer residents provided lodging during their three
week stay, and the group fit well in this small fishing and
tourist town.
A few special items had to be ordered in advance from
elsewhere: a Swedish gear box, a German bearing ring, a
generator-motor, and wood for the propeller blades.
However, the mahogany plywood that was shipped by
air from Seattle was of inferior quality, and laminated
so lid mahogany was substituted for the blades.
The three tapered blades, which the Danish team
Th e preparat ions (l eft) for raising the wind generator near com-
pletio n (above). A v iew of Steve Smiley's former h ouse and
wind generator.
made in 10 days, feature stainless stee l yawl-li ke feath-
ering mechanisms that automatically slow rotation in
excessively high winds.
Most of the metal components used in the project were
either purchased locally or in Anchorage, or fabricated in
Homer machine shops. For example, the propeller shaft
braking mechanism was fabricated from a 1965 Chev-
ro let brake cylinder found in a Homer junk yard and
from a Datsun disk brake caliper donated by a local
resident.
Modifications and Performance
For a short time in 1980, the windmill produced
power, purchased by the Homer Electric Association
(HEA) at 1 V2 cents per kwh. The power at that time
entered the HEA grid through existing e lectri cal lines
connected to an a lternating current, three-phase induc-
tion e lectrical ge nerator .
Because the lease on the property on the Spit expired,
the sys tem was dismantled a n d put in storage until 1981 .
In 1982, the State of Alaska provided additional money
to have the generator system moved to p roperty Smiley
98
owned at Mile 12 East End Road near Homer. Smiley
sold his house on the adjacent lot in 1984, and by late
summer that year the idled sys tem lay partially dis-
mantled o n the site.
A single-phase Reliance IS-horsepower motor from
Debenham Electric had replaced the original 230-volt
three-phase unit. And although it was uncertain how
this would effect actual electrical output, the new con-
figurat ion did not see m to present a hook-up problem
with HEA.
Funding
U.S. Department of Energy
State of Alaska
Grant Recipient
Steven Smiley
SRA Box 41-C
Homer, Alaska 99603
$ 5,000
25 ,750
Generator hits rough
weather at sea
Jon Seager, hoping to reduce his dependence on diesel
fuel, designed a wind generator for his commercial
fishing boat.
And it worked we ll when the wind in the Bering Sea
did not exceed 30 mil es per hour.
Unfortunate ly, gusts of 40 an d 80 mph are fairly
common off the coasts near Platinum, a Native com-
munity located at the mouth of Goodnews Ba y and
named for a platinum m ine located nea rby. Some 53
people live in this windswept community in the south-
west corner of Alaska, about 130 mil es south of Bethel.
The average wind speed is about 16 mph .
"It's a heck of a good idea:' sa id Seager, a commercial
fi s her man and maintenance worker for the Pl a tinum
Sc hool. "Bu t when we'd get 40 to 80 kno ts of wind o n the
water I couldn't sto p the rpms from building up. And it'd
burn out a bearing'.'
Moreover, the w ind generator produced noisy vibra-
tions throughout the boat, which may have sca red some
fish off , Seager sa id .
'There was just n o way of shutting the system down;'
sa id Seager, who also has installed a Bergey 1 kw wind
ge nerator for his h ome. "It worked , b u t it didn't work
well enough. S o I to ok it down and put it away in the
shed '.'
Design and Construction
The design for Seager's wind generator was based o n
the common anemometer. Four, 18-inch diameter fiber-
g lass cups, each three-sixteenths of an inch thick, were
used to catch the wind.
WIND GENERATOR WITH BATTERIES
99
Seager bolted the unit atop a wood, two-by-two pole
behind the cabin on his 32-foot-long commercial fishing
b o at. The generator was seve n feet above the water line.
The vertical shaft wa s driven by the cups. The shaft
turned a 12-volt DC a lternator (sa lvaged from a
Cadillac) with a pulley and V-bel t. Elec t ricity from the
alternator was stored in a deep-cycle, 12-vo lt marine
battery. The power was used for lights, radios and other
equipment.
Performance
The system worked well at low wind speeds. But it
tended to spin o ut of control in high g usts. Also, the
generator produce d to o much vibra tion, which was not
good for gill net fi shing. Seager tried usi ng a tens ion bar
as a brake du r in g hi gh winds, but thi s did not work.
Seager recommends using the normal hori zo ntal wind
generator with wooden blades.
Unfortunately, he says a wind generato r with cups does
n ot function properl y in areas prone to periods of force-
ful wind.
"I would say it worked qu ite well around 30 mph ~
Seager said. "But ther e was just no way of shu tting it
down at higher speeds. The idea is super, but not on a
small fishing boat'.'
Funding
U.S. Department of Energy
State of Alaska
Grant Re cipient
Jo n W. Seager
General Delive ry
Platinum, Al aska 99651
5200
200
l
Wind power practical
in remote locati on
"Whew, it's up a nd working:'
Richard Logghe is attempting to harness some o f the
power in those strong gusty Southeastern Alaskan winds
to ge nera te all the electricity he needs at his remote
h o mestea d.
'The wind ge nerator is an in tegral part of our tota l
pl a n, which incl udes buildings bu ilt fr om sa lvaged
beach logs, an ice house for refrigerati on, wood heat , a n
attached solar g reenho use and a co mposting toilet:' says
Lo gg he .
Logghe, a ca rpenter and an electrician, lives with hi s
family in isolated Kasaan Bay, o n P rince of Wales Island .
He says it's a lot cheaper to produce power with wi nd
than rely on expensive diesel and kerosene .
"A wind energy co nversio n system is the best way to
meet ou r lighting and power needs without consuming
foss il fue ls and having a destructive impact on the
envi ro nm ent;' he sai d . "A wind system also is ea s ier
to main tai n and w ill la st longer than a gas or diesel
system. Wind power is practical, ecologically sound
and relatively inexpensive'.'
Syste m Design
Lo gghe p la n ned to put a 24-vo lt direct current,
Aeropower-brand wind ge n erator atop an 80-foo t-hig h
galvanized steel tower. The output of t he wind ge nerator
w ill b e fed to four, six-vo lt 500 amp/hour storage
b atteri es. The wind ge nerator is actually a
self exciti ng a lternator, much like those used in auto-
mobil es, but with all the internal components water-
p roofed to ensure trouble-free operation for long peri ods
of time. The three-phase output from the a lternator is
rectified for smooth input to the batteries.
The average monthly w ind speeds, which range
between 9 .3 and 4 .7 miles per hour, are sufficient to
generate electricity. Logghe says he expects to generate
between 250 and 400 kilowatt hours of electrical power
monthly. The power will be stored in the storage batteries
a nd used fo r both the house and workshop. A H o nda-
brand E0-1000 charging unit and a Sentry 2.5 ki lowat t,
120 volt alternating current generator will supplem ent
and back-up the wind ge nerator.
Construction and Problems
''We easil y put the first 20 feet of the tower up;· Logghe
sa id . "B ut we decided t h at it would be unsafe and very
difficult to bui ld the remaining 60 feet in place. We 'll
have a helicopter pick it up and lift it into place:· he noted
in one of his progress reports.
As of mid-1984, Logghe had experienced several
delays. These range from a fire that destroyed his
cabin-which he spent a year rebuilding-..:to back
problems and unexpected difficulties in obtaining the
right batteries and bolts.
As if Logghe didn't have enough p roblem s, when he
s tarted asking questions about hi s new wind generator,
he was to ld that Aeropower was no longer in business.
Other owners of the same system also informed him that
t he engineering seemed poor, especially with t he gover-
101
nor-blade system; the epoxy coating on the blades was
a lso said to be less than adequate . The blades, t hey said ,
will need recoating and therefore rebalancing.
However, his biggest p r oblem was trying to ge t a
helicopter to lift the rema ining 60 feet of tower. W he n
Logghe called Temsco for a helicopter, he found that t he
one he p lanned to use was out o n contract and wouldn't
be back for fou r months; the only other one avail able
would cost twice as much to rent .
"We gulped and choked a little;· said Joni Zimmerman,
w ho also was close to the project. 'Then Rich (Logghe )
talked to Ken Eichner, owner of Tem sco, and he said
they'd try to work something o ut when they already had
a helicopter in our area :· she said . This would cut the cost
considerably.
Knowing that a helicopter would be coming at some
time in the future, but not knowing when can be discon-
certing for some people. For Lo gghe, it meant that the
tower would have to be built on a level spot on the beach
a bove the tide line. In Southeast Alaska, this is quite a
chore in itself .
Fr iends from Ketchikan a nd Holli s, a litt le community
across the b ay, were supposed to help put the tower
toge ther, b u t ne ither could make it , so Logghe, Zimmer-
man, a nd th e rest of the fa m ily we n t to work o n their
own .
"I t was kind of interest in g to see the tower on the
beach ;' says Zimmerman, and "o ur little kids tightening
the bolts:'
The tower went together with only a fe w small
pro blems. Some of the leg braces required a little jogging
before they fit in to place, but within a short time the
tower was ready for the helicopter.
Ei chner to ld Logghe when he left that he would contact
him just before the heli copter arrived. Unfortunately, the
nois y, gas-powered washing machine was running when
the radio call was attempted.
"I was out hangi ng up laundry a nd I had even hung
some over the tower legs;' said Z immerman, "when I saw
a helicopter go ove rhead. A littl e while la te r we were
launc hing our skiff to go to Kasaan Vil la ge to pick up
our mail, when we saw another sma ll er helicopter com-
ing . lt swooped and landed'.' It was Eichner and hi s son
Dan , te llin g them that the big one was on its way.
T he Eichners prepared the tower, while Logghe a nd
Zimmerman panicked . They could see their friends from
Hollis, sailing over to help, but still about four miles
away.
"All of a sudden the big helicopter was here:' Zimmer-
man ran to move the kids away from the house windows
for safet y and to g rab the camera. By the time she found
it and snapped a few pictures, it was over. The tower was
up and the helicopter on its way home . As it left , their
friends from Hollis arrived.
A surveyor friend helped plum b the tower over the July
4th holiday and also he lped mount the generator. It took
two long days, using a g in pole with a rope to keep the
generator from banging the tower a nd a winch. Luckily,
everything went smoothly, and by the end of the week,
the generator was in stalled and wired to the control
panel. The following day a 20 mph w ind gave them more
power than they'd ever hoped for.
Performance
"We are really p leased wi th the performance of the
system so far;' says Logghe, "a lthough it has on ly been
running for a week and a half:' The 20 mph winds pro-
duced a consistent 20-to-40-amp charging current.
A lthough they can't run heavy shop tools and appli-
ances at the same time, the system is able to operate a
small automatic washer and dryer (both run on 110 volts
alternating current), and Logghe has already made
several pieces of furniture .
"We are thinking of ge tting a small electric hot water
heater and a fan for the wood shop;' says Logghe. "There
was some doubt on the part of a lot of people when we
were planning this project , but the performance of this
wind generator system has exceeded our hopes a nd
expectations. Our only problem so far is radio inter-
ference. We assu me that we can figure out something to
correct this':
102
Tips
Logghe offers this suggestion to both potential w ind
generator owners a nd wind engineers:
"It would be nice to h ave some frame of reference in
determining what ;excessive v ibration' is. Ours doesn't
seem to be vibrating much, but who knows':
Conclusion
'The delays were very frustrat in g, but seem to partly
be a result of trying to do a project of th is scope in a
remote location;' says Logghe. "Anytime w.e want one
more tool or piece of hardware~we can't just run to the
store. We must wait for our monthly trip to town, wh ich
usually takes a minimum of three days.
"Liv ing in such a remote location am idst modern
society is a true lesson in patience and perseverance;' he
said.
Funding
U.S. Department of Energy
State of A laska
Grant Recipient
Richard J. Logghe
General Delivery
Kasaan, Alaska 99950
$8,930
995
Floating wind generator
a partial success
Like most commercia l fishing vessels, The Lady
Simpson produces her own electrical power. About the
o nly time her generators are shut down is when she's
tied up in port, when power is supplied from the dock.
Ken Simpson, the owner/captain of The Lady Simpson,
figured that there might be a better and cheaper way to
supply some of that electrical power. Frank Simpson,
Ken's brother and a wind power specialist, offered to help
design a system that would use wind power to offset
some of the vessel's electrical needs.
Frank Simpson's project involved selecting a suitable
wind charger, constructing and installing a control box
and power transfer switch, and building the deep-cycle
battery bank.
Design and Construction
The design called for pl acin g a small , 24-watt, 14 volt
di rect current wi nd generator on top of the wheelhouse .
The output of the wind generator would be connected to
a co ntrol box and transfer switch in the wheelhouse and
the outp ut of the transfer switch would either go to the
deep-cycle emergency battery bank or t he vessel's ma in
battery ba nk. A co ntrol box would monitor the condi-
tion of the emergency batteries. Electrical power would
either be applied to the emergency batteries, or, if the
emergency batteries are fully charged, to the main
battery bank.
Unfortunately, The Lady Simpson sank in the Bering
Sea in November 1981. Ken Simpson soon had a second
Lady Simpson on the way a nd Frank's w ind generator
system was an integral part of its design.
The wind generator, a Model 24-14 Sencenbaugh, is
mounted over the wheelhouse atop a short piece of gal-
va nized pipe. The rigidly mounted system is p laced near
the left edge of the bridge (roof) to ensure th at it d id not
interfere with the radar and other communication
systems.
Frank used galvanized pipe to reduce salt water corro-
sio n effects. The wind generator was not given any addi-
tional protection because of its aluminum housing. The
sh ort, stro ng propeller b lades are a lso of aluminum.
The power output cables from the w ind ge nerato r are
run through the back of the wheelhouse to a control box
mounted on the rear wall . The power transfer switch and
battery charge monitoring devices are mounted inside
the control box.
The battery pack, because of its weight (more than 150
pounds) is mounted on the wheelhouse cabinet. These
batteries are able to supply 350 amp hours of power at 12
volts direc t current and consist of two, six-volt, deep-
cycle marine batteries connected in series.
Performance
The "floating wind generator" has proven partiall y suc-
cessful. It does provide more than enough power to keep
the emergency batteries fully charged and has on occa-
sio n been able to charge the main battery system. T he
emergency batteries are also away fr om any danger of
fire or explosion in the engine room. However, because
103
this is a new boat, some of the original design specifica-
tions have had to be modified. The new Lady Simpson is
a tender /crab boat and as such requires much more
power than t he little wind generator is able to produce.
Even when the vessel is in port, a small diesel generator
or shore-based power is needed.
Ken found that the power available from the deep-
cycle batteries was much greater than his main battery
bank . This prompted him to improve his main battery
bank and also connect the ship's radar and other impor-
tant systems to the emergency batteries.
Since no provisions were made to monitor fue l flow, it
is virtually impossible to accurately determine fuel
savings, if any. However, because the wind generato r
is used occasionally to supply power to both the emer-
gency and main battery banks, it can be assum ed that
some fuel savings does occur, h owever marginal. Frank
stressed that the main purpose o f the system was to
provide a safe, reliable power source for emergency
communications at sea and that fuel savings is not a n
importa nt part of this project.
Conclusions and Problems
Overall, the construction and in stallati o n of the
system does provide a safe, reliable power source for
emergen cy communications; h owever, it did not produce
the intere st the developers hoped for. Frank offered a few
ideas on thi s subject. He felt that if a method of moni-
toring fuel savi n gs was incorporated into the original
project, more interest would have been gen erated. Fish-
ing in Alaska is a high cost adventure and devices that
show no return on investment, even if they mean im-
proved emergency communication s, are la rgely ignored.
The size of the wind generator may a lso have some-
thing to do with the lack of interest. If the wind gen-
erator's output were increased to supply more power,
reducing the need for shore-based or ship generated
(die sel) power, the system's impact on th e fis hing
industry mi ght agai n be different . Unfortunately, since
this model wind genera tor is no longer manufactured, it
is hard to say if a larger uni t would improve interest.
Another problem that surfaced after The Lady
Simpson put to sea is that the w ind generator tend s to get
n oisy during high wind condition s. Ken Simpson is plan-
ning on either modifying the original mount with rubber
noise insulators, or moving t he wind genera tor to the
front of the boat.
Funding
U.S. Department of Energy
State of Alaska
Grantee
Frank Simpson
2005 East Third Ave. No. A
Anchorage, Alaska 99501
$498
498
Wind powered
telephone system
On the shores of a bay by the same name, Cold Bay is
226 miles southwest of Anchorage. It is the gateway to
Izembek National Wildlife Refuge and the world's largest
eel grass beds, where up to 50,000 lack brant geese (the
entire North American population) feed during their
annual migrations. Bracketed by volcanoes and on the
tip of the Alaska Peninsula, there's not much out here
except grass, brown bears, the brants, the sea and the
wind.
"There's alot of wind out here . It's usually blowing at
20 to 25 miles per hour about 80 percent of the time;' says
Frank Simpson, chief engineer for the Interior Telephone
Company. And Frank would know, because Cold Bay
is also the location of an Interior Telephone Company
communication facility.
This facility, in addition to serving the community
locally, is one of the few links Cold Bay has with the rest
of the world. The others are periodic plane flights from
Anchorage and periodic visits by the MV Tustumena, an
Alaska Marine Highway ferry.
A remote location, staging area for tourists visiting the
national refuge and the larger 3.5 million-acre Alaska
Peninsula Wildlife Refuge, Cold Bay is an ideal location
for a totally self-sufficient, wind-powered telephone
project, thought Frank Simpson, longtime proponent of
this renewable resource.
105
Design
Simpson originally chose a five-kilowatt, Australian-
made Dunlite windcharger; however, unexpected price
increases brought about by the strengthening dollar,
forced him to accept a two-kilowatt model, instead. This
caused a couple month's delay in the project right from
the start.
The smaller generator is mounted atop a 60-foot,
three-legged , galvanized steel tower. Diagonally criss-
crossed steel braces reinforce the tower's legs to with-
stand sudden wind gusts of up to 120 knots .
A three bladed, 11-foot diameter self-governoring
propeller assembly drives the generator. Stainless-steel
blades are used to prevent marine and environmental
corrosion, and because they are extremely strong.
The blades are mounted to an aluminum hub assem-
bly that has a special "s hock-absorber" unit to smooth
oscillations and a sliding governor. As wind increases,
the governor slides on a shaft and "feathers " the blades,
slowing down the generator. This action reduces strain
on both the generator and the tower.
The wind generator is a brushless, three-phase alter-
nator with a built-in rectifier assembly. The rectifiers
change the alternating current produced by the alter-
nator to a direct current usable by the control panel and
battery-bank.
Battery storage (above) is located in the Cold Bay te lephone
facility (/eft). The Dun lite wind generator is sit uated next to
the telephone building.
The output from the windcharger is fed down the
tower and into the telephone central office where it is
connected to a control panel. The control panel sends the
power to either the 120-volt direct current load, the 350
amp/hour battery bank, or to a six-kilowatt, 120-volt
alternating current inverter. The inverter changes the
direct current output from the battery bank or wind-
charger to 120 volt alternating current used b y the tele-
phone equipment. The battery bank has priority over the
power from the generator, however, and consumes the
entire output from the w indcharger if battery power falls
below 96 volt s.
Performance
Although this project was beset by problems in the
very beginning, Simpson believes that the wind generator
has worked beyond expectations. All the equipment
worked with the exception of the six-kilowatt inverter. A
design error caused the device to fail and required a new
one to be shipped from the Australian manufacturer
which took almost five months.
Frank Simpson added a low-voltage monitoring
switch to the original design to en sure that the inverter is
shut off w hen the battery-bank voltage is low. This
protects both the inverter and the telephone e quipment
and is a sound engineering practice .
106
The first four days of system operation were highly
successful; the windcharger generated at least 23
kilowatts of power over a four-day period and charged
the battery bank up to 110 volts. The voltage monitoring
switch is adjusted to shut down the inverter if the battery
bank voltage drops below 96 volts and to turn the system
back on when the battery charge reaches 120 volts.
Tips
Simpson says it's important to calculate-in advance-
the wind speeds and power requirements. Also, s horter
(11-foot ) blades are preferable in areas of high winds,
while longer, 12-foot blades do well in areas which do
not consistently have strong winds. The shorter blades
are less prone to stress damage in high-wind situations.
Funding
U.S. Department of Energy
State of A laska
Grant Recipient
Interior Telephone Company
Main Office
508 W. Sixth Avenue
Anchorage, Alaska 99501
$11,750
11,750
Teacher, students build
a wind generator
Two hundred miles southwest of Anchorage, on the
south shore of Lake Clark is Nondalton, a small village
of about 400 residents. Lake Clark is in the center of an
area noted for trophy fish and game, as well as incred-
ible scenery. Only the drone of the diesel generators and
the Native fishing boats break the serenity.
It was those noisy diesel generators and the rising cost
of the fuel that feeds t hem that first got John Norton,
local school teacher, to begin searching for alternative
ways to generate power. Although a large powerful wind
ge nerator could provide electricity for the entire area,
Norton was looking for a system that could be used by
si ngle households.
Soon after he began talking about his ideas, he found
that little knowledge existed in the village concerning
wind-powered elec trical generators. Rather than giving
up, Norton decided that it would be beneficial to con-
struct a small wind generator system with the help of
local high school students. It would introduce them
to alternative energy systems and, more important to
Norton, it would help teach the youths alternative ways
to so lve problems . Su ch a project would benefit the com-
munity by reducing electrical costs and contributing to
the educational program in the village .
In 1981 , Norton was granted AT funds for the selec-
tion, purchase and installation of a small wind ge nerator
system at the Nondalton School.
Design and Construction
Norton decided that the wind generator system should
be similar to one that could run a typical v illage home .
This way it would edu cate and demonstrate to the village
that wind generated electricity is a viable alternative to
petroleum-based power sources.
Norton began by researching weather records for the
previous 30 years a nd found that the wind averaged
between 8.3 and 14 .8 miles per hour. The windiest
month was January and the calmest, July. Next, he
searched for a wind generator that would operate within
these wind averages.
A Bergey 1000 48-volt direct current upwind generator
was chosen to generate electrical power at a low mini-
mum wind speed in the eight-mile-per-hour range; 12-
foot diameter blades are also automatically braked when
the wind exceeds about 30 miles per hour. This auto-
matic braking action is important in an area where
regular monitoring is impractical.
107
The wind generator was mounted on top of a 40-foot,
self-supporting tower next to the school building. The
generator output cables feed down through the tower to a
voltage regulator and a battery bank composed of 20 six-
volt, deep cycle batteries connected in series and parallel.
The series and parallel arrangement of the batteries was
planned to ensure a constant voltage under varying
loads.
The batteries also are connected to an inverter, which
can change the 12-volt direct current battery voltage to
120 volts of alternating current. This allows standard
household appliances to be used without modification.
The relative condition of the system is monitored by a
metering system consisting of a microamp meter, a direct
current voltage meter, and an alternating current voltage
meter. These effectively tell the condition of the batteries,
the output of the wind generator, and the output of the
power inverter.
Performance
Unfortunately, before Norton could finish with the
project he left Nondalton. Although the wind generator
and tower were erected, not much else was done imme-
diately. The batteries for the battery-bank were never
charged and were stored over the winter in an unheated
building. By spring the cases were ruptured and the
batteries useless.
A strong wind shortly after Norton left also caused
problems. The automatic brake mechanism failed, caus-
ing ex pensive damage to the internal components of the
generator. The blade has since been removed and placed
in s torage.
As of mid-1984 , the project has been mothballed,
although the sch ool district is considering restarting the
project.
Funding
U.S. Department of Energy
State of Alaska
Grantee
$3,660
8 ,540
Lake and Peninsula School District
Nondalton High School
Nondalton, Alaska 99640
Students learn from
wind project
About 450 miles due west of Anchorage, where the
Eek River meets the Kuskokwim and both meet the Ber-
ing Sea, is the small Yupik Eskimo village of Eek, popu-
lation 200. The wind blows constantly here, a scant six
miles of open tundra from the sea. Even on calm days,
the wind averages almost 10 miles per hour and the flat
delta offers little terrain to stop it.
In remote villages such as Eek, subsistence hunting
and fishin g remain as a cultural lifestyle a nd economic
necessity. And in many cases, low-cost fuel is a thing of
the past.
Harnessing wind power is not a new idea for Eek.
Between 1930 and 1960, there were three or four wind
generators operating. This was before the village power
plant operated by the Alaska Village Electric Coopera-
tive was installed. The wind generators faded from the
Eek skyline soon after the diesels arrived.
Eek is in an area of Alaska that offers little oppor-
tunities for the younger citizens. Tom Mcintyre and the
Lower Kuskokwim School District were determined to
change part of that.
The Lower Kuskokwim School District is one of 21
Rural Education Attendance Areas (R EAAs) in Alaska.
(The Northwest Arctic and Lake and Peninsula School
Districts' experiences with their projects also are
described in this book.) The REAAs were formed in
1974, to allow local control of education and to even-
tually take over rural education responsi bilities from the
federal Bureau of Indian Affairs. Increasingly in recent
years, these REAA s have recognized the value of voca-
/I
108
tiona! education in assisting students in mak:ing a
smooth transition to rapid changes in Alaska; Native
culture and language programs also are common, as we ll.
The district figured that having the vocational
students construct and operate a small wind ge nerator
would teach practical, new skills with a locally available
energ y source. The project also was co n ceived as part of
a visible symbol of what can be done when a village
cooperates together.
The 1980 gra n t project involved selecting the wind
generator and support tower, voltage re gulator and
battery-bank, back-up generator system, and developing
a record keeping system to monitor the results of the
project. Throughout the course of development, the
education of the students would be kept in the forefront.
Design and Construction
Shortly after the project began, the village was
informed that the old school was being replaced with a
new building . It wa s decided to mount the wind gener-
ator on the roof of the Traditional Council building
instead of the school and to move it when the new school
was completed. The w ind generator chosen had to have
the following qualities; it had to be able to withstand
extreme cold, hi g h winds, a salty environment, and it
had to be affordable. A WIN CO 1222 wind generator
a nd su pport tower was chosen because it was thought to
match the se parameters and was readily available.
The output tower cables from the roof-mounted wind
system are connected through a voltage re g ulator to two
T-16 , six-volt batteries connected in series. The wind gen-
The Council building (above left) w here the wind generator is
mounted. A v iew of the village of Eek (above right).
erator is manufactured so that its propeller blades must
be manually braked when the wind velocity is too high
(around 30 miles per hour). With the tower a lso designed
to keep the generator from turning a full 360 degrees, the
system se emed suitable for the type of wind conditions
found in Eek.
The battery output is connected to a 120-volt a lter-
na ting current inverter which changes the 12-volt direct
current to the standard 120-volt alternating current used
by most modern appliances and televisions.
A small , gasoline powered, 120-volt AC 440 watt gen-
erator is used to keep the batteries charged during long
periods of no wind, or in high wind when the wind gen-
erator is shut down.
Performance
The WIN CO operated without any major problems
until the late fall of 1982 , w hen a storm slammed into the
coast with 70 mph winds. The wind generator's brake
malfunctioned a nd within seconds the propeller blades
were splintered. Luckily, the local television s tati on,
KYUK-TV in Bethel, had already featured a story about
the windmill at Eek and how the proud students had per-
formed the major work on the project. The generator
s tands idle today because the village lacks the funds to
replace the d a maged parts.
109
While it ran, the wind generator lived up to its original
design parameters. It operated during the first winter,
spring, and summer without a flaw. The second part of
the project w as also successfu l. The students were
instructed on construction and operating techniques,
wind system monitoring, and project management.
Conclusions and Problems
The only major problem encountered with this project
was the failure of the wind generator during the s torm.
The other problems were relatively minor and typical of
rural areas.
Coordinating skilled craftsmen with class room hours
was difficult, especially when the craftsmen were due at
another project. Over time, however, the system was
completed.
Funding
U.S. Department of Energy
State of Alaska
Grantee
$4 ,500
$4,500
Lower Kuskokwim School District
Eek High School
Eek , Alaska 99578
0
Windmill pumps
hatchery water
"The aquaculture industry should set an example of
utilizing pollution-free techniques and work toward
energy se lf-sufficiency since its we lfare and production
depends largely upon clean water. Simple economics
makes energy self-sufficiency a necessary reality," says
Jack M. VanHyning, aquaculturist and president of
Nerka, Inc. a nonprofit private fish hatchery located on
remote Perry Island in Prince William Sound.
VanHynin g believes that the periodic peaks and dips
in sa lmon production can be moderated by farming
salmon much like cattle ranchers farm beef in the
wes tern states. The same problems are common to both
industries' e nergy cos ts and water.
One major problem facing salmon hatcheries in gen -
eral is the a b ility to supply a constant flow of clean , clear
wa ter over eggs and youn g fry. Periodic flushes with
seawater also a re necessary. In a remote s ubarctic
location w ithout access to a year-round clear stream ,
supplying this water is ex tremely difficult and expensive.
Van Hyning has initiated a method that may reduce both
dependence o n petroleum-based fuels and possibly
eliminate the need for a year-round fast flowing stream.
Hi s a nswer is wind pumps.
Phil osophi cally, VanHyning chose wind e n ergy
because it 's a renewable resource that can be used to
inc rease a ren ewa ble biological resource (salmon ). It a lso
helps conserve a non-renewable resource (oil ). In add i-
ti o n , wind pumps are easy to install a nd require minimal
maintenance and training to operate.
Van H yning's 1980 gran t was to research and develop a
wind powered water s upply system for the Perry Island
sa lmo n hatchery. The p roject invo lved researching avail-
able li terature and consulting wind energy experts ,
studying wind patterns at Perry Island, purchasing a
suitable wind pump as a result of the research, field
testing the system, a nd publishing the results of the
project.
Design and Construction
The operational requirements for the Perry Island
h a tchery would be similar to those of o ther remo te l oca-
tions in Prin ce Will ia m Sound. Bo th seawater a nd fres h
water would have to be transported from a low water site
up to the hatchery. The seawater would be ne eded o n a
daily basis for about two hours per day. Fresh water
woul d need to be pumped in an "on demand" si tua tion,
usually w hen the flow from the fresh water stream dried
up or lowered during w inter. The fresh water would have
to be delivered at a rate fast enough to compensate for the
reduced stream flow. In each case , the need to replace
standard petroleum-based energy sources would be
necessary to make the h atcher y economical.
After consultation and research, Nerka, Inc. decided
t hat a sm all Savonious rotor windmill connected to a
diaphragm pump would be sufficient for pumping the
seawater to the h atchery. A Dempster w indmilL like the
ones dotting the American West, would be used to
supply fresh water. Each of these pumps were chosen
111
WINDMILL , WATER PUMPING
because they promised simplicity, low maintenance, and
ease of operation.
Seawater is added once per day to the hatchery trays to
reduce fungus infestations and, being several degrees
warmer than fresh water, to enhance growth and produc-
tion. Because the seawater is not needed in large
quantities, the simple Savonious windpump was chosen
for this purpose. The Savonious windpump was con-
structed in Fairbanks from two halves of a 55-gallon
drum. Initial tests indicated that it functioned well; how-
ever, when it was moved to Perry Island and attached
to a diaphragm pump, the results were marginal at best .
A piston pump substituted for the diaphragm pump
helped a little, b u t only d uring a high tide and high wind
combination.
The water transfer lines for this pump were flexible one
inch pipes, one extending down to the mid-water line on
the beach and another to the hatchery trays 10 feet above
the pump. Calculations showed that this combination
with a submersible diaphragm bilge pump would
produce an output of about four gall o ns per minute with
a 10 mph wind.
A traditional farm-type, multibladed D empster wind-
mill would supply the fresh water. This windpump was
chosen because of availability of parts, minimal main-
tenance, reputation for durability, automatic "furl-out"
for high winds, manual braking, docume nted pumping
rates and ease of interface with a mechanical pump for
windless period s. After attending a seminar at New
Mexico State University on installation and operation of
this type of system, Van H y ning purchased o ne and
m oved it to the hatcher y site. In a ddition to the 10-foot-
diameter wind p u mp, a 35-foot tower and six-inch brass
we ll pump were ordered.
The final location of the Dempster was a compromise.
The poor performance of the Savonious and low wind
measurements co nvi nced the builders that another
location sho uld be us ed. It was decided to move the
tower and windmill to pilin gs in the fresh water reservoir
near the hatchery. Construction was as easy as "putting
up an erec tor se t ;' according to VanHyning . Anemom-
eter measurements taken earlier indicated that adequate
wind existed in t his new location to pump sufficient
water for the hatchery needs. A two-inch pipe carried the
water from the windpump to the hatchery.
Unfortunately, during shipp ing, the wind vane was
los t. Creative cutting of some old scrap me tal rectified
this situatio n and by the spring of 1981 the wi ndmill was
ready for te sting.
Performance
The performance of this project was n ot as initially
projected . The Savoni ous windpu mp never produced an
adequate supply of seawater and was soon abandoned.
Even the larger capacity pi ston pump did not help. Sea-
water is still supplied by a petroleum-fueled water pump.
The larger Dempster w ind pump was also a disap-
pointment. It was determined after installation that
although the anemometer showed adequate wind speed,
it did not show the wind turbulence in the area . The
north ridges surroundi ng the hatchery site produced a
"wi nd sh adow" that caused t he Dempster to gyrate
instead of face the wind as desi red . T he small diameter
water transfer pipe was also too restrictive, indicating
that a three or four-inch pipe was needed.
With all the co n sulta nts and literature used to re search
this project in the beginning, a ll rules were b roken when
t he actual system was ac tually installed. The wind direc-
tion was ne ver monitored. When the Dempster was in-
stalled, it was installed according to convenience and
necessity in stea d of measured results . The farm windmill
ended up in a protected location, a "wind shadow." As
VanHyning put it , "the systems worked in the sense that
they pumped water, but with the locations chosen, the
amount of water would be margi na l for even a mom and
pop operation :· For a commercial venture, the project
was not over ly success ful.
Future p lans are to relocate both the hatchery and
wind systems. Wind speed and direction measurements
will be used to determine the optimum lo cation for the
Dempster . The Savonious is still questionable. Other
ideas include purchasing a small windgenerator to power
112
an electric pump. This could be used to deliver seawater
to the hatchery location and may prove more econom-
ical; however, the need to maintain battery banks makes
this a questionable approach.
The last aspect of this project, gathering a nd assimilat-
ing information for o thers was accomplished success -
fully. A detailed project report was made by Nerka, Inc.,
which in cludes a tremendous amount of background on
wind power a nd windpumps.
Tips
"Place th e windmill in an open area, away from trees
and out of she ltered va lle ys," sai d VanHyning. "I cannot
stress t his point enough. Although such a reas may n ot
be the best location for the hatchery itself, a suitable
compromise must be found if you are to use this energy
source :'
Funding
U.S. Department of Energy
Grant Recipient
Nerka, Inc.
Jack M. Van H yning
P.O. Box 80165
Fairbanks, A laska 99708
$21 ,805
Windmill parts (top right) are unloaded from a makeshift land-
ing craft. (Bo ttom right), the installatio n of a firm tower base.
The completed installation (left).
I
Waterwheel made
more efficient
Water whee l technology has undergone a n other
revolution in th e hands of entrepreneur Robert Nelson.
He's designed a water wheel capable o f ge nerating 600
watts of electricity-perhaps twice as much as s im ilar-
sized , conventional w he els. That's more than en ough
power for his remote lodge on Thayer Lake , about 60
miles sou th wes t of Juneau on Admiralty Island in S o uth-
east A laska.
"Mos t of the electricity goes for the radio, p ower tools
o r for cooking," says Nelson. 'The freezer is operated
directly off the wheel."
This isn't the first time Ne lso n has bui lt a water wheel.
H e built a co nventional water wheel at Thayer Lake in
1947 because it wa s too expensive and too difficult to
tran sport gasoline to the lodge.
So far, Ne lson's new water wheel has been working
we ll since he installed it in 1981. Now he and his wife,
Edith , do not h ave to worry about fly ing in expensive
gas to their remote lodge.
"''ve got most of the bugs out of it ," says Nelson, a
retired electrician from Ketchikan who runs the lodge
from spring until fa ll. "It works beautifully. A ll I h ave to
do is g rease it once in a while :'
System Design
Conventional water wheels are not very efficient be-
cause they ca rry t he water through only about one quar-
te r of the turning radius before rele as ing it.
By compari son, Ne lson improved the efficiency of the
conventional water wheel by adding covers to the trough-
like buckets that do not dump th eir load of water until it
completes a 180 degree revolution . This means hi s water
HYDROELECTRIC OVERSHOf WHEEL
113
wheel is able to add more thrust to the drive sh aft.
"In conventional, overs h ot wa ter wheels the water falls
onto the top of the wheel and stays there un ti l it gets
about a quarter of the way down ;' says Nelson . 'The one
I designed h olds the water in until it gets to the bottom of
the w heel , doubling the power."
Nelson's seven-foot-di ameter water wheel is made of
three-sixteenth-inc h thick s heet steel. The wheel has 42
cedar buckets he ld in place by metal slots.
Each bucket is 36 inches lon g a nd is fitted along its
length with a five-inch-wide wooden cover attached by a
s lightly off-center nail. With the force of gravity a nd the
weig ht of the water, each bucket cover w ill open and
close at the appropriate time. At the b ottom of the
wheel, the weight of the water w ill sh ift to the opposite,
outer edge of the cover, forcing the cover open a n d
d umping the water o u t.
At the top of the wheel, cascading water fills the bucket
and the w heel begins its downward rotation. The water
wi ll force the cover s hu t . The cover doesn't reopen until it
swings to the bottom of the w heel's arc.
"With our modern te chnology, the steel water w heel is
just as easy to construct as a wooden one," said Nelson.
"I believe this project could have been built SO or 75
years ago without too many difficulties provided rolled
shee t s teel had been available :·
Ne lson a lso built a 500-foot-long, polye thylene "pipe-
line" to channel water fr om a nearby creek to the water
w heel. The fle x ible material wa s laid on wooden braces
three feet above the grou nd . The t ube would lay flat
w it h out any water passing through it , because it is such a
A cedar trestl e (/eft) supports th e w aterwa y. A gea ring and
heat ing element (above) give overspeed protection. (Next
page), buckets cl ose as th e w heel ro tates.
light material.
Water cascades onto the water wheel at about 100
cubic feet per minute, turning the wheel at three revolu-
tions per minute . This makes a two-phase, 110-volt,
60-cycle generator turn at 450 rpm, producing about 600
watts of electricity.
"By using a two-phase AC generator I was able to run
a refrigerator of 3 .5 amp capacit y directly off the water-
wheel generator," Nelson said. Additional power is stored
in a bank of Edi son batteries.
Other features Nelson has a dded at his home include a
hydraulic ram system that pumps water to a tank located
high in a tree . H e also u ses dried muskeg mixed in plaster
as insulation on the freezer and hot water storage tank.
Water is heated throug h pipes placed across the back of
the fireplace.
Performance
Overall, Nelson has been ve ry pleased with his water
wheel, which took only eight months to build and test at
his Ketchikan home .
Afterwards, he di smantled the hydro project , loaded it
into a plane, flew to Thayer Lake and reassembled it. So
far, his system has worked well.
One problem -flooding of the creek-threatened the
project. But Nelson resolved this difficulty by building a
small gate that will automatically close off the entrance
to his water tube any time the creek floods. This ingen-
ious device uses a block of s tyrofoam that floats o n the
water. An old broo m stick extends up from the block
with a thin r o pe fastened at the top. When the water level
rises , the rope is pulled up, causing a wedge to fall out
from under a weighted five-gallon bucket that forces the
gate closed .
He also strung an electric wire along portions of the
pipeline to prevent bears from clawing into it.
114
Tips
Nelson discovered a number of small details that
improve the wheel's performance. Among them is his
advice to :
• Soak all wood for at least one week before installing
it in t he water wheel.
• File the heads of any of the nails used for the bucke t
covers to get rid of roughness that may h inder their
free-swinging motion.
• String a thin monofilament line over the· ce nter of
the wheel so that the bucket covers gently bounce
against the line and ensure the bucket covers close
promptly.
• In order to convert an AC motor it must be at least
seven horsepower so that its rotor is seven inches in
diameter. The rotor must be milled to provide fl at
spaces to hold permanent magnets. The stator must
be rewound with a lightweight enameled wire.
• Direct the power produced by the 450 rpm ge nerator
through a 110 volt A.C. battery charger to prevent
power surges.
• Consider designing a mechanism that will automat-
ically close when the creek flood s. Such a device w ill
reduce the amount of water traversin g the pipe, and
prevent flooding of the water w heel.
Funding
U.S. Department of Energy
State of Alaska
Grant Recipient
Ro bert Nelson
P.O. Box 5416
Ketchikan, Alaska 99901
$454
929
I
Hydro system powers
hatchery
Eugene Richards b ui lt a hydroelectric system so he
wouldn't have to rely on expen sive diesel fuel for his
sa lmon hatc her y in Southeast A laska.
A favo r ite s top of the cruise sh ip lin es because of its
Gold Rush her itage, Skagway is also the gateway to
Canada's Yuko n Territor y along the Kl ondike Highway.
Across Tai ya Inl et lie s Burro Creek a nd Richards' non-
profit hatchery. Access to the s it e is by boat only. No
power, water, electricit y or other servi ces are supplied to
the remote si te by the city.
Richards was committed not only to the hatchery proj-
ect to re p lenish local sa lm on s tocks, but to build an
e nergy system a nd home o n the site , as well. In a ll , these
projects to o k five years to accomplish; the firs t year, the
hatchery took top priority. After being awarded the 1980
AT grant he built the p owerho use for the hydro system .
The Richards used the structure as a temporary home
until their log res idence was completed in 1982.
'The hydr oelectric plant was necessary a t Burro Creek
Fa rms to provide inex pensive electrical e nergy fo r the
operation of a nonprofit sal mon hatchery," said
Richards .
Diesel oil, he sa id , was p riced at about $1.09 per
ga llon fo r No. 1 fue l and 98 cents per gall on for No. 2
fue l during the spring of 1984. Residential power cost
from 17 to 20 cents per kwh depending on consumption.
Richards hopes his hydroelectric plant will serve as a
model for buildi ng s imi lar p lants t hroughout Alaska.
"The project will deve lop a renewable energy sou rce
and the hatchery will p rovide more sa lmon fo r co mmer-
cial and sport fi shermen," he said.
Design and Construction
A 1,400-foot-long, 10-inch PVC pipe channels water
fr o m a dam on Burro Creek to two pelton w heels
mounted side by side. There are two water je ts on each
of the two tu rbines. The two turbines drive a 25 kw
generator. The turbine units are commercially made by
Pe l te ch .
The 25-ki lowatt, three-phase 220-volt Lima-brand
brushl ess alternator produces electri city for refrigerator
co mpressors used to process fish.
The pipeline, which has a 125 psi rating, was laid in
sections. Richards uses quarter-inch aircraft cable and
cable clips to secure the pipe to expansion bolts, w hich
are anchored in bedrock or large boulders.
At the anchor po in ts, the pipeline is wrapped in build-
ing pa per, a lumin u m flashing, and used firehose to
se cure and protect the pipe from chafing. Downhill ties
a re used o n s lopes at 200-to-300-foo t intervals to prevent
the pipeline fr om "c rawling" down the hill.
Where the pipe changed grade, supporting posts were
fabricated from six-by-eig ht-inch treated wood at 10-foot
intervals s o that the pipe re sts on saddles formed by two-
by-1 0-inch braces.
Special co n cre te a n chor s were in s tall ed for the last 80
feet of the pipel ine to p revent t he pipe fro m excessive
11 5
HYDROELECTRIC, PELTON
movemen t and strain where it approaches the power-
h o use. A t the inlet above the dam , a woo d filter box and
sc reen also were install ed to prevent debris larger t h an a
half-i nc h in w idth en tering the pip el ine a nd possibly
plugging the nozzles at the pel ton w heels.
P roblems
Overall the system h as worked well si nce it s install a -
tion, providing t he Richards with round-the-clock
electricity.
Low winter temperatures, however, caused free zi ng
and icing on th e fi l ter box, along sections of the pipe and
in the metal discharge pipes. And despite good perform-
a nce , the governor disen gaged from the pel ton wheel,
causing a bearing b urn-out a nd scored shaft.
Freezing temperatures made it difficult to maintain
adequate wa ter fl ow. Ric hards says he p la n s to inc rease
the height of hi s dam o n Burro Creek to boost the depth
of its water.
An atmospheric vent a ls o was install ed at the top of
the pipeline to d ecrease the possibility of dead water
freezi ng. And he pl ans to put a man ifo ld in the lower end
of the pipe for clean-ou t and to keep the jets and the
main throttle valve free.
Tips
• Make cer tain t he system can shut down easi ly and
will drain automati cally. The atmospheric vent at
the top of the pipeline is critica l to p revent blow-
outs and p ipe coll apse when drain in g t he p ip eli ne.
• Install requ ired valves near heated areas wherever
possib le to keep them from freezing.
• Avoid bending PVC p ip e, especially in the lower
sec tion s wh ere pressure is greatest.
• Make s ure the pipeline is anchored well .
• Use an open ditch or a wood flume to c h annel
water from the pelton wh eel si nce metal pipes tend
to freeze during winter.
• PVC pipe s h ould not be exposed to direct sunlight
after in stallation. It s hould be pa in ted wi th a
water-base synthetic la tex paint or wrapped with
ta pe when install ed in s unlig ht.
Funding
U.S. Depart ment of Energy
State of Alaska
Grant Recipient
Eugene Rjchards
Burro Creek Farms, Inc.
Box 455
S ka gway, Alaska 99840
$5,675
5,675
..
' 1
-I
Micro-hydro project
generates interest
Noted for eagles and rugged mountain peaks, at the
head of the Lynn Canal sits Haines, one of the historic
embarkation points for trails leading to the interior gold-
fie lds and last stop for most tour ists traveling the Alaska
Marine Highway. From here, it's up the C hil kat River
Va ll ey, over the backbone of the Saint Elias Mountains to
Haines Junction and the Alaska Highway, 'passing many
small picturesque streams along the way.
To the tourists, these streams make beautiful snap-
shots for the folks back home. To Roy Lawrence, these
same streams make excellent locations for micro-hydro-
electric projects. In an area of high electrical bills,
limited solar and wind power potential, hydro power
and steam generators are about the only a lternatives.
Lawrence chose hydro power because in addition to long
life and low maintenance costs, "there are no emissions
from hydro units and even the sound is at a minimum:'
Lawrence had visions of a small hydroelectric system
when he first bought hi s 43-acre farm in the early 1970s.
Electricity was expensive then and after the oil crisis, it
became a lmost out of reach for many of the 1, 700 resi-
dents in the Haines area. Lawrence figured that if he
could successfu ll y demo n strate the benefits of hydroelec-
tric power, he could generate en ough interest to develop
and market his own energy systems. "Thi s will not be
something just on paper or in a book, but a real live
entity actually producing power and not theorizing
about it:' he said. With this project, Lawrence would
have a running demonstration unit, plus practical experi-
ence. If hi s vision were proven true, he would also have a
successfu l business somet ime in the future.
In April1981, Lawrence received a grant to build a
micro-hydroelectric power generation system on his
property at mile 37 of the Haines Highway. The project
involved building an impoundment dam, water transfer
system, power generation system, and transmission line.
Design and Construction
Lawrence decided that his dem onstration unit should
be large enough to supply the power need s of a small
h ouse, yet within the economics of area citizens. He
chose a small1.5 kilowatt, 120 volt, 60 Hertz, alternating
current generator from Hydro-Watt of Oregon. This
generator uses a Pelton-type turbine to turn it. The solid
s tate controls keep voltage level and frequency within
three per cent of its rated value. Automatic load control
and other safety features were also incorporated into the
design. For instance, a special safety solenoid is pro-
vided for complete system shut-down in case something
were to go wrong. The sole noid must a lso be manually
reset, ensuring that the problem must be corrected before
the system can be restarted .
The impoundment dam is located about 310 feet
above the power unit. Four-inch PVC pipe transports
water from an impound box located behind the small
dam. The earth /rock fille d dam has a two-inch-thick
wooden reta inin g wall backed by a 28-gauge galvanized
metal "I.:' shaped seal. Additional bracing is provided by
galvanized pipe pounded in to the ground in front of the
dam. Galvanized cab le from these pipes to deadman
117
beams imbedded in the pond's floor behind the dam
provide additional safety.
A movable 18-by-six-inch spillway keeps leaves and
other float ing debris from clogging the screened open ing
in th e water impound b ox. T he four-inch, schedule 40
PVC water transfer pipe is fi t ted to the bot tom of t he
impound box, below the theoretica l seasonal low water
limit. T he spillway is designed to allow periodic removal
for cleaning and maintenance .
The water transfer pipe carries the water to the power
unit located about 130 feet below the dam. Located in a
six foot-by-six foot uninsulated building, the pipe can
deliver water at about 56 to 60 pounds per square inch
pressure at a l most 100 gallons per minute, more than
enough to produce 1,300 watts under fu ll load.
Freeze pr otection for the generator is provided by an
insulated 30-by-16-inch enclosure made of two-inch-
thick polystyrene bead board. Only the turbine and
generator are insulated during the winter. As long as
water is flowing in the s tream, freeze protection is not
needed for the water transfer pipe. When the system is
shu t down, the impound pond is simply drained along
w ith the water p ipe.
Power from the generator is transported to the house
through approximately 650 feet of 110 size cable.
Lawrence originally planned to use tripods made from
12-foot-long four-by-fours to support the cable, but
during brushing the transmission line path, it was found
that enough tall, straight trees existed to forgo the
tripods.
Performance
The small 1.5-kilowatt generator has successfully pro-
vided enough electricity to run both house lights, a
small refrigerator and a chest-type freezer. Heavy usage
items such as shop tools or electric heaters obviously
require a larger system .
Even during the late summer, when the water level is at
its lowest, the generator has been able to produce power.
If it had not b een for a small leak in the face of the dam
and one extremely dry summer, Lawrence's hydro proj-
ect could h ave supplied a full1 ,300 watts at all times of
its operation. As it was, the leak combined with the low
streambed water level dropped head pressure to about 35
to 40 pounds per square inch. The generator's output also
dropped to about 100 watts at 110 volts. During this
time, a small diesel generator supplied household power.
The small size of the generator required continual
energy conservation. A volt meter was plugged into a
wall socket to monitor line voltage. Any sudden unex-
plained drop usually meant that the screen on the water
impound box was clogged. This did not happen often
and periodic monthly cleaning usually prevented this
problem.
Although the system was fairly easy to install,
Lawrence recommends using a more flexible water
transfer pipe. The ri gid PVC required special bends to be
made at an added cost. The original design also has the
pipe p laced a couple of feet off the ground. Burying a
flexib le pipe would reduce both freeze damage a n d the
chance of a fa lling tree destroying the water transfer
system.
Problems and Conclusions
Lawrence has experienced very few p roblems with this
project. This can b e attributed directly to the exce ll en t
planning he did in the beginning stages. The solid state
controls and si mplici ty of the system eliminated many
problems experienced by other micro -hydroelectric
developers.
Although some time was lost due to personal illness at
the start of the project and the fact that the ge n erator ran
backwards at first, Lawrence was able to overco me these
delays and finish the project. The small leak in the dam
was repaired during a routine scheduled maintenance
period .
118
Lawrence has been in terviewed by KH NS, a local
radio station, an d there seems to be a lot of local interest
in his system. Since this was one of the project's original
intentions, it can be considered a complete success.
Whether Lawrence can develop a market for his idea
depends o n his continued enthusiasm for this renewable,
non-polluting power generating system . Since his total
energy costs for 1983 were only $68, there is no reason to
believe his enthusiasm will wane.
Funding
U.S. Department of Energy
State of Alaska
Grant Recipient
Roy La wrence
Mile 37 Haines Highway
Box 644
Haines, Alaska 99827
$3 ,370
7,862
\
I
\ ,
Willie Nelson regulates
power output
Energy independence is a dream m a n y Alaskans h ave,
including Chester Johnson. When h e first homesteaded
at Mi le 49 of the Richardson hi ghway in 1968, he would
of ten look at the water fall behind his house a nd wonder
how he could tap it s energy. In 1969 , he fou nd his
answer. While on a trip to Chitina, he found an old
Francis turbine in t he ci t y dump. Although it had lain
there for some yea rs , the hydro turbine w heel was still in
workable shape. Later that same year, Johnson recovered
an o ld 2.2 k il owatt generator from a burned-out build-
ing. Now all he needed was something for t he penstock.
The Valdez city d ump su p plied that. He sa lvaged the
a lu minum pipe that served as Valdez's emergency water
main after the 1964 earthquake.
Using a lot of creativi ty, sweat, and a few new words,
Chester Johnso n soon made himsel f a makeshift micro-
hydroelectric p ower pl ant , usi ng the e nergy of his back-
ya rd waterfall a nd all t hat "junk" he found. After initial
adj ustmen ts, the c r ude system put out one kilowatt of
energy, en ough fo r his small house. Un fo rtu nate ly, he
had to "re gulate" hi s sys tem manually. A volt
meter was plu gged into o n e of the house sockets. When
the meter indicated that to o much power was available,
Johnson simply switched o n another li ght. He kept
sw itchi ng on li ghts until either the meter indicated the
proper voltage and power values, or until "Willie
(Ne lson ) so und ed right on the phonogra ph :' If his
phonograph played a little slow, Jo hnson s imply turned
off lights un til power in creased . This s impl e "load
control" worked for almost 10 years and would h ave
worked much longer, except Johnson had bigger plans
for his waterfall.
119
In 1979, he received a grant to upgrade his small one-
kilowatt ge nerator to a five-kilowatt system. His new
system was to include automatic load co ntrol a nd would
be able to supply his house and two others with power
fro m May through October. The project invo lved modi-
fy ing the turbine/generator, instailing a new water gate
and new p enstock, a nd la ying transm issio n lines to his
neighbors' homes.
Design and Construction
The upgraded system would essentially follow the
same design a s his older system with a few enhance-
ments, unfortunately, load control wouldn't be one
of them. No one could remember h ow the old turbine
was governed. Johnson decided to continue his meter
mo nitoring until a load co ntrol cou ld be d es igned.
By midsummer, work began on the penstock. Johnson
and several friend s ha nd carried 30 foo t sections of the
new fo ur-inch aluminum pipe up the steep cliff and
strung them along the side of t he waterfal l. Although
each section only weighed 20 pounds, t he stee p, heavily
timbered moun tai nside and thick underbrus h made it
see m doubly h ard.
The most difficult part of the whole pro ject wa s
w in ching a h uge cast iron, 10-inch gate va lve up th e
mountain . T h is valve wo uld be used to shut off the water
during the win ter months. The half-ton va lve, mounted
on a skid, had to be slowly lifted up the cliff with a
12-volt (direct current) winch. A portable gasoline
p owered generator was also moved up the m o untain. The
generator was used to recharge the large "CAT' batteries
p o wering the w in ch. Moving the gate was a long slow
proces s, taking two co mplete summers to fini sh . The
Chester Johnson (above left) brings new life to abandoned
equipment. Johnson's open air hydroelectric system (above
right).
final resting place for the gate valve was about 1 ,000
feet from the turbine u p a 45 d eg ree grade. The w ater
delivery pipe is reduced to a one-inch nozzle at the
turbine.
Problems and Con clusions
Ver y few problems were encountered d u ring system
constructi on. A few sections of p enstock had to be
replaced w hen an early freez e broke two sectio ns . There
was also a continuing problem of birch leave s clogg in g
the inlet screen of the penstock.
Load control was a continuing problem with both t he
o lder system and the new five-kilowatt model. Johnson
is still awaiting assistance here. An experimental m ag-
netized a luminum disk "Eddy Current Brake" will b e
attempted at a later date, but it is unsure if this device
will really work.
Water beats wind for
reliability
There's a history of pioneers relying on water wheels to
generate power in Southeastern A laska . And Ken Cassell
is adding to that heritage in a modern way.
Cassell is buildi ng a hydroelec tric sys te m on two
creeks that tumble by his home in Juneau. Students from
the Juneau-Douglas High School are assisting him.
'Water is more reliable than wind power and you can
get more power out of it;' says Cassell , a h igh school
teacher who studied the p roject's Pelton wheel tech-
nology during graduate school. ''I'm interested in
mechanics and how you can corner the water's power'.'
T he project has been an invaluable educat ional tool.
High school students in such classes as surveying,
physics, drafting, photography and metal s h op have
worked on various stages of the project.
The physics students also will continue to monitor the
system's efficiency after it begins producing electricity in
the fall of 1984 . Power from the sys tem will be sold for
up to 9Q: per kwh to the Juneau electric utility. He
expects his system will ge nerate 10 kwh.
Casse ll, who's enterin g his fourth and fin a l year on the
project, is optimi stic about finishing it shortly.
"''m in t he final stages;' says Cassell, who also owns
his own business and is in the U.S . Navy Reserves .
"I worked with students a nd I built everything from
scratch . Even the switch panel. It's been a good learning
experience'.' And he sees no reason why the system will
not perform well.
120
A ll -in-all , Johnson s ucceeded in d eveloping a micro-
hydroele ctric system from m ostly sa lvaged parts that
cou ld s upply enough power to run three household s.
An automatic load co ntrol in the future woul d
enhance this system a little more, but "as long as Willie
sounds right;' power is under control.
Funding
U.S. Department of Energy $6,280
Grantee
Chester Jo hnson
Mile 49 Richardson Hi ghway
Valdez, Alaska 99686
System Design
Water from the two streams is piped in two pipelines
down a steep hillside to a powerhouse with two six-inch
Pel tech turbines and t wo GE induction generators . The
r ushing water turns the Pe ltech turbines, producin g
e lectricity.
Ke n measured his two streams every other day for a
year, except during the winter when h e measured them
just once a week. To measure the smaller stream, he used
a five-gallon bucket with a stop watch to measure the
flow. Because of the size of the larger stream, he had to
use the weir method. Eve n with the wei r, he was not
satisfied with the results, so he went to the U.S. Weather
Bureau and obtained monthly rainfa ll data for the
prev ious seve n years. Then, he calculated a theoretical
average month and watched the Weather Bureau data for
t he month that was closest to the theore tica l average. He
measured the larger s tream dur ing th at month to deter-
mine the turbine size he would need for his system.
The water is initially held in concrete catch basins
which were placed in each s tream. The basins are
designed to release water into pipes leading downhill to
the powerhouse when there is enough water to operate
the turbines.
By the summer of 1982 all the materials needed for the
powerhouse, penstock, and access stairs were on site and
ready for construction. It took the rest of the summer,
three athletic high sc h ool helpers, and an excavator
brought in on a Navy-type landing craft to complete this
121
Ken Cassell (t op) stands beside his powerhouse at the tidel ine.
Installing (middle right) the hydroelectric unit. A concrete
form (bottom right) works as a catch basin. (Left), Cassell
inspects his control panel.
stage of the project. The project could have been done in
less time had Cassell not had to drag everything either
down the steep bluff, or up the beach.
Building the catch basins was a major problem. The
steep angle of the hillside made climbing difficult and
climbing with equipment and materials virtually impos-
sible. It was decided to use the services of a helicopter
and cement pumper for these structures.
The catch basin for the smaller stream, which was
closer to Thane Road, used a six-sack mix of cement
delivered by a cement truck and pumped 120 feet uphill
to the basin's location. Fourteen inch deep holes had
previously been drilled a foot apart into the bedrock, to
pin the structure to the rock face.
The catch basin for the larger stream is located in a
high and remote site. A generator was packed up the
mountain for power during the form-making and drill-
ing process. Four yards of concrete were finally poured
into the forms in October using a helicopter.
The penstocks are two plastic PVC pipelines, each
rated at 200 pounds per square inch pressure. The pipe,
manufactured by Johns-Manville Company, comes in
20-foot lengths with bell and socket joints that do not
require cementing. The socket has a rubber gasket which
must be clean during installation to prevent leaking.
One pipe is four inches in diameter and is 1,300 feet
long. It drops 437 feet in elevation to provide 200 pounds
per square-inch pressure at the turbine. The stream flow
is 13 cubic feet per second (cfs).
Similarly, a second, parallel pipe extends 800 feet,
dropping 200 feet in elevation. This pipe has a four-inch
diameter which narrows to 2.5-inches. Stream flow is
3.5 cfs.
Both lines are buried to protect them from bears and
falling trees. However, the pipes are above ground where
they extend down a bluff to the powerhouse. The pipe is
supported every 10 feet and held off the bluff face by
cables anchored by rockbolts. The cable is fastened to
clamps at the pipe fitting joints.
Each pipe channels the tumbling water to nozzles
which spray onto each of the six-inch-diameter Peltech
turbines. The turbines turn fast enough to achieve
1,800 rpm.
In the winter, when water flow is low, there is a mani-
fold between the two turbines so that the small generator
can be switched to the highest head stream for greatest
efficiency.
The brass Pelton wheels for the turbines were made by
Bill Ketchings in Kent, Washington. Rough castings were
shipped to Juneau where the high school machine shop
students ground off the burrs and polished the buckets.
Using electrical controls designed in the U.S. and
manufactured in Denmark, the power plant monitors
over/under voltage and frequency conditions, over
current, reverse or out-of-phase power, and low water
level in the catch basins. The controls are plugged into
tube sockets on a control strip and activate water deflec-
tors in the turbines when a problem is detected. These
122
water deflectors rotate 90 degrees into the spray from
the water jets, shutting down the turbines. When this
happens, the control valve in the catch basin is closed
and the penstock pipe is allowed to drain. To restart the
seven-kilowatt generator, this problem has to be rectified
and the generator restarted manually; with the smaller
generator, restarting is automatic.
This system uses two induction generators, one rated at
7.5 kilowatts and the other at 5 kilowatts. An
induction generator is used for safety reason~. These
power plants require an outside signal before they pro-
duce any power. Since the object of this power plant is to
supply power to the local utility grid, a method of shut-
ting down the generators automatically when the power
company experiences problems is essential for safety
reasons. Whenever the utility company loses power, for
whatever reason, the reference signal is also lost and
Cassell's hydroelectric power plant also shuts down.
Problems
Receiving equipment on time was one of the biggest
obstacles Cassell had to overcome.
"By the time one researches the equipment to find
what is best suited, finds the vendors, orders and waits
for shipped merchandise~one year is gone:' Cassell says.
"The items needed to build a hydro generation system are
industrial equipment and are not found in mail-order
catalogs':
The project also has taken more time than he antici-
pated. He suggests ordering pre-assembled units when-
ever possible.
'This was partly due to the fact that the whole project
was put together in bits and pieces, each little item was
ordered separately~ Cassell says.
Tips
After spending four years on the project, Cassell has
several suggestions to make:
• Plan ahead. Obtain as much information as possible
about stream flows, elevations, and where to place
the power house, catch basins and pipeline.
• Set aside at least a year's time to find, order and
obtain necessary equipment.
• Make sure gaskets in the pipelines are clean to
prevent leaks from developing.
• Use bell and socket joints that do not require
cementing for the pipeline. In rainy climates, like
Juneau, it is hard to keep the fittings clean, or obtain
a good seal with glue. Also, if glue forms a ridge
inside the pipe, the resultant turbulence could cause
cracking.
Funding
U.S. Department of Energy
State of Alaska
Grant Recipient
Ken Cassell
5680 Thane Road
Juneau, Alaska 99801
$ 4,850
25,080
" ... care involved when
you become your own
power crew''
When Louis Butera first saw the sparkling creek
tumbling through the woods, he knew that's where he
wanted to build his hydroelectric dam . ·
So he bought a creek-side lot and built a home and a
hydroelectric system in Eagle River, about 16 miles north
of Anchorage.
"I got interested in hydro first," says Butera. "And, then
I went out and looked for a creek property. And I found
this particular place:'
The project is a success, generating between 1,000 and
3,000 watts year-round, despite sub-zero temperatures .
Butera uses the power to operate his refrigerator and heat
his 1 ,600-square-foot home. He says it's saving him $15 a
month on his electric bill.
"It's working great," says Butera , a civil engineer and
consultant who owns Alaska Hydro Systems. "I haven't
had any serious problems.
"''ve als o installed other similar hydroelectric systems
for homeowners in the Ea gle River area;' he says . "They
like them . But there is a lot of care involved when you
become yourcown power crew:'
System Design
Butera built a two-foot-high dam using two-by-six
lumber across the five-foot-wide creek . The boards of
the dam can be easily removed to lower the water level
for cleaning the screened intake .
Water diverted by the dam flows through the screen
into a six-inch-diameter, 408-foot-long, polyethylene
tube . The 40-foot sections of the polyethylene pipe were
joined together with bolted clamps that secure rubber
gaskets on the ends of the pipe . The pipe lays ex posed
directly on the ground . The pipe, anchored with pilings,
channels the water to a Pelton wheel turbine . A gate
valve at the dam allows the water flowing to the turbine
to be shut off .
The Pelton turbine is housed in an eight-foot-
by-12-foot wood shed. The shed has wood siding to
match Butera's house.
Butera redesigned the Pelton wheel and built a new
housing for it that's six inches wider and two feet longer
than the original. He also made it r o und instead of
square.
'The advantage is less resistance to water flow, and
less splashback inside the Pelton wheelhousing;' he says.
The creek water is funnelled through two nozzles so
that it hits the Pelton wheel at 35 pounds per square inch .
The Pelton wheel spins, turning a belt system which is
connected to a five-kilowatt alternator. The system
generates a 120 volt , 60 cycle current .
An electronic governor regulates the electrical current
by keeping the turbine spinning at 1,800 rpms. Water
flows out of the turbine into a 55-gallon drum, and then
back to the creek via a six-inch PVC pipe.
123
Performance
Butera says he's pleased with the hydroelectric system.
It works well , performing better than his expectations.
Its simple design makes it easy to build and cost-
effective .
But like any new system he 's had to spend some time
fine-tuning it. A defective governor had to be replaced ,
and a back-up governor was added to shut the turbine
down if the voltage exceeded 140 volts.
A few other tie-ups occurred. The creek's water flow
has occasionally dropped too low to run the turbine.
Trees also have toppled on top of his pipeline, but he says
the polyethylene pipe was not damaged. He's also had to
contend with a bearing failure in his turbine two years
after he installed the system.
Each year a critical time is just before freeze-up . The
stream temperature will drop below 32 degrees. When
the stream forms an ice layer on top, the water tem-
perature rises a couple degrees. So far this critical period
has not caused a freeze-up problem in the intake, pipe-
line or turbine, but the possibility exists . "But the turbine
has per formed as expected;' Butera says.
Tips
Butera has several suggestions to make regarding his
system , including :
• Order equipment early as it can take three to six
months to receive items such as the turbine and
governor.
• U se polyethy lene pipe . It 's ex pensive , but durable
and fle xible.
• The powerhouse should be well built and have a
south-facing window for solar heat. The floor
should be made of marine plywood .
• Place the screen so that the creek's flow will help
keep debris from building up on it.
• Make sure all wire connections are secure. A loose
wire could damage the governor, alternator, or gen-
erator. Split bolts should be used for all connections.
• Allow some slack when routing any wires between
trees to allow for tree swaying.
• Use flange fitting for all hydro installations to
prevent leaks at the joints. Silicone seal makes a
good gasket.
Funding
U.S . Department of Energy
State of Alaska
Grant Recipient
Louis A. Butera
SR Box 1667-ER
Eagle River, Alaska 99577
$4,251
2,811
124
Louis Butera (top left) rests beside the darn in let of his micro-
hydroelectric project. The water pipeline (top righ t ) snakes its
way through the woods. The Pelton system (left) shown inside
the powerhouse. (Above). Butera cleans debris from the screen
intake.
Hydro success requires
careful planning
"After living for three years without electrical power,
we are very excited and happy to have electricity any-
time we need it. The inside of our house is now bright
with both flourescent and incandescent li ghts; modern
appliances grace the kitchen counter tops; and a stereo
plays softly in the background. Best of all, t[-10se long
trips to Ketchikan for fuel and propane are now few and
far between-meaning boat fuel also lasts a lot longer'.'
All-in-all, the Cohrs, James and Maureen, are happy
with their new micro hydroelectric power plant.
When the Cohrs first moved to Saltery Cove , a small
sheltered harbor on the eastern side of Prince of Wales
Island, everything was run by propane or gasoline
engines. This included the clothes washer and dryer,
refrigerator, and even house lights. However, during the
1930's, the Straits Packing Company operated a small
cannery in the cove and made electricity from a small
stream near the Cohrs residence. The remains of the dam
and parts of the wooden penstock can still be seen along
the creek. James Cohr figured that if electricity could be
produced then , it could be produced now, especially
using modern, high output generators .
In 1980, James and Maureen Cohr applied for a water
use permit from the U.S. Forest Service. Soon after, they
were awarded grants from the AT program to build a
microhydroelectric (less than 10 kilowatts) plant on
a stream known as Saltery Cove Right. Their project
involved building a new dam on the stream, installing a
penstock from the dam to a new powerhouse where the
turbine and ge nerator would be, and laying underground
transmission line from the powerhouse to the family
dwelling and shop areas.
125
Design and Construction
The Cohrs planned to dam the small stream and
transport water through an eight-inch penstock about
500 feet, with a 50 foot head, to a Pelton wheel impulse
turbine . The turbine's output belt drives a 10-kilowatt,
brushless generator. The pulley ratio for the belt drive
would be adjusted after installation so that the generator
shaft turns at a constant 1800 rpm (revolutions per
minute). The generator's output would be 120 Volts AC
(alternating current) at 60 cycles per second. Although
the generator could produce up to 10 kilowatts, stream
flow calculations indicated an actual output potential in
the neighborhood of two to three kilowatts.
The dam was made from a large beach-logged cedar
that was cut to size and dragged up to the dam site. The
wood and rock filled dam, built upstream from the
Straits Packing Company site, was calculated to hold
back almost 500,000 cubic feet of water. A gate valve and
the inlet for the penstock were placed an additional40
feet upstream. The gate valve is surrounded by a wood
and galvanized screen "trash bin': Cohr also installed a
short catwalk to the trash bin and valve for periodic
inspection and cleaning.
The rigid trestle-mounte~ penstock hugs the right
stream bank. A small slide area had to be blasted clear
and a protective covering made duri ng this installation.
The penstock enters the powerhouse through a metal
reduction tube narrowing its diameter from eight inches
to about four inches. The four-inch pipe then splits into
two flexible 1% -inch pipes feeding the Pelton wheel jets.
Two jets are used presently, a 1-3 /8 and a 9116-inch
(inner diameter) jet. The turbine housing has facilities for
The old dam (a bove left) which produced electricity in the
1930's . (Above right), Jim and Maureen Gohr arriving home at
Saltery Cove.
II
additional jets if needed later.
The output of the turbine is connected through a belt
drive to a Lima-brand 10-kilowatt generator. The Lima
was chosen because the Gohrs believed that it is virtually
maintenance-free and extremely durable. Both the tur-
bine and the generator are mounted on a hand-poured
concrete slab within the powerhouse structure. The
output of the generator is transported about 400 feet
through 2/0 size underground cable to the house and
shop.
System control is through water deflectors and a full
load governor. The full load governor is used to evenly
distribute the load between a heat sink (electric base-
board heater) and other demands, such as the electric
stove or refrigerator. As the electric devices demand
power, the load is removed from the heat sink. This
works well because the Gohrs ensure that no appliance
uses over 1,000 watts and the available power is con-
stantly monitored. A volt meter is mounted with the full
load governor in the house for this purpose.
Over/under voltage conditions are also regulated
within a range of 110 to 140 volts. Whenever an
over/under voltage condition is encountered, a water
deflector solenoid is activated, dropping deflectors in
front of the water jets, shutting down the system. The
loss of power then causes a shunt trip circuit breaker to
disconnect power from the transmission line.
Performance
'The system appears to be fail safe;' said Gohr.
Although they are somewhat disappointed that the
generator produces less than half the calculated out-
put (1,300 watts), it produces enough for their needs. A
third jet may be added later to bring power output to 1.5
kilowatts.
During initial shakedown, a few small water leaks
were encountered, but they were minor and easily cor-
rected. Gohr was very methodical in his shakedown.
First, he checked the penstock for leaks and, then ran the
turbine for one week to seat the bearings and ensure
everything was in order. Finally, the alternator was
126
installed on an adjustable frame, the pulleys and belt
installed and the alternator run for a week, with all
power going into the heat sink. The result is a very stable
microhydroelectric power plant that is getting a lot of
interest from others in the area.
Problems and Conclusions
Other than the small water leaks encountered during
system shakedown, the Gohrs have had no problems
with their power plant. This can be attributed to thor-
ough planning in the beginning phases, selection of a
good hydro-engineer, and not taking shortcuts after con-
struction began. Although the lower output was dissap-
pointing at first, it did provide enough power for their
needs, in addition to a little extra so that their neighbors
could charge batteries or run small power tools.
Other land owners have also begun to show interest in
hydropower. One has already obtained a 12-inch Pelton
turbine and is planning to build a water-powered battery
charger. The Gohrs have also been asked to consult for
other similar hydro projects in the area.
Tips
"Check and recheck your available water system and
install a system compatible to the available water~ says
Gohr. Also, great care must be taken at the dam so that
small face leaks do not enlarge and cause water losses.
But, above all, remember what Francis Soltis, their
hydro engineer told them, Gohr said: "When you turn it
on, you find out how much power you will have-each
system performs differently'.' Don't get frustrated if
things don't turn out exactly as planned.
Funding
U.S. Department of Energy
State of Alaska
Grantee
James and Maureen Gohr
Box6077
Ketchikan, Alaska 99901
$5,300
5,300
What a difference a hot
bath makes
Sixty miles south of Sitka, near the tip of Baranof
Island, is Port Armstrong. Once a shore station for the
U.S. Whaling Company and later a herring reduction
plant, a few residences and a hatchery now nestle among
the few remaining signs of the former facilities. The once
profitable salmon fisheries are reduced to a . third of the ir
former levels and the herring catch is limited to seasons
measured in hours .
However, today's residents of Port Armstrong are
looking beyond the ruins . A commercial10 million-
egg chum salmon hatchery is now in operation . This
hatchery will bolster the reduced salmon fishery. Other
plans include a 20-ton cold storage plant to support a
new bottom fishing industry; and a small commercial
greenhouse that will supply fresh produce.
The only drawback when the initial plans were being
made was the lack of electrical power. Commercial diesel
units were available, but the residents weren't sure if they
wanted a noisy, foul-smelling, fuel-gulping diesel in the
midst of their town .
During the time that Port Armstrong hosted a herring
reduction plant, power was supplied b y ge nerators
driven by no less than 11 Pelton wheel generators .
Richard Mathews, a veteran commercial fisherman
a nd Harvard graduate, figured that what worked once
could work again . Next to the small community is a
year-round stream draining a small mountain lake . This
stream was used to power those generators before, and its
285 foot drop fr om the lake to the sea was more than
enough to drive a modern, high-efficiency micro hydro-
electric power plant.
In order to be sure that hydropower would be a good
choice, Mathews compared the price of a 50 kilowatt
diesel generator plus one year's supply of fuel with the
cost of a complete microhydroelectric power plant. To
his surprise, there was not much difference. H ydropower
had to be the answer to Port Armstrong's power prob-
lem . In addition to being cost effective , it would save
over 35 ,000 gallons of fuel oil yearly.
In 1980, Mathews obtained an AT grant to build a
hydroelectric project in Port Armstrong. The project
involved installing a penstock from the headwaters of the
small stream outflowing from Jetty Lake, building a
power h o use a nd installing the turbine /generator, and
installing an underground power grid to the various end
users. Dreams of long baths, fresh vegetables, and other
comforts soon filled the three-house village.
Design and Construction
The hydroelectric plant had to be able to supply the
needs of the planned commercial hatchery, greenhouse,
cold storage unit, and the three local residences, plus a
small wood shop/boathouse. The penstock would have
to b e more than 1,300 feet long with a 285 foot drop, all
over rough terrain . In places the penstock could be
secured directly to the bedrock; in other areas, heavy
cement weights would have to be used . Because Port
Armstrong is a fishing-orie nted community, the gener-
127
ator system would also have to be easy to operate and
virtually maintenance free . The unit also would have to
operate on a net head after friction loss in the pipe of
230 feet and a net flow of 3.5 cfs (cubic feet per second
of water) and generate at least 48 kilowatts. Mathews
originally chose a Peltech Model 975 impulse turbine
(Pelton wheel-type) connected directly to a Kato #6 P2-
0850 ge nerator. This was changed to a Lima belt driven
generator rated at 440 volts, alternating current, and 60
Hertz at 50 kilowatts when driven at 1,200 rpm. A Basler
voltage regulator and a control panel completed the
system. The control panel includes full metering for
voltage, frequency, and amperage, plus an electronic
switching panel with 24 contactors for heaters. These
form a prioritized constant load system that diverts
unused electricity to water heaters located in large tanks .
Excess energy heats the water in these tanks instead of
being deflected into the tailrace and wasted. The heated
water in turn is used to warm the greenhouse, hatchery,
and residences. The entire unit is self-contained and skid-
mounted making installation relatively easy.
The penstock was another s tory. Because of the rough
terrain and lack of room for a trestle , a flexible but
strong polyethylene pipe was used . The pipe material,
trade name "Driscopipe 8600;' is heat fu sed to form one
continuous piece with a single flanged joint fused to the
penstock where it attached to the turbine . This pipe was
chosen because it is tough and flexible, has low friction,
and can freeze solid without rupturing. More important,
Mathews obtained more than 900 feet of it at discount
from the dormant Starrigavan hatchery in Sitka .
Installation of the pipe was accomplished by helicop-
tering sections to the edge of Jetty Lake along with a
special machine to heat fuse them into the one continu-
ous piece. The heavy, black pipe was shoved out into the
lake as sections were added; then , the 1,300 feet length
was towed down the hill as a single piece. There were a
few side bets on the success or failure of this scheme .
Someone in town even predicted that the whole mess
would end up at the bottom of the grade looking like
huge coils of li corice. Luckily, there were n o problems
when the pipe was pulled down the hill .
The penstock is supported in the lake with 210 pound
pre-cast concrete blocks. A weighted crib of treated
timbers with a stainless steel screen was use d to weight
down the open end of the pipe and keep debris from
entering it. Between the lake outflow waterfall and the
powerhouse, rock anchors, galvanized steel cable, and
restraining collars were used to keep the pipe from
slipping.
The 10-by-12-foot frame powerhouse shields the tur-
bine and generator from the Southeast's perennial rains .
The penstock, after a 285 foot drop, enters the p ower-
house and is attached to the two-nozzle Peltech turbine .
A Woodward hydraulic governor keeps the o utput fre-
quency at 60 Hertz.
128
A meta/saddle (above) clamps the pipeli11e.
Richard Math ew s a11d a11 assista11t (left)
p repare to i11stall the 300 lb. gate valve.
From the powerhouse, underground wires lead to the
newly constructed salmon hatchery, the cabins, shop
building, and cold storage facility. Underground cables
were chosen to keep the aesthetic beauty of Port Arm-
strong intact.
Performance
At 4:30p.m. Christmas Eve in 1981, Richard Mathews
threw the switch and the Port Armstrong hydro system
went on line. For the first time in more than 20 years,
electric lights glowed in the winter night. In celebration,
a large roast was cooked in an electric range for a special
Christmas dinner. Two other residents eagerly waited
their Christmas present, long baths in water heated by
"electric" water heaters. Baths in the "old days" required
heating big awkward pots of rainwater and lugging them
out to a bathhouse. While they soak in the laps of
luxury, their clothes will be drying in an electric dryer.
From all indications, the power plant is a resounding
technical and social success. There is enough power
available for the hatchery, shop, cold storage, cabins, and
grow lights in a greenhouse. The unit produced consis-
tent power throughout the year, never experiencing
freeze up, or lower output during the winter months
when stream flow was minimum.
Conclusions and Problems
There were very few problems with this project other
than the design changes in the power house. The original
Kato generator and control panel were replaced by a less
129
expensive, but equivalent Lima generator. The Lima's belt
drive mechanism posed no problems to Mathews as the
turbine/generator was purchased as a complete unit. All
modifications were done by the manufacturer.
Mathews' method of developing this project success-
fully shows that with proper planning it is easy to install
hydroelectric systems in remote locations. The almost
forgotten technology has tremendous potential in this
area of Alaska and the modern self-contained units
which are assembled, aligned, and tested in manufactur-
ing centers makes the power plants relatively simple to
install, operate, and maintain. Another point Mathews
likes to make is that the system is environmentally
sound, does not pollute; operates quietly; and has an
extremely long life in relation to other electrical power
generators.
Funding
U.S. Department of Energy
State of Alaska
Grant Recipient
Richard Mathews
Box 538
Douglas, Alaska 99824
$22,084
26,325
II
Hydraulic ram ensures
reliable water supply
An innovative pump powered by water from a nearby
creek works "fine" as it provides a continuous supply of
fresh water from the same stream for most of the year to
the home of Don and Kathryn Chaney.
In fact, adds Don, it was Kathryn who designed the
hydraulic ram system that is driven by a sm.all amount of
the water tapped from the creek .
The water drops three feet as it flows through a two-
inch pipe from the creek to the hydraulic ram.
This vertical drop provides adequate force to drive the
pump, which lifts the rest of the tapped water through a
one-inch pipe to a 500 gallon storage tank 23 feet above
ground .
Don, a retired telephone construction and mainte-
nance worker, says the pump also provides water for a
nearby greenhouse . He describes the enclosed storage
facility as a "mini-city water tank'.'
As long as the water behind a small diversion dam in
the creek maintains its three-foot level , and the tem-
perature remains above 21 degrees, Chaney says their
domestic water supply source is "reliable'.'
A gasoline-powered pump is used to lift water to the
insulated tank for one to two months each winter.
Otherwise, the only interruption in the operation of
the hydraulic ram-driven pump is "an occasional clean-
ing that takes about 10 minutes . It's really simple;' he
says.
The system has been operating since 1980 .
131
HYDRAULIC RAM
The hydraulic ram, a type that has been manufactured
since 1894, operates silently, and pumps water continu-
ously with only the energy of a portion of the tapped
creek water.
It has eliminated the year-round operation of a
7,000-watt gasoline powered generator that used about
six gallons of fuel a day to run a one-half horsepower
electric water pump and electric water heater.
A wood-burning water heater now supplies the
Chaney's domestic hot water needs.
Part of the system's success is its location. The Chaneys
live near Petersburg in Southeast Alaska, where the
climate is comparatively mild and water is abundant. The
town lies along the Alaska Marine Highway (ferry
system ) Inside Passage and is resplendent with spruce
and tumbling waterfalls .
Don says there is "certainly" enough water in the creek
(excess water pumped into the tank is returned to the
stream ) to support similar systems in the area-if more
people lived near the water.
The system also is practical for widespread use where
climate and water conditions are favorable , he adds.
Funding
U.S . Department of Energy $1,535
Grant Recipient
Don Chaney
P.O. Box 1276
Petersburg, Alaska 99833
Freon steam propels
turbine
Sometimes an idea comes along that's so simple but so
unique that nobody believes in it. Arthur Manning had
that problem when he first proposed his novel power
generation idea. He even asked a professor from the
University of Alaska-Fairbanks' Geophysical Institute
for a professional opinion~'It won't work because you
can't build a perpetual motion machine;' he was told.
It's to our benefit that people like Manning aren't
deterred by "ex perts:' He knew his idea for generating
electrical power would work and could benefit groups
needing power in remote locations.
Conventional methods of generating electrical power
have either a fossil fueled motor turning a generator or
water or steam turning a turbine, which in turn turns the
generator. What Manning proposed was not really much
different from a conventional steam-powered electrical
generator. However, instead of boiling water, he wanted
to boil Freon and use the Freon steam to propel a turbine .
Because Freon typically boils at -20 degrees, the colder it
got outside, the more efficient his system would get .
In 1980, Manning was granted funds to build his Freon
powered electrical generator. He proposed to develop a
device that could tap hydrothermal sources, a previously
untapped energy source. The project involved building,
operating, and monitoring a hydrothermal Freon electric
power plant.
Design and Construction
Manning wanted to prove that you could use the tem-
perature difference between warm, running water and
outside ambient air temperatures (especially in the
winter) to develop electrical energy. His prototype
system would produce 2.25 kilowatts of power at 115
volts, alternating current. The energy used to boil the
Freon comes from the relative warmth of a lake or
moving water. The Alaskan winter will be used to
enhance that warmth, producing more electricity during
the winter when the demand is the greatest. The system
could also be used in geothermal areas that do not have
enough steam pressure to drive a turbine or ice island
research stations where energy sources are limited at
best.
Manning's design closely paralleled the construction
and operation of a low pressure, closed loop steam
plant. His Freon plant would have a heat exchanger; low
pressure, high expansion turbine; governor; condensor/
expansion chamber; feed pump; electrical generator; and
the necessary system controls and monitoring devices .
The four-by-five-by-six inch heat exchanger is made
from V2-inch 0.0. (outside diameter) hydraulic tubing
arranged in three rows on two-inch centers with a total
surface area of 53.7 square feet. Steam-type pressure
flanges rated at 600 psi (pounds per square inch) connect
the pipes carrying hot Freon from the heat exchanger to
the jet harness on the turbine unit. These connections
provide great strength while allowing a slight amount of
movement. Valves placed in both the supply and return
lines enable manual shutdown and complete isolation of
133
the heat exchanger from the rest of the system.
One-inch 1.0. (inner diameter) stainless hydraulic
tubing runs from the heat exchanger to the jet harness.
The jet harness feeds 16 jets up to %-inch diameter. The
size used depends on the outside temperature conditions,
load factor, and type of Freon used. A butterfly valve in
the pressure feed line controls pressure input to the
turbine. A governor built as an integral part of the
turbine assembly controls speed fluctuations.
The low pressure, high expansion turbine consists of a
sliding rotor, governor mechanism, and evacuated
housing. The self-throttling feature Manning used is
important because the Freon gas pressure will change
wi th the ambient temperature change . The governor
mechanism is a flyball arrangement that physically
moves the rotor as speed increases. Turbine fins are cut
so that as the rotor slides with the increase in speed, they
restrict the amount of Freon gas allowed to enter the
rotor area. When resistance causes the rotor to slow, the
governor action causes more gas to enter the rotor
chamber producing more thrust, overcoming the resist-
ance. This action keeps rotor speed relatively constant
under varying load conditions.
The 10-by-24-inch expansion chamber has a two-by-
seven-inch deep liquid collector at the far end. A pres-
sure /vacuum seal between the chamber and the turbine
housing ensures that this joint will be both pressure and
vacuum tight. The housing is designed to operate at
pressures up to 26 psi and temperatures exceeding -40
degrees. Although this may seem like a bit of overdesign-
ing, the prototype system experienced even colder tem-
peratures during actual operation. "I have no idea what
the max was," says Manning, "the temperature went
clean off the scale, maybe -80 or more:'
A magnetic, impulse-activated sole noid drives a spring
powered feed pump to return liquid Freon to the heat
exchanger. As the level of liquid Freon in the bottom of
the expansion chamber rises to a predetermined level, a
magnetic float/reed switch operates, activating the
pump. Freon is drawn through a one-way valve into the
heat exchanger feed line. Liquid Freon will flow until
liquid level in the collector area of the expansion
chamber falls enough for the reed switch to open.
The generator is a Homelite, singlephase, 2 .25
kilowatt, 110-volt, 60 Hertz unit operating at 3 ,600 rpm.
This generator was chosen because Manning knew it to
be well made, dependable, and requiring very little
maintenance . Also, it has a taper-drawbolt type of
connection that allowed true concentric coupling of the
turbine to the generator. Manning modified it so that
monitoring instruments could be attached to the outer
housing.
The instrument monitoring panel has a frequency,
voltage, and amp meter. Additional monitoring devices
include temperature probes placed in the heat exchanger,
warm water supply, turbine housing, expansion cham-
ber, plus a temperature probe placed in the atmosphere
near the expansion chamber and outside the test build-
ing . This configuration allowed monitoring of the heat
exchanger, the effect of high and low load conditions on
the expansion chamb er, and the effect of ambient air
temperature on the efficiency of the system.
A pressure gauge is also located on the pressure line
between the heat exchanger and throttle valve, between
the throttle valve and the jet harness, and on the turbine
housing directly over the turbine fins.
Performance
The prototy pe unit was housed in an eight-foot square
building on skids placed over a hole in the ice of the
Chena River. The building shields the equipment from
the e lem ents and allowed for artificial heat fo r greater
experimental control of the a mbient air temperature.
Start-up of this system requires the operator to gen-
erate an artificial vacuum in the expansion chamber and
to prechill the condenser walls. As the system is turned
on, the expanding Freon gas chills the expansion
chamber below the condensing point of the Freon ,
causing a partial vacuum. Because the feed pump creates
a pressure of 18 psi on one side of the turbine, and the .
expanding Freon itself creates a vacuum o n the other s1de
(about eig ht psi) a pressure difference of approximately
26 psi is actually created within the system during
normal operation .
After initial start-up, the prototy pe was allowed to
operate continuously for a week with 12-hour checks.
Then the unit was shut down and dismantled for inspec-
tion. A second five hundred hour test was then run.
After the lo ng test , the system was again shut down for
inspection. Prior to breakup, the test building, prototype
unit, and heat exc hanger were removed and test results
tabulated .
Manning found that although his device did produce
electricity, system control was more difficult than orig-
inally expected. The non-linearity of the expansion of
the Freon made speed contro l difficult using only the
134
Arthur Manning (above left) explains the unique design of his
sys tem . (Right), shown here are electrical gauges and the un-
m achined turbine used in the design
s imple spring/flyball arrangement and sl iding rotor.
"The system either tries to run away with itself, or shuts
down ;' said Manning, who feels that a more sensitive
contro l system may help solve this problem.
It was also found that the heat exchanger configura-
tion did not allow optimum heating of the Freon; but,
because the Chena River supplied more than enough
"warm" water, the ori gi nal design was adequate . In other
situations, the design may need to be modified.
Problems and Conclu sions
"You 've got to b e kidding :'
This just about sums up the technical assistance
Manning got throughout this project. Relying on per-
sonal creativity, many hours of research, and belief in his
own ideas was what Manning used to prove his theory.
Al though his Freon powered generator is not cheap and
cannot compete with today's fuel prices, it did work.
In making it work , Manning had to overcome funding
problems, extreme temperature effects on metal and
gaskets, speed contr ol at those varying temperatures:
and a lack of supporting information. He was essentially
on his own.
Early in the project, funding delays by the federa l and
s tate agencies caused costly project delays. The U.S.
Department of Energy reduced the requested funding for
the project by 30 percent. The funding reduction and
delay caused Manning to change the expansion chamber
design as the or igina l model was no longer available by
the ti me funds were received .
With little support from the university, turbine design
was based on the hope that the extreme cold temperature
would not critically affect the metal. As it was, the metal
held up fairly well ; only one of the fly balls used in t he
governor cracked from the cold. Although the tempera-
ture extremes were greater than originally calculated,
increasing system efficiency, it pressed the seals and
gaskets in the prototype to thei r limits. The temperatures
of the lubricants decreased their effectiveness, which
increased friction. Further developments in these areas
will probably have to be done before a suitable material
or lubricant is found.
"In small scale operations, it's almost impossible to
control speed accurately without costly electronics or
computer controls;' Manning adds, "large scale units
would be more efficient because they wouldn't be as
touchy:' However, when Manning approached devel-
opers for additional support in this project (a proven
135
concept), the common response was: "You've got to be
kidding:' It now sits in boxes in Manning's machine
shop, waiting for another chance.
Funding
U.S. Department of Energy
State of Alaska
Grantee
Arthur Manning
P.O. Box 10013
Fairbanks, Alaska 99701
$4,547
4,547
A water-powered
refrigerator
Don Baile y is keeping his f o od chilled by circulating
cold well water through an innovative refrigerator that
doesn't use electricity.
It 's also saving him about $3 to $5 monthly on his fuel
bill.
But there are a few drawbacks.
Bailey ca nnot keep ice cream frozen, make ice cubes or
keep his milk very cold because the refrigerator never
gets colder than about 43 degrees .
"Our refrigerator keeps liquids at about 43 to 45
degrees -a little warm;' said Bailey, who lives in Anchor
Point on the Kenai Peninsula in Southcentral Alaska.
"As long as the water flows, the refrigerator works
great. When no one is at home, the system doesn't work,"
he said.
Design
Bailey modified a used upright free zer and installed
more than 40 feet of coiled, three-quarter-inch fin tubing
on its interior walls. Almost all of the interior surface of
the freezer was covered to increase the amount of water
flowing through the system .
Bailey also said he selected a freezer because it is better
insulated than a refrigerator and doesn't have a separate
freezer compartment, making the fin tubing installation
easier. All fin tubing was soldered securely to the refrig-
137
erator's interior walls so that vibrations didn't break the
fittings loose.
The fin tubing is linked with Bailey's water supply
from his well . The pipe from the well's holding tank was
insulated to keep the water temperature as low as possi-
ble . The water temperature ranges between 34 to 40
degrees.
The water, however, only circulates through the refrig-
erator when someone in the house turns a faucet on
because the water flows through the refrigerator on its
way to the faucet.
"Everytime someone flushed the toilet , took a bath,
did the wash or did dishes-cold water would circulate
through our refrigerator, cooling the interior and its con-
tents," Bailey said.
Before installing the system, Bailey flushed water
through the used fin tubing for over a day and used
Clorox to disinfect the inside of the tubing.
Fin tubing that has been used in a heating system
should not be used later for a domestic water system
because you can never be sure what may have contami-
nated the pipe . For example, had toxic antifreeze once
been used in the fin tubing, water circulated through the
system could not be used for drinking or cooking. Where
national plumbing codes are in force , this practice is not
allowed.
The interior (left) of Don Bailey's water-powered refrigerator.
Bailey shows the oil furnace he converted to wood (above).
Two valves were installed in the water line so that
Bailey has the option of having water bypass the refriger-
ator. The second valve, placed in the lower part of the
pipes, enables him to drain water from the coils for
repairs or cold weather shutdown.
Performance
Bailey is generally pleased with his refrigerator. It was
simple to build and has been almost maintenance-free.
Also, it's helping him reduce his electric bill.
"All items, except milk, keep well in our refrigerator;'
Bailey said.
The major drawback is that there is no way to keep the
138
refrigerator cool when there is no one at home for a day
or two to run water. One solution is to leave a faucet
dripping, but then the well pump has to run unnecessarily
when no one is at home.
Bailey also had to increase the well pump's pressure to
provide the desired pressure at the faucets. The extra
piping through the refrigerator causes a greater pressure
drop between the pump tank and the faucets.
Funding
U.S. Department of Energy
State of Alaska
Grant Recipient
Don Bailey
Box79
Anchor Point, Alaska 99556
$200
$200
Bush refrigerator an I ti?JI I ~~ I ~ I £ I
unqualified success ·:' alii ~
Out near Trapper Creek, going to the store can be a bit
more involved than walking to the end of the block or
driving to market. First, you stoke the trusty wood stove,
tossing in a couple of extra logs for good measure; then,
move all the water containers closer to the stove so they
won't freeze when the fire burns low; finally, high-tail it
three miles through deep snow to the nearest store . Don't
stay long, because you have to be back at the cabin
before the houseplants freeze.
Trapper Creek is a small community near the Parks
Highway some 100 miles north from Anchorage. This
small homesteading and gold mining community has
about 200 year-round residents sprinkled among dense
stands of spruce and birch. For these people, the area
offers natural beauty and seclusion, yet easy access to
one of Alaska's major highways, and on clear days a
spectacular view of North America's largest mountain,
Mt. McKinley (Denali).
Perry Hilleary was building a house on his property
near Trapper Creek early in 1980 and thought that it
would be nice to be able to leave home for a couple of
days without fear of freeze damage. While he was at it,
he figured to tackle "Bush refrigeration" too.
In the fall of 1980, Hilleary received an AT grant to
build both the heat storage and refrigeration systems,
plus record data illustrating the success of the project.
Design and Construction
Each section of this two-part project had the same
development criteria: materials had to be easy to install,
maintain, and operate ; they had to be inexpensive; and
they had to be energy efficient. In return, the two
systems would provide some of the comforts that urban
folk take for granted and rural dwellers dream about.
The heat storage system begins with a seven-foot-
eight-inch by twelve-foot-eight-inch by fifty-four-inch
deep concrete block structure built in the basement of
the cabin. Four-inch Thermax brand Polyisocyanurate
insulation was used to line the inner surface of the box
and the leveled box floor. After a layer of sand is applied
to the bottom, a horizontal three-pipe grid of four-inch
ventilated tubing was placed across the short axis of
the heat sink. Each horizontal tube has three , four-inch
ventilated pipes rising vertically from them. Above this
is another grid of one-inch copper tubing. The copper
tubing is looped along both sides of the vertical risers,
crossing the horizontal tubes at right angles and the
entire struct1,1re is backfilled with a compacted clay/
sand /pea gravel mix ture . Hilleary believes that this
desi gn distributed heat better within the heat sink.
Another four inches o f Thermax tops off the heat sink.
The copper tubing feeds through the concrete block
wall of the thermal mass into a furnace /control area.
Here, they connect to an ex pansion tank, pressure relief
valve, and heat coils from the 55-gallon drum /barrel
stove. Originally, a small battery-driven pump was used
to push the antifreeze solution through the heat sink.
The battery was kept charged by a small portable gen-
139
erator. However, this pump was quickly discarded when
Hilleary found that the liquid was flowing too fast
through the heat sink to give up heat. Thermoconvection
now propels the antifreeze through the system .
The second part of this project involved building a
semi-passive "Bush refrigerator:' By using a drawer-type
of refrigerator instead of the standard door refrigerator,
Hilleary hoped to decrease the cooling energy enough to
make a simple, but effective system.
The refrigeration chamber is located under aU-shaped
kitchen countertop. A wood cook stove is at one end of
the "U" and a propane stove at the other. The cooling box
is insulated by a two-inch thick rigid Thermax. Attached
to the back wall of this box is a serpentine loop of
1/z -inch copper pipe. One end of this tubing exits the
cooling cabinet and runs along the underside of the
countertop to the wood cook stove. It rises along the
backside of the cookstove fluepipe , held on with metal
straps, and exits the cabin near the ceiling. The pipe then
drops into the ground in a long 60-foot loop beside the
house and returns through the log wall to the lower end
of the serpentine loop in the cooling cabinet . An anti-
freeze solution fills the copper pipe.
When the woodstove is being used the antifreeze is
heated slightly, causing a convection flow up through the
pipe. The liquid flows down through the ground, cools,
and then returns to the refrigerator. When the woodstove
is not in use, a small battery-powered, 12-volt pump pro-
vides the needed circulation . Through experimentation,
Hilleary discovered that a continuously running pump
pushed too much liquid. A switch from a car windshield
wiper is used for intermittent operation. The pump runs
for one second, then rests for 13.
The drawers are also customized for different food
container sizes . One has an egg tray. The bottoms of the
drawers are made of wood slats for better circulation .
Performance
The first part of the project (the heat sink) worked
even better than expected. Hilleary originally calculated
that the thermal mass could store up to one million BTUs
of heat. Even with the small pump removed, however, it
was determined that the mass could store enough heat to
supply the house with about 465,000 BTUs of heat per
day for up to three days without additional heat input.
The ability to selectively uncover only the amount of
thermal mass needed to keep the house above freezing
greatly enhanced the effectiveness of the system .
Storing heat in the heat sink also saved on fuel require-
ments because it allowed a more efficient , hotter fire to
be burned in the barrel stove.
The "Bush refrigerator" was an unqualified success.
The R-8 Thermax, combined with the simplicity of the
system, resulted in an easy to install, relatively energy
free system. Outside energy is required only during the
summer when the wood stove is not used. Then only
periodic charging of the battery is required. The addition
of a small solar powered pump would reduce this power
requirement to zero. Measurements indicate that the
refrigerator effectively cools foods to about 40 degrees
with a ground temperature variation from 39 to 44
degrees .
Problems and Conclusions
Hilleary encountered few problems building either
system . He has successfully shown others that a heat
storage and heating system and a "Bush refrigerator" can
both be built with less than $1,000 in materials. Now,
whenever Hilleary goes out to the store, he can stay a nd
chat for a while.
Funding
U.S. Department of Energy
State of Alaska
Grantee
Perry E. Hilleary
Box21
Trapper Creek, Alas ka 99688
$432
432
In Perry Hillea ry's home (ab ove) n ear Trapper Creek. the kitchen dra wers are
refrigerat ed.
140
I
Kenai City Hall saves
energy
Since 1981 an air-to-air heat exchanger has helped the
City of Kenai save energy by pre-heating air circulated
through City Hall. The prewarmed air for the ventilation
sys tem has meant less demand on the building's oil-fired
heating system.
The exchanger recaptures heat from exhaust air and
uses it to preheat fresh air as it's drawn into the
12,000-square-foot government building from outside.
The south wall of the building also is made of triple-
glazing for solar heat absorption.
Howard Hackney, city building inspector for Kenai ,
said the system is working well and has not malfunc-
tioned. He said it works at about 66 percent efficiency.
And architect Carmen Gintoli estimates the exchanger
has reduced the city's annual oil consumption by about
3 ,279 gallons.
"It's always on," Hackney said. "It picks up the heat
from the exhaust air and tempers the incoming air:'
System Design
The heat exchanger, manufactured by the Q-Dot
Corporation, was installed in a duct o n top of the city
hall roof.
The duct, which is about eight feet square, is parti-
tioned into two sec ti ons; one for incoming air and the
other for ex haust air. Fans continuously expel exhaust
air from the building and replace it with fresh air.
The air-to -air heat exchanger, which is about five feet
wide by 10 feet long, was installed inside of the big duct.
The heat exchanger has a center assembly with rows of
protruding aluminum fins that span across both the duct
for incoming air and the duct for exhaust air. (The
system is partitioned so that the exhaust air does not mix
with incoming air.)
141
The heat exchanger is mounted on a til table axis to
control the flow of the Freon that is used to conduct heat
to the fin assemblies.
When the heat exchanger is tilted toward the exhaust
duct, liquid Freon flows into the fins bathed by the hot
air. As the Freon absorbs the heat , it converts to a gas
which rises upward into fins spanning the cooler incom-
ing air duct.
As the cold air absorbs the heat from the fins , the gas
converts back into a liquid and flows back down to the
exhaust side to be heated up again.
In summer, the heat exchanger can either be shut down
or used to cool incoming hot air by tilting it so that the
liquid Freon flows into the fins spanning the incoming
air duct.
During mid-winter, a hot-water boiler also is used to
provide supplemental heat for the building.
Performance
City officials say they are pleased with the heat
exchanger. They say it has been working well and has
required little maintenance . Architect Carmen V. Gintoli
estimates that the system saves about 365,719 BTUs per
hour, conserving about 3,279 gallons of fuel over the year.
Funding
U.S . Department of Energy
State of Alaska
Grant Recipient
City of Kenai
P .O. Box 3504
Kenai, Alaska 99611
$4 ,225
4,225
A wastewater heat
exchange system
Every time someone takes a shower, runs a dishwasher
or washes clothes-precious heat is lost as the water
swirls down the drain.
But Mark Gudschinsky has designed a compact, vir-
tually maintenance free system to help homeowners
recover heat from wastewater.
It's called a greywater heat recovery system.
"It definitely works real well;' says Gudschinsky, a
plumber and apartment owner in Fairbanks, Alaska .
"And I'm going to put it in the other buildings I own'.'
Before installing the system , however, Gudschinsky
suggests that homeowners make sure that they produce
enough wastewater-at least 3,000 gallons monthly-to
make the system cost effective . Also, he advises against
installing the system if it will require major plumbing
changes.
Gudschinsky's system preheats the domestic water by
as much as 40 to 50 degrees before it enters the hot water
heater. And it's helping him save some $300 annually on
his hot water heating bills .
Better yet, the system is compact and virtually main-
tenance free.
"I put mine in the laundry room corner;' Gudschinsky
said. "My goal was to make this so it would be out of
sight and out of mind. I didn't want pumps and stuff. I
wanted absolute simplicity'.'
143
HEAT EXCHANGER, WATER
System Design
The greywater heat recovery system consists of a three-
to-four gallon sealed, steel tank, with three-sixteenths-
inch walls . It is 24 inches long, 16 inches high and 6
inches wide.
Wastewater from the showers and dishwasher flows
directly to and through the tank before being discharged
into the city sewer lines.
Cold, incoming domestic water is piped through the
tank through two Crane finned copper coils , which are
immersed in the warm wastewater tank. The system
raises the temperature of the domestic water by as much
as 40-to-50 degrees, before it flows into the oil-fired hot
water heater for warming to household use temperature
(110 to 120 degrees).
Small thermometers measure the temperature of the
greywater and of the domestic water as it enters and exits
the sealed tank.
Gudschinsky also experimented with two variations,
but found that they were not cost-effective.
One variation consisted of segregating dishwasher and
washing machine water by moving it through the tank in
a copper pipe enroute to the sewer system. This was to
prevent contamination of the greywater (from sinks and
showers) with food and dirt sediments .
Gudschinsky, however, does not recommend install-
Mark Gudschinsky (above left) explains the details of his
in vention. (Above right), a manufactured coil collects h ea t
from wastewater.
ing a separate copper pipe for dishwater and washing
machine wastewater because it increased the cost of the
system by $300 and because tank contamination is not a
problem.
Gudschinsky also tested a waterjacket arrangement,
which consisted of installing a small pipe inside of a
wider tube. The greywater flows through the inner pipe,
heating the domestic water which encases it.
This design, however, did not work out because a
homeowner would have to install a waterjacket about
60-to-70 feet long to obtain satisfactory temperature
increases, he estimated.
Performance
Gudschinsky's greywater heat recovery system is per-
forming better than he expected.
It boosts the temperature of his domestic water from
about 42 degrees to 80-90 degrees before it enters the hot
water heater.
This saves at least 168 to 336 BTUs per gallon of hot
water used, he calculates. For a 15-minute shower using
30 gallons of hot water, 5,000 to 10,000 BTUs will be
saved, which is about one-twentieth to one-tenth of a
gallon of oil for a heater firing at 80 percent efficiency,
Gudschinsky said.
In Fairbanks, this means a 6 to 14 cents in savings per
shower, no small cost reduction for apartment managers
or tenants.
Tips
Gudschinsky says he's learned several things from his
project:
• Homeowners should make sure that they can recycle
the heat from enough hot wastewater to make the
project feasible. As noted previously, Gudschinsky
considers 3,000 gallons of water monthly usage a
minimum.
• Do not install the system if it will require major-
and expensive-changes in the plumbing.
• Consider insulating the house first and other conser-
vation measures, before installing the wastewater
heat exchanger system .
Funding
U.S. Department of Energy
State of Alaska
Grant Recipient
Mark Gudschinsky
1608 Laurene St.
Fairbanks, Alaska 99701
$3,495
3 ,495
Heat exchanger cuts fuel
bills
Instead of tossing out hot water used for bathing,
cleaning and washing, Richard Runser is recycling it to
pre-heat his domestic water.
The system, called a greywater heat exchanger, has
helped slash his water heating bills about 40 percent.
In fact, it's working so well that he's even designed a
more compact version of his heat exchanger that could be
installed in new homes.
"I think it's wonderful-it's one of the few successes
I've had;' says Runser, who has dabbled in solar energy,
heat extractors and other alternative energy devices. "I
really believe this would save a lot of energy for home-
owners, commercial users, and industries:'
Runser, a science teacher at East High School in
Anchorage, says the high costs of energy make it
desirable to conserve wasted heat. This philosophy of
energy conservation also is practiced by his family on
their five-acre farm in the heart of the Matanuska Valley
north of Anchorage. They built their own house and
raise goats, pigs and sheep, not unlike the colonists who
came to the Valley in 1935 under the New Deal. The
government program gave the colonists 160 acres to
clear, farm and live upon . Today, the Valley remains as
Alaska's rural agricultural center.
Moreover, the greywater heat exchanger is simple to
build and install in a home, apartment building or com-
mercial enterprise, he says.
'This project is intended to develop and test a heat
exchanger system which will remove much of the wasted
heat and recycle it to the domestic hot water heater;' he
says. "Some of the recovered heat may be diverted to the
144
toilets where it is needed to prevent condensation around
the toilet and the resulting damage from the moisture:'
System Design
Runser's heat exchanger is based on piping cold water
through a larger tube filled with hot waste water from
the sinks and showers (known as greywater). Heat from
the wastewater warms the domestic cold water as it flows
to the hot water tank. The wastewater passes out of the
heat exchanger to the sewer.
The heat exchanger, installed in Runser's basement, is
formed of four, six-inch PVC plastic pipes. The pipes are
linked to form two upright U sections. He sealed the four
tops of the vertical PVC sections with urethane foam.
Hot wastewater flows down and up one U-section
before flowing through the second U-section. These two
U-sections segregate the greywater into four different
temperature zones.
Domestic cold water flows through three-quarter-inch
copper pipe in the heat exchanger. It moves in the
opposite direction as the wastewater.
The domestic water flows through the two U-sections,
gradually moving from colder to warmer wastewater.
The temperature of the cold water can be increased by
over 40 degrees .
Runser also installed gas vents at the top of each U-
section. The gas vents are connected to the home's sewer
system . There also is a clean-out plug at the bottom of
each U-section to allow for any cleaning of sediment or
sludge build-up.
Performance
Overall, the heat exchanger has functioned with out
any problems since it was installed in the winter of 1980.
Incoming and outgoing greywater and cold water tem-
peratures have been measured with thermometers to
evaluate the system's effectiveness.
Runser discovered th at the cold water temperature has
been increased by as much as 46 degrees. He estimated
that his heat exchanger is he lping him save between 30 to
SO percent on his hot water fuel bills.
Moreover, Run se r's heat exchanger is compact enough
to be installed in a lm os t any new home with only a
minimal increase in cos t .
145
"It could be adapted for any h ome:' Runser says. "It
would be extremely simple to build. And I'm really con-
vinced it is an energy-conserver . It ex tracts heat out of
the wastewater before it goes down the drain:'
Funding
U.S . Department o f Energy
State of Alaska
$971
971
Grant Recipient
Richard Runser
SRA 6289 Yadon Drive
Palmer, Alaska 99645
A ppropriate technology is seco nd na ture t o
the Runser fami ly (a bove). Richard Runser
(far left) discuss es the details of his system
design . (Left), an indoor/outdoor thermom-
eter is used to m easure incoming and out-
going water temperatures.
Computer prioritizes
wind energy use
A microcomputer was installed in Stanley Baltzo's
home in Kodiak, Alaska to regulate electricity produced
by a wind generator.
'The computer related demand to supply on a priority
basis ;' says Baltzo, a product manager for Prudhoe Bay
Supply who now lives in Wasilla, north of Anchorage.
"It was a sensing device that would determine where
the need was and reroute the electricity to meet that
need'.'
First, electricity was used to light the house. Once that
demand was met it was used for the hot water tank and
home heating . Any additional power was sold back to
the Kodiak Electric Association for about 7 to 9 cents a
kilowatt.
Overall, Baltzo said the computer-monitored wind
generation system worked well, reducing his monthly
electric bills from $3 to $150 depending on how much
the wind blew.
The biggest setback he faced was making his wind
generator work properly. He had to replace the governor,
put shorter blades on the machine, and reset the angle
of the gear head to increase the distance between the
whirling blades and the tower.
But once the wind generator was repaired for free b y
Jacobs, the manufacturer, everything worked well.
147
MONITORING AND TESTING
"It definitely worked after the bugs were removed from
the Jacobs wind generator;' Baltzo said. "It required nor-
mal watching . I was absolutely pleased with it. If I had
to do it all over a gain , I wouldn't hesitate if I lived in an
area with viable wind energy '.'
System Design
The commercially-built microcomputer panel, about
eight inches by 12 inches, regulated electricity produced
by a wind generator.
The microcomputer was an Ohio Scientific C-2 OEM-
NET. Its components consisted of a 6502 processor chip
with 32 bytes of dynamic random access memory, a
CA-15 universal telephone interface board, CA-20 time
clock with battery back up, a CA-12 96-line parallel
I/0 board and an OSI 538 Eprom board with 32 K of
erasable, programmable memory.
Every tenth of a second the computer monitored heat
demand and the domestic hot water temperature, and
stored all the data in its memory.
Meanwhile, electricity was produced by a 10 kilowatt
Jacobs wind generator, which is intertied with the Kodiak
Electric power.
The generator was placed atop a self-supporting,
80-foot-high tower. Each leg of the tri-pod tower was
A wind system (left) on the Kodiak shorelin e catches sea
breezes.
anchored six feet in bedrock with cement.
The blades, originally 12-feet long, were replaced
with 11-foot-long laminated spruce blades to reduce the
chances of the blade hitting the tower as winds shifted.
Power from the generator was channeled through a
commercially built "mastermind" Jacobs control panel.
Since Baltzo was tied into the local electric company,
he did not use batteries or other back-up energy systems.
He purchased power from the local power utility only
occasionally when his wind generator failed to produce
enough power.
Performance
Baltzo was very pleased with his energy system after
he was able to "get all the bugs" out of the wind gener-
ator. He said it required little maintenance, and it helped
him lower his electric bills substantially.
He says the problems with the generator were likely
caused because it was the first Jacobs 10 kw wind system
to be installed in Alaska.
The blades of the machine, for example, smashed
against the tower within the first 30 minutes of its oper-
ation. He doesn't know what caused the accident , but
said the spruce blades have solved the problem . In-
creasing the angle of the gear box from 9 degrees to 13
degrees also prevented the blades from hitting the tower.
Overall, he says he was very pleased with the system.
In fact, he says that if there were enough wind around
his new home in Wasilla-he'd install a similar system
there too.
Funding
U.S. Department of Energy
State of Alaska
Grant Recipient
Stanley A. Baltzo
SR Box 5232
Wasilla, Alaska 99687
$3 ,076
5,175
Automatic stack dampers
installed
It was an article reviewing automatic stack dampers in
the January 1980 Consumer Reports that motivated
Thomas Busch, general manager of radio station
KNOM , to see if these devices could help reduce high
yearly fuel costs .
The nonprofit Nome station nestles in a town known
for its Gold Rush beginnings, brutal winter cold, vicious
ocean storms and Front Street finish for the 1,049-mile
Iditarod Sled Dog Race.
The article indicated that stack dampers (devices that
keep heat from escaping up the chimney when the fur-
nace is off) could give up to 23 % fuel savings . In Nome,
on the southern shore of the Seward Peninsula and only
three blocks from Norton Sound, the possibility of 23%
savings bore investigation .
Busch started checking with o thers in the area and
found that very few people, if any, had ever heard of
a stack damper, let alone had installed one. Even the
Cooperative Extension Service could offer no hard facts.
If these devices could save him money, and since non-
profit KNOM was "more desperate than most to save
money;' Busch decided that it was time for the small
station to do its own research .
Fuel savings could be calculated easily. KNOM had
already been hauling its own fuel since late 1980 and had
records for its non-damper consumption. Recording fuel
consumption during the same period after damper instal-
lation would allow an easy comparison .
In 1981, KNOM and Busch received a grant to install
stack dampers in five furnaces and monitor the results.
The results would then be compared to a corresponding
period without the dampers and fuel savings calculated.
148
Design and Construction
Furnaces in five buildings used by KNOM were fitted
with motorized Flair brand stack dampers. The stack
dampers were installed above the customary barometric
damper. Theoretically, the stack dampers would dramat-
ically improve the efficiency of the furnace by closing the
chimney whe n the burner was off, preventing heat loss
from the fire chamber and from the area w here the fur-
nace is located. The damper must open before the burner
can start. A built in safety feature a lso opens the damper
if there is a motor or power failure.
The furnaces included both water boilers and hot air
furnaces . The buildings ranged in size from 640 square
feet to more than 4600 square feet. Although two of the
furnaces also provide hot domestic water to the build-
ings, the fuel savings would still be interesting, Busch
reasoned .
Performance
'The analysis was a surprise, indicating quite varied
results-results that appeared to be in variance from
subjective impressions;' said Busch. "I lived in one of the
buildings and it was clear to me that after the stack
dampers were installed, the furnace ran less often. Yet,
the data indicated a 6.5 per cent increase in fuel con-
sumption;' in his building, he said. Some of the other
buildings showed no gain, others showed only a slight
savings. "Cle arly, something was wrong;' said Busch .
Different theories suggested fuel theft or leakage, but
Busch feels that the poorly insulated buildings were
affected by heat loss from wind. One reason that the data
may be inaccurate is that the oil consumption analysis
did not determine a gallon per degree day, but rather a
gallon per year figure, for the b efore a nd after data .
Buildings in Nome are n ot known fo r thick insulati on.
Th is, combined with the fact that Nome is a very tran-
sient town means that upkeep may not be up to profes-
sio nal s tandards, either. Busch's h o use also had a settling
problem. "I've used a b out a half d ozen tubes of caulk
this year alone, just sealing th e cracks;· sai d Bu sch, "a nd I
can feel drafts again'.' This indicates that the settling
problem a nd air infiltration may be the most probable
c ulprits.
The dampers themselves, however, are vi rtually main-
tenance free. Only o ne h a d to b e replaced, a nd that was
b eca use of incorrect installation a nd not due to a faulty
mechanism .
Conclusions and Problems
The only real proble m w ith this project was that n o
o ne in Nome had ever installed a stack damper before .
After learning on the firs t one, the remainder were a
snap, Bu sc h said.
149
The project itself stimulated a little interest, but little
su ccess in getting others to install the dev ices. Better
result s mig ht have changed this, but Nome is affected by
other problems. One of them was transience; a commo n
remark to Bu sch was "s ure it will save a couple percent
(fuel usage) but I'll only be here for two years .. .'' Busc h
also found some resist a nce to the dampers from "the old
t imers and contractors:· He feels that this attitude is
changing, a nd that the future may find more of these
devices in Nome.
Funding
U.S. Depa rtment of Energy $1 ,150
Grantee
KNOMRadio
Thomas Bu sch , General Manager
P.O. Box 988
Nome, Alask a 99762
To m Bu sc h (l eft ) initiated th e use o f s tack dam pers as an
energy -sa v in g device in the tow n of N o me.
Building a fire-proof
chimney
Several years ago, an apparent creosote build-up
caused a fire in David Norton's chimney. Fortunately, no
one was hurt and his home was not damaged .
But the incident prompted Norton to design a more
fire-proof chimney for his home in Fairbanks, Alaska .
"I thought there must be a better way to build a chim-
ney than to endanger the structural part of the dwelling,"
said Norton, a biologist at the University of Alaska-
Fairbanks. "A n engineering friend of mine had an idea:
why not build it (the chimney stack ) exterior to the
home? So we did it, and it's working quite well:'
System Design
The chimney system is comprised of three parts: a
wood stove, a buried steel trap that collects creosote, and
an 18-foot-high chimney stack. Hot gases flow through
a pipe from the wood stove to the underground steel trap
before swirling out of the chimney stack.
A six-foot-long, by six-inch-diameter steel pipe
connects the wood stove in the basement with a five-
foot-deep by 18-inch-diameter steel trap, which was
buried outside the basement wall. The chimney stack,
which rises above the creosote trap, was built three feet
away from the outer wall of Norton's house .
"The original intent was to put enough distance be-
tween the chimney and combustible structural materials
of the dwelling, so that, if creosote accumulations in the
chimney did ignite-there would be no threat to letting
the stack fire burn itself out;' Norton said.
The chimney also was designed to withstand high
temperatures. Stack fires can burn at 2,000 degrees-hot
enough for thin-walled smoke conductors to melt or
oxidize.
Therefore, Norton chose steel well casing with an
internal diameter of six inches and a wall thickness of
three-eighths-inch for the smoke conductor. It was insu-
lated with sections of asbestos-lined, double-walled steel
chimney made for use with Heatilator brand fireplaces.
These sections have an inner diameter of nine inches and
an outer diameter of 13 .5 inches .
Moreover, the 1 .25-inch-wide space betwee n the outer
and inner walls was filled with clean dry sand. The sand
annulus was tamped to prevent settling .
Norton also fitted the chimney system with two ther-
mocouples that register temperature on a digital readout
display. A stack fire warning instrument with analog
readout and a variable setpoint readout also was pur-
chased. It was installed in the pipe that connects the
wood stove with the creosote trap, to sa mple flue gas
temperatures under normal operations.
Performance
The chimney system worked well from mid-October
through March for several years . Mixtures of birch,
aspen, poplar, willow and spruce were normally
combined in a 2:1 ratio by volume with coal for each
loading of the stove .
When Norton gets ready to fire up the stove for the
first time each fall, he connects the b lower side of an
150
industrial vacuum cleaner to the air intake of the stove.
This prevents a reverse draft problem that could fill the
house with smoke.
Creosote does build up in the chimney's smoke con-
ductor, but not as fast as Norton originally feared.
Reduced draft is an indicator tha t creoso te has built up;
this occurs two or three times per heating season for
Norton's system. The pipe co nnecting the wood stove
with the steel trap can be cleared of this flammable
residue with a conventional six-inch chimney brush on a
rigid pole .
It's a little harder to clean the ver tical smoke stack
however. Norton lowers an old screw jack base (5 .75
inches in diameter) into the chimney and jigs it up and
down . If the jig becomes stuck, he drops a second roped
weight on top of the jack and jiggles it until both are
free.
Norton, however, has not determined how much heat
transfer to the dwelling is sacrificed by externalizing
the chimney or what the life expectancy of the present
system may be .
Deliberate Ignition of the Creosote
Norton said he could not cause a creosote stack fire
just by building a roaring blaze in the stove and operat-
ing it with all dampers open. By the time sufficient creo-
sote accumulates to sustain a stack fire, the draft in the
chimney is so weak that it cannot transfer sufficient heat
from the wood stove to start a stack fire.
On March 7, 1984, the University of Alaska Fire De-
partment assisted in a controlled burn-out experiment
when most of the season's creosote accumulation was in
the chimney system.
A p ile of wadded newspapers was ignited in the under-
ground creosote trap after it had been disconnected from
the wood stove. It took 15 minutes after ignition to gen-
erate a self-sustaining creosote fire in the vertical section
of the smoke conductor.
The combustion climbed slowly up the chimney,
reaching the level of the top sensor 120 minutes after
ignition. All creosote had burned, melted or fallen off
the inner chimney walls. The entire system began cooling
off steadily, except in the trap where glowing embers of
fallen creosote produced he at for about 24 hours.
Fears that he.at from burning creosote would build
up in the smoke conductor and melt the steel were un-
founded. Meltdown did not occur because heat was
transferred from the smoke conductor to the sand
annulus, and out of the double-walled Heatilator
sections.
No significant problems arose from the burn-out
experiment, but it is a dangerous undertaking . There is
a lways a risk of backflashing during oxygen regulation .
A backflash did occur when oxygen was restored after
starving the fire of air. Such backflashes can fill the
house with smoke, cover an unwary observer with soot,
si nge eyebrows, or damage property and injure nearby
people if sparks are shot o utward.
l
Overall, the experiment was successful and showed
that the chimney could be cleaned by starting a two-
hour stack fire far easier than a six-hour vacuuming
project.
Norton said t hat experts advise against letting creo-
sote fires burn in standard chimney installations . Besides
backflashing, he said, the stack fire causes considerable
noise and a ghastly pall of foul smoke. He said neighbors
downwind of the experiment would have been justified
in complaining.
Tips
Since most people may have little experience with a
chimney configuration such as his, Norton has several
tips:
• The pipe linking the woodstove with the buried
steel trap should be exactly level, rather than
slightly descending as it was inadvertently in-
stalled. This may prevent a creosote fire from
working its way backward toward the furnace
from the trap.
• Do not be alarmed by a "rainshower" sound in the
chimney trap when you start up the fire for the
very first time. The sound is caused by the con-
densation of water from combusted mater-ials on
151
David Norton and his dog (le f t) inspec t the
c himney of their Fairbanks home.
the walls of the vertical portion of the smoke
conductor. Eventually, the water evaporates.
• The chimney heats the soil surrounding the under-
ground trap. The area could be an ideal location
for a greenhouse, or the base of an attached solar-
ium. The heat also could be used for year-round
com posting next to the chimney.
• Be sure to seal off the sand annulus from moisture
and creosote. Sheet metal collars corrode in less
than a season; two masonry collars also have
cracked and disintegrated. Consider welding
a three-eighth -inch steel collar to the smoke
conductor.
• Use a masonry jacket for the smoke conductor
core, and retain a sand annulus to allow for
expansion and contraction of the steel in the
smoke conductor.
Funding
U.S. Department of Energy $1,460
Grant Recipient
David Norton
SR20787
Fairbanks, Alaska 99701
Monitoring system
collects useful data
"I realized that the project was going to be slightly
more complicated when I stood beside my pregnant wife
and watched the snow drift down onto the cabin. The
cabin itself was slightly tipped to one side, and its foun-
dations were sinking into the hole I had just excavated
for the greenhouse rockbed:'
Jeremy and Linda Weld were building an attached
passive solar greenhouse and rockbed thermal mass for
heat storage on the east side of their small log cabin . The
cabin is located on the crest of a hill , about 200 feet
above the Gulkana River, and 14 miles north of Glenn-
allen. Temperatures in the area range from a blistering 90
above to 60 below. Seasons change with a snap.
The greenhouse was an integral part of the Welds plan
to make their little homestead self-sufficient. In addition
to providing fresh vegetables, the greenhouse would also
supplement the cabin's heating system during the spring,
summer, and fall. During the winter, the greenhouse
would be closed down and the below ground thermal
mass placed in "hibernation'.'
Being a park ranger, Weld certainly knew about ani-
mals a nd hibernation, but little a bout arctic construction
techniques. When he began asking questions, he found
that he was not alone. Weld found that most construc-
tion in the area was at the builder's convenience rather
than to maximize environmental benefits. For ins tance,
"a new development near the Richardson (Highway) has
every house facing the road;' says Weld, "if the builder
would have turned the houses slightly to take advantage
of the sun, those homeowners would have considerably
lower heating bills'.' Weld also found that most written
information was "wrapped up in the technical aspects of
construction and offered little practical information for
the inexperienced owner-builder'.'
The greenhouse that the Weld's were building was
made possible by a grant from the Alaska Council on
Science and Technology. Jeremy and Linda felt that if
they could monitor the greenhouse and include perform-
ance data with construction information, a practical
example of passive solar construction for the Copper
River Basin would be available for others. In 1980, they
received a grant from the Appropriate Technology pro-
gram to install a monitoring system in the attached
greenhouse and also in a free-standing control green-
house.
Design and Construction
The original design called for a one-story, east facing
structure with a small below-grade rockbed thermal
mass . But as Weld was repairing his damaged cabin
foundation, the project grew "like a snowball rolling
downhill:' The small one-story affair grew to a two-story
"heating center': His greenhouse monitoring idea also
grew to a study of arctic building techniques and
materials.
In addition to his automatic temperature monitoring,
Weld planned to include the results of visual observation
in his final report. He felt that this would be more bene-
ficial to others attempting the same type of project.
152
The new greenhouse /heating center would have a
15-by-20 foot first floor with a 9-by-20 foot upstairs
bedroom. The newly repaired and reinforced hous.e
foundation was extended to support the addition . A
three foot deep, 12-by-16 foot depression below the main
floor houses the rockbed. Two layers of four inch-
urethane foam (salvaged from the Alaska Pipeline ) line
the depression to prevent heat seepage from harming
the permafrost eight feet below. Although the experts
recommended two-inch river rock for the thermal mass,
all that was available in the area was coarse sewer rock .
Embedded in the sewer rock are two perforated pipes .
These pipes are connected to a solid pipe that ends above
the ceiling separating the first and second floors. On top
of the sewer gravel, Weld layed a six-mil plastic vapor
barrier and then a layer of pea gravel. Finally, the floor
area is covered with a 31fz inch cement slab with narrow
slots cut in it above the thermal mass area to allow heat
to escape.
Post-and-beam construction using logs and rough cut
dimension lumber frames the a ddition. Discussio n s with
others w h o have built greenhouse s before convinced
Weld not to use the traditional angled windows because
they're difficult to seal. At the last minute, Weld decided
to put in two angled windows, to allow comparisons on
building techniques.
An insulated wall and door sealed the greenhouse
from the ca bin and six inches of fiberglass and water-
proof sheetrock isolated it from the second story bed-
room . The ceiling, backwall, and door are painted white
to ensure a bright interior, while all other walls are
covered with cedar. The insulated wall and ceiling was to
keep with "common wisdom that says the best thing to
do with a solar project in the winter is to isolate it from
the house'.' By the end of February, a new plan was
b rewing, and Weld was determined to find a way to use
the greenhouse throughout the winter.
The purchase of a small multi-fuel hot air heater was
the final step in the greenhouse's evolution. Using flou-
rescent lights during the winter, removable thermal shut-
ters and a removable 3 1fz inch insulated floor, Weld
figured he could minimize heat loss and almost double
the size of his house during the long cold winter. The
insulated floor would still let his thermal mass "hiber-
nate" during the winter.
The thermal shutters are made from two-inch , alumi-
num-clad urethane foam b o ards with a vapor barrier
stapled to the outside and decorative burlap attached to
the inside making an attractive and efficient barrier. Both
the shutters and the floor insulation are removed in the
spring and stored until late fall.
A medium volume, squirrel-cage blower mounted
atop a three legged two-by-four tower blows air into the
thermal mass inlet pipe. Another large, reversible fan is
mounted on the side of the greenhouse . Rated at 3 ,300
cfm (cubic feet per minute), this fan could quickly
evacuate the greenhouse, but was found to be very
expensive to run . Two smaller, low wattage fans help
move warm air from the ceiling to the floor reducing
stratification problems.
To ensure a complete picture of the solar environment
was recorded, Weld used two automatic thermometers, a
strip-chart recorder, visual observations of cloud cover,
and temperature sensors placed at various lo cations
throughout the attached and free-standing greenhouses
and thermal rockbed. The re sult s of these measurements
would be graphed and made available to various state
and local agencies.
The rockbed in the attached greenhouse and the
internal area of the smaller free-standing control g reen-
house were monitored on a daily and sometimes hourly
basis. At the end of the year's study, Weld collec ted his
data and discovered that the rockbed was coolest from
November through January, never getting beyond 40
degrees, then lo sing warmth quickly after the sun went
down. From February on, the rockbed increased both in
temperature and thermal capacity, reaching a peak in
early Jul y.
Since We ld 's ori ginal plan was to let the rockbed
"hibernate" during the w inter, he wasn't disappointed
when it wouldn't supply heat during the first winter's
use. Future plans are to draw heat directly from the
multi-fuel furnace in stead of the ceiling area between the
first and second floor. This heat would be injected
directly into the thermal mass. Although this would
mean higher internal temperatures for the rock bed, Weld
doesn't expect permafrost damage, but he 's "real worried
about it'.'
Another interesting thing that was discovered during
this project was the debunking of the "closed-buil ding
rule'.' This rule infers that all so lar structures should be
closed off and sealed from the rest of the home during
the winter months. Jeremy Weld discovered that by
defying thi s rule, heating performance actually im-
proved . "Closed, it not only looked terrible, it simply
didn't work:' His real problem wasn't isolation, but
rather infiltration. "If I were to build this structure again,
I would use a version of double-studded wall ;' he said. It
was vi rtually impossible to seal the corners of the post-
and-beam wall s. The only place that remained sealed
was the sloped w indows. This, by the way, was also the
j eremy and Linda Weld's greenh ouse (right) was under con-
struction during 198 1.
153
only part of the structure that worked well as a green-
house, the original purpose of the addition, and was
probably due more to the increased light from the sloped
windows than anything else.
Weld also found that although post-and-beam con-
struction is very attractive, it is virtually impossible to
seal. Normal wood expansion /contraction caused by the
Copper River Basin climate would leave small cracks
around the support beams. He tried many different com-
mercially available caulks and concluded that a bout the
only way to actually seal them from the outside was to
cover them up.
Tips
After building a n u mber of experimental walls, testing
insulation materials and techniques, and caulking com-
pounds, Weld offers the following tips for the amateur
owner-builder:
• Don't get wrapped up in the technical aspects of con-
struction, remember practical is better.
• The ability to ventilate moisture out of a wall is as
important as keeping moisture from entering it.
• When conflict arises between keeping out the winter
chill and letting in as much li ght as possible, better
to err on the side of more glass.
• Although proper insulation is important, air infil-
tration will de stroy any benefits of the insulation.
• Build to make maxi mum use of the environment,
i.e., solar gain, wind protection, etc.
• Finally, have a definite idea of what you want and
like before you pick up a hammer. Keep in mind that
the most important result of the building is not the
structure itself, but the improvement you feel in
your quality of life.
Funding
U.S. Department of Energy
State of Alaska
State of Alaska (Greenhouse)
Grant Recipient
Jeremy and Linda Weld
Box224
Gakona, Alaska 99586
$ 408
408
5,000
Demonstration project a
success
Once the site of the worl d's most profitable low-grade
gold mine, Juneau now hosts politicians, tourists, fisher-
men, and determined gardeners. Located a t the base of
Mount Juneau a nd Mount Roberts, Juneau is a short
drive sou th from the great Mendenhall Glacier Va ll ey.
Its location places Juneau a lmost directly in the path of
every storm crossi n g the Gulf of Alaska; consequently,
the area does not exhibit the most h osp itable gardening
climate. This means t h at those sun loving, high tempera-
ture vege tables either have to be imported, g iven -up, or
grow n in a climate-controlled greenhouse. Unfortun-
ately, these greenhouses are usually so expensive to build
and operate, that the owners cannot afford to grow those
items that the greenhouse was built to handle .
Stan Moberly felt o therwise. By usin g passive solar
principles, he though t he could successfully extend the
growing season and improve the climate fo r those special
vegetables without mortgaging his soul to the energy
companies. In 1979, Moberl y built his solar g reenhouse
and is amazed at h ow well it was working. After a
cursory canvassing, he found that "this solar greenhouse
is the only known solar greenhouse in this area of
Alaska that is utilizing stored solar energy to grow
vegetables and flowers;' and that it could "ser ve as a
154
demonstration project if careful records are kept:'
In 1980, Moberly was awarded a grant to develop a
monitoring system to keep th ose records. The project
would involve monitoring the climate both inside and
outside the greenhouse, recording the sun's daily
intensity, and keeping track of any supplemental
electrical energy usage. T he monitoring p roject would
last one year and the results would be tabulated for
public in terpretation.
Design and Construction
The 12-foot-eight-inch-by-16-foot south-facing struc-
ture sits in the rear of the owner's residence where the
garden used to be. Supported by a treated wood founda-
tion, the building is 11 feet high at grade and is sunk
a n other 14 inches in the ground to reduce a ir infi ltration
and to enclose a 235 cubic foot sand and gravel heat sink.
The two s ides, rear, and short front wall are framed
with treated two-by-four studs. The bottom two feet of
the sides and rear wall are insulated with styrofoam,
sheathed with treated plywood and have a vapor barrier
both inside the s h eathin g and stapled outside around the
bottom of each w a ll. Meta l flashing caps the treated ply-
wood. The remaining wall area is insulated with fiber-
155
Stan Mo b erley (p re vious page) takes a break dur-
ing the const ruction o f his g reenh ouse. (Above
and middle left ), two phases in the construc tion of
the g re en h ouse. A view (b ottom left) of the struc-
ture's interior w ith pla nts and seedlings.
glass, with a plastic vapor barrier attached to the inner
surface, and is enclosed with painted plywood. The ply-
wood is painted white on the inside of the building and
brown, to match the owner's residence, on the exterior.
The insulated roof is covered with white plywood on the
inside, insulated with fiberglass, and then covered with
corrugated green fiberglass sheets.
The south facing solar glazing is angled so that the sun
strikes it at exactly 90 degrees on March 21. The solar
energy passing through the corrugated clear fiberglass
and clear plastic inside is absorbed and stored by a
1,000-gallon water thermal mass. The water is stored in
discarded 55-gallon drums, five-gallon fuel cans, and
plastic storage bottles that are stacked across the north
wall.
A time-activated oscillating fan is turned on for one
hour every three hours to prevent thermal stratification
and to ensure equal temperatures throughout the green-
house. A thermostatically controlled wall fan and lou-
vered opening on the opposing wall purge the green-
house when inside temperatures get extreme.
Electrical outlets are located about half way up in the
middle of each wall for convenience. Other nice features
are the small sink and potting bench near the split dutch
entry door. The split door allows more ventilation in the
summer. Growing benches along the side walls and a
lattice in front of the thermal mass for climbing plants
complete the structure.
Performance
Although the location of the greenhouse resulted in
solar interference from both Moberly's and his neighbor's
house, the structure's design was so good that the inter-
ference never has caused any problems. Even during the
coldest months, the solar mass never went below 32
degrees. Because of this, and because electrical usage was
156
minimal, the power meter and solar intensity meter were
never used.
'Usually, the coldest temperatures in Juneau are during
periods of clear skies'; states Moberly, "this, of course,
allows more solar energy to be collected than on cloudy
days~ From all indications, Moberly built a successful
solar greenhouse and provided a mass of information for
others interested in passive solar construction.
As for those sun loving, high temperature plants,
"experimentation with various varieties of tomatoes
was tried" and "the variety that performed the best was
selected for growing thereafter:'
Conclusions and Problems
About the only real problem Moberly had building
this structure was accidently mounting the front ·and
back walls outside of the end walls instead of butted
against the end wall as designed. This added eight more
inches to the structure and added material costs.
"The greenhouse provided the opportunity to garden
over two months earlier than could have been accom-
plished outside, and the risk of late freezing temperatures
was eliminated:' writes Stan Moberly. For a serious
hobby gardener, a greenhouse full of flowers and vege-
tables is the true mark of success. ·
Funding
U.S. Department of Energy
State of Alaska
Grant Recipient
Stan A. Moberly
9414 Berners Avenue
Juneau, Alaska 99803
$1,415
1,415
Satellite aids in cordwood
inventory
During the early part of the century, before the Alaska
Railroad opened the Interior to the vast Matanuska and
Healy coal fields, the main fuel source for the Fairbanks
area was cord wood. Vast stands were slashed to fuel the
boats plying the Yukon and Tanana Rivers, after gold-
seekers created this 1903-incorporated city ..
Today, most of the remaining timber is either in pri-
vate ownership or in the hands of the state . Unfortun-
ately, the rising use of woodstoves as an alternative
energy source is putting stress on this remaining re-
source. This pressure has made resources inventory
important to determine what the sustainable yield is
for a particular area. Arbitrary cutting beyond this
limit may do irreparable damage to the resource and
reduce its availability to support future generations.
'Timber inventories, and those of other natural re-
sources, are usually managed by separate government
agencies. This type of management may or may not
reflect the actual availability of a resource to the local
community;' says Dr. William Stringer, associate
professor of geophysics at the University of Alaska-
Fairbanks Geophysical Institute . The main impediment
to inventorying cordwood potential is the cost of survey-
ing large , remote areas. Even using airplanes is costly.
Stringer's solution would have amazed those rugged
Fairbanksans of 80 years ago-the use of satellite tech-
nology that has been pioneered by Alaskans of another
age.
The need for a cordwood inventory was early recog-
nized in a February, 1980 meeting of the Tanana Valley
Development Council, which identified the need for a
cordwood inventory as essential for "future cordwood
use in the Fairbanks North Star Borough'.' Without this
knowledge it is virtually impossible to monitor this
resource for the benefit of future citizens and self-
reliance, said the council.
In 1980, Stringer and the Geophysical Institute
obtained an AT grant to develop a low-cost method for
inventorying cordwood. Stringer proposed to use high-
resolution satellite images and remote sensing techniques
for this purpose.
Project Description
Stringer and a research associate, Janis Zender-
Romick, proposed to use Landsat satellite imagery to
produce low-cost inventories of selected areas. Landsat
uses a series of polar-orbiting satellites to produce an
image of a particular area every 18 days. These images
are produced qy a variety of devices; one, a Multi-
Spectral Scanner (MSS) would be used for this project.
When finished , both a low-cost method of cordwood
inventory would be developed and a cordwood mapping
manual prepared so the technique could be replicated
elsewhere.
MSS is obtained both separately and simultaneously
in four wavelengths. It is also possible ·to obtain black
and white images representing the amount of light
reflected from the earth in each of these wavelengths.
Since different types of vegetation reflect different wave-
157
lengths of light and higher densities reflect more of that
wavelength, using both color and black-and-white
images, it is possible to roughly estimate the types and
densities of ground cover .
It was decided that the cordwood inventory process
would be developed in stages. First, satellite images of
the selected area would be obtained for both the summer
and winter. This would help determine both the types
and densities of ground cover.
Stringer and Zender-Romick chose Viereck and Little's
description of interior Alaska forests as a base for their
study. Viereck and Little's book, Alaska's Trees and
Shrubs, Agricultural Handbook Number 410, divides
Alaska's ground cover into six categories. These are:
• Closed Forests, consisting of white spruce, aspen,
birch, and poplar
• Open Forests, consisting of black spruce, small
birch, and tamarack
• Recent Burns, consisting of willows, saplings, and
scrub
• Treeless Bogs, consisting of willow, berries, dwarf
trees, and no cordwood
• Shrub Thickets, consisting of flood plain thickets
and elevated thickets
• Alpine Tundra
The next step was to determine which color in the
satellite photographs corresponds to a particular ground
cover type . This was done by using high-altitude aerial
photos in color infrared. Field observations were used to
classify the color blocks in the satellite photographs.
Analysis
The first stage in data analysis was to trace the color
boundaries from the summer satellite photographs. Four
main color scale classes were used: bright red; mostly red
with some mottling of blue-grey; dark reddish-purple;
and dark blue-grey to black . The winter photograph also
was divided into four categories: very bright; light grey
or brown; medium to dense brown; and dark black-
brown. These classes were subsequently traced onto a
topographical map and copies of that map were taken to
the field to determine the composition of each category
base on the information presented in Table 1. This was
done by direct observation or, if direct observation was
not possible, binoculars and aerial observation.
The information gathered from the field caused some
adjustments of the maps. It was found that it was almost
impossible to separate pure birch and pure aspen stands
in the satellite photographs and that extremely dense
undergrowth may indicate a different type of vegetation
than actually exists. During map interpretation it was
also found that the blurry nature of these extreme
enlargements made it difficult to determine actual
boundary lines between vegetation types. It was deter-
mined that the final maps for this project would have to
be larger to be of any value.
After this table was prepared, 10 sample units were
selected at random for quantitative sampling. Each
sample was superimposed on a high-altitude aerial
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photograph and species composition and density esti-
mated. This final analysis resulted in a more accurate
description of vegetation indicated by the two Landsat
photographs and are illustrated in Table 2.
By relating average cord wood per acre to the type of
vegetation present, it is possible using this method to
estimate the cordwood available in selected locations
throughout the state at an extremely low cost. In all,
Stringer and his staff mapped over 962,000 acres and
actually inventoried 120,000 acres. The total cost for this
inventory was 16 cents per acre.
Conclusion
The method developed by Stringer is indeed a low-
cost cordwood inventory process; however, it cannot be
deemed totally accurate. Because of the difficulty deter-
mining borders between vegetation groups, a 30% varia-
tion should be anticipated. This variation may mask the
locations of highly significant stands of mature hard-
woods, but "it should be stressed that the technique
described here is largely a reconnaissance process aimed
at exploring a wide region quickly in order to locate
areas for closer investigation. Before consideration of a
potential cord wood area progresses very far, a site
should be visited~ said Stringer.
Funding
U.S. Department of Energy
State of Alaska
Grant Recipient
Dr. William Stringer
$9,500
9,500
Geophysical Institute, University of Alaska
Fairbanks, Alaska 99701
Table 1
FINAL DESIGNATION DF COLOR· GRAY SCALE UNITS IN TERMS OF VEGETATION DESCRIPTIONS
SUMMER IMAGE-COLOR
Bright Red Red with Some Some Mottled Blue-Gray, Very Blue-Black
Blue Mottling Red-Blue, Maroon Few Red Patches
Purple, Lavender
A B c D E
0 Low-lying deciduous Low-lying deciduous Alpine tundra Largely bog. Not observed.
White vegetation. Open vegetation with with some black
crown cover, grassy some spruce. Some spruce.
fields, recent urban areas. Sap-
burns, urban areas. ling size trees.
Sapling size trees.
1 Largely closed Largely closed Open crown cover Medium crown cover Not observed.
Lt. Blue-Gray deciduous forest deciduous forest shrub thicket and shrub thicket, 65%
Lt. Brown-Gray with-10% shrub, with 20% spruce treeless bog, 60% shrub, 35% spruce.
little spruce. and 10% shrub. shrub, 30% black Sapling size trees.
Sapling to pole Sapling to pole spruce, 10% decid-
size trees. size trees. uous trees.
2 Completely closed Completely closed Largely closed Largely closed Largely closed
Brown-Gray deciduous forest deciduous forest crown cover. 50% crown cover spruce crown cover, 80%
to with little spruce with 20% spruce, no deciduous, 35% forest, 70% spruce, spruce, 10% decid-
Deep Brown or shrub. Pole to shrub. Pole to com-spruce, 15% shrub. 20% shrub, 10% de-uous, 10% shrub.
commercial size mercia! size trees. Pole to commercial ciduous. Pole to Pole to commercial
trees. size trees. commercial size size trees.
trees.
3 Not observed. Largely closed Largely closed Largely closed Moderate crown
Black crown cover. 75% crown cover. 50% crown cover, spruce cover, 50% shrub,
Deep Shadow deciduous (very deciduous, 25% forest, 80% spruce, 50% spruce (largely
likely largely spruce, 25% shrub. 10% deciduous, 10% black spruce). Sap·
birch). 17% spruce, Commercial size shrub. Commercial ling to pole size
18% shrub. Pole to trees. size trees. trees.
commercial size trees.
Source: The Northern Engineer, Vol. 15, No.4
158
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Table 2
SUMMER IMAGE-COLOR
Bright Red Red with Some Some Mottled Blue-Gray, Very Blue-Black
Scarlet. Magenta Blue Mott ling Red -Blue , Maroon Few Red Patches
Purple , Lavender
A B c D E
0 dec iduous young deciduous forest ; tundra with black
White trees o r saplings , some spruce, spr u ce ,
grassy fields , urban areas urban areas
tundra, recent burns,
urban areas
deciduous forest; dec iduous forest shrub, alder/w illow, black spruce ,
it . blue -gray small to medium with some spruce ; black spruce ; some shrubs ;
it . b rown -gray tree s small to medium small trees small trees
trees
2 deciduous forest ; deciduous forest mixed forest, spruce ; spruce forest;
brown -gray med ium to large with some spruce ; climax stage; medium to large medium to large
to trees medium to large medium to large trees trees
deep brown trees trees
3 mixed forest spruce forest spruce forest
black
deep shadow
N otes: For the mostly deciduous A and B categories, moving from a 1 to a 2 indicates older trees as well as a higher proportion of conifers.
Cl areas, usually found in drainages and floodplains, are not us eful sources of cordwood; C2 areas on a slope are likely to be good
cordwood sources .
D l areas of black spruce appear as a light-bluish -gray in winter images; deciduous vegetation appears light-brownish-gray in t he winter
color infrared image .
An E2 category is often a forest of tall white spruce in a sunlit location . The E3 category is not well defined, but probably has a low
cordwood poten t ial .
Source : The Northern Engineer, Vol. 15 , N o.4
159
Ethanol production
requires large amounts of
energy
Most alternative energy systems need some means of
heat storage as part of their overall design. This is due to
the often interruptive nature of specific power sources.
Solar cells generate electricity only when the sun is out;
likewise, wind generators need wind, and solar collectors
store heat only during the daytime.
Other than conventional batteries, there are few long-
term energy storage devices available for these systems.
One device that is gaining a following is the hydrogen
fuel cell, but hydrogen is highly explosive and hard to
control.
Neldon Wagner, a former teacher in Kodiak, thought
that ethanol, a form of alcohol, would be a perfect
energy storage medium. Ethanol can be burned in car
and truck engines, home space heaters, water heaters,
cooking appliances, and so on . It has a long, stable "shelf
life;' and it's not explosive like hydrogen.
In 1980, Neldon Wagner obtained a grant to study the
economic feasibility of ethanol production . His project
would use electrical power to generate ethanol from
water (H20) and carbon dioxide (C02 ). The experiments
would take place at a local Kodiak High School.
Project Design
Wagner purposely designed a project that was too
small for large scale energy production; however, his
concepts and findings could be upgraded to a full pro-
duction system easily. The main thrust of his experi-
ments was to execute four independent but serially con-
nected chemical reactions that would convert water
and carbon dioxide through methane and acetylene to
ethanal and finally to ethanol. The reactions were chosen
because:
• They were environmentally safe and produced no
unmanageable or toxic by-products .
• They were technically simple, and
• They were low cost and used no exotic metals or
apparatus.
Each reaction in the synthesis series was independently
conducted to achieve maximum efficiency, simple con-
struction, and technical feasibility. The final results
of these reactions would give Wagner an idea of the
economics of ethanol production .
Two glass reaction chambers were manufactured for
these experiments. Reaction Chamber A, used for reac-
tions one and two, is a 36 em long, 12 mm diameter
quartz tube with a Nichrome heating element supported
down the center of the tube with mica spacers. The mica
spacers provide mechanical support and also help inter-
rupt gas flow for better contact between the gas and the
Nichrome wire .
Reaction Chamber B is a necked-down (12 mm to
three mm) quartz tube with a 200-watt tungsten filament
inserted in the narrowed section . Although it was orig-
inally planned to insulate the two reaction chambers, no
insulation was used during the course of these experi-
160
ments . This is because temperature was visually con-
trolled with a crude SCR (Silicon Controlled Rectifier)
light dimmer circuit.
The four chemical reactions Wagner would use to
convert the water and carbon dioxide were: 1) combining
carbon dioxide with hydrogen to produce methane,
2) converting the methane at 1400 degrees to acetylene,
3) combining the acetylene with water to make acetalde-
hyde (ethanal), and finally 4) combining the ethanal
with hydrogen to make ethanol.
Wagner decided to perform the experiments out of
order since the reactants for reaction Number 3 were
readily available. This reaction converted acetylene to
ethanal. Ethanal is needed for the last reaction. As he
was converting the acetylene to ethanal, Wagner found
that simply bubbling the gas through an aqueous solu-
tion was very inefficient. He improved the process by
"squirting" the gas through a pinched off glass tube and
baffling the container with small pieces of plastic. Actual
efficiency was determined visually. Acetylene by itself
burns in an open flame and produces a lot of particu-
late matter (pure carbon), ethanal burns with a clean,
slightly yellow flame . Wagner simply adjusted the
amount of acetylene introduced to the reaction chamber
until he could produce an ethanal flame.
This same type of attitude was taken performing the
three remaining reactions. Visual observation was used
as the final test to determine the quality of the reactions.
During each reaction, the flow rates of the raw ingredi-
ents were monitored and compared to the gas produced .
This, Wagner decided, would give an accurate efficiency
value for ethanol production.
Results
Wagner found that although ethanol is a safe, long-
lasting fuel source, it required much energy to produce.
Starting with 100% energy, a full99.8 % would be con-
sumed just to store 0.2 %. Very few situations would
justify that type of energy loss.
Minimizing the number of reactions, or creating
larger, more efficient production units may reduce the
energy loss somewhat, but the ability to make this
process economically feasible seems highly unlikely.
Another problem with this process is the relative
sophistication of the components and processes as they
would relate to remote locations . More urban locations
would not have the type of storage problems this project
envisions because of more uniform usage .
Funding
U.S . Department of Energy
State of Alaska
Grantee
Neldon Wagner
1250 S .W. McGinnis
Troutdale, Oregon 97060
$1,639
1,639
Energy-efficient salmon
drying facility studied
Two Native village corporations conducted a study to
see if they could start up a commercial salmon process-
ing plant powered with solar panels, wind generators,
hydroelectric or some other local energy source .
Unfortunately, the lguigig Native Corporation and the
Levelock Natives Ltd . did not build the plant, and there
is no data about whether solar and wind power is
applicable .
The two village corporations had intended to build the
plant about 20 miles north of the mouth of the Kvichak
River which flows into Bristol Bay near Naknek and
King Salmon . The region is the world's largest commer-
cial salmon spawning area . There are no roads into
Levelock, so everything must be flown or shipped to this
small village of 100 residents.
Commercial fishing, trapping and subsistence hunting
and fishing are the principal economic activities of
Levelock . During summer, salmon are dried and smoked,
many on open-air drying racks.
Purpose
The feasibility study was to develop ideas for an
energy-efficient solar-heated, wind-powered commercial
salmon drying facility. In addition, a videotape was
planned to illustrate how innovative technology could be
used for a commercial salmon operation in a small
community.
All Alaska Services, Inc., of Kodiak, Alaska, con-
ducte d the study. The consultants compiled information
on fisher y resources, mar keting , smoking procedures,
plant facilities , staffing, transportation and financing .
But the evaluation of alternative energy options was
given only a cursory review in a one-third-page discus-
sion of solar and wind energy. Instead, the report spot-
lighted the potential use of diesel generation with waste
heat recovery fo r providing the fish processing heat
requirements .
161
STUDIES
Study Findings
The consultants proposed a $1 .64 million plant which
would process about 4,000 pounds of smoked salmon
daily during a 10-week period, for an annual production
of 240,000 pounds of smoked fish with a price of $7.20
per pound in Seattle, Washington. The consultants also
said an additional $1.5 million would be needed for
operating expenditures.
The village corporations, however, decided not to
pursue a project of this size after reviewing the study.
Project Evaluation
The feasibility study was approached from the stand-
point of high technology production equipment, requir-
ing significant amounts of energy and minimal
manpower.
State AT evaluators have indicated that a more appro-
priate approach would have been to analyze the available
and potential alternative energy sources. These would
have included active solar water heating , photovoltaics
and wind generation among other options . The issue of
using local labor and importing hired help also should
have been analyzed, in the State's view.
By assessing all these resources and their alternatives,
the parameters for plant design could have been iden-
tified under all potential scenarios, something the report
did not do.
Funding
U.S. Department of Energy
State of Alaska
Grant Recipients
Iguigig Native s, Ltd .
General Delivery
lguigig, Alaska 99613
Available Materials
$5 ,000
$5 ,000
Levelock Natives, Ltd .
General Delivery
Levelock, Alaska 99625
All Ala ska Services, Inc., A Study of the Feasibility of
Establishing A Commercially Smoked Salmon Process-
ing Facility, 1981 , 70pp.
Salmon waste study
shows good result
M t f . h men do not think twice when they clean a os 1s er . .d 1 . f h and let the fast movmg stream or tl a actwn carry
IS th f se· but when the total amount of that away e re u ' b . d . . 130 million tons, you egm to un er-v1scera 1s over . 1 k ' · d
d h blem faong A as as cannery m ustry. stan t e pro . 1 f" h . d
AI k ' 1 crative commerc1a 1s enes pro uce
as as u d 11 f · ld"
d f 500 million poun s annua y, o ten y1e mg
upwar s o . . d Th I h
h 1 to one b1lhon poun s. e sa mon catc ,
catc es c ose h If f II · I d d) ·
I ( entl·ng about a o a species an e IS a one repres h A d d d.
87 o/t f the total U.S. catc . n epen mg upon
hsome h f~ ho re processed once they are landed, from 15 ow t e 1s a · F
33 ot f th catch becomes processmg waste. or every to ./0 o e f d . . .f. t t t
d f lmon stuf e m a can, s1gm 1can was e ge s poun o sa . d" 1 d . 1 ndfill or in manne 1sposa areas.
tosAseb mka a und in both the seafood processing industry
ac gro · d D Le R ·d h h.
d t d . posal convmce r. roy e1 t at t IS an was e IS . · · Th t bl ded further mvestlgatwn. e presen
pro _em nfede. posing more than 50% of each fish is both
practiCe 0 IS u· f h Jd
f 1 d unnecessary; m many parts o t e wor , waste u an · 1 h 1 d · · t · stes are routme y c anne e mto a vane y
Processmg wa . .f. . . ht d h t t h
f b d ts What soentJ IC ms1g s an w a ec -0 y-pro uc · d 1 . h.
I d A laska nee to proper y manage t IS waste
no ogy oes ]]?" k d R .d
d to use it we . as e e1 . resource an h · R ·d
I ff t to find answers to t ese questwns, e1 , nan e or . 1 I . "d t f Alaska Env1ronmenta Contro Services,
pres! en t 0d funds to study methods that would make
was ?ran e e of each salmon caught in Alaska waters.
max1mum us 1 · · · d · th
H . · t would invo ve mvestJgatmg an testmg e IS pro1ec . f f" h .
f ·b·]·t f digesting hsh wastes rom IS processmg easl I I y o 1 ·] l"d d I. "d Th
I t Ver usab e 01 s, so 1 s, an 1qm s. e p ants o reco . h . . t !d be performed m two p ases. First, a
Projec wou b. d . d" .
1. ch of anaero IC an enzymatic 1gest1ve 1terature sear d h b h 1 f !d be performe . T en, a enc -sea e test o
shystemstwfofuctive method would be done and the results
t e mos e e R .d d d .
t d · a formal report. e1 acte as a visor to presen e m d d h 1 k . t t who woul o t e actua wor . two ass1s an s ~
Testing and Analysis . .
The first part of the project, the librar;: search, was
· d t b a graduate student, Roy T1mmreck. carne ou Y h f h U ·
T . k b gan with a computer searc o t e mver-Immrec e ·b d h 0 f . f AI k Resource LI rary an t e epartment o
s1ty o as a L"b f 11 db ·
I · ' AI ska Resource 1 rary, o owe y a tnp to ntenor s a . ' F" h · R L"b
h U · ·t of Washmgtons IS enes esource 1 rary t e mversi y . d d d S h 1 f Fisheries. The literature stu y was to eter-a~ ch 00 0 urce potential of cannery wastes and identi-mme t e reso h R ·d
f · methods to extract t ose resources. e1 y processmg . ·1 bl · h d th t b identifymg the resources ava1 a e m
hope at ythe fishing industry would begin to seek t ose was es, f d .
t d lop it instead o ump It. ways o eve ld 1 k ·1 1· ·d; The literature study wou oo at 01 content, 1qm
l .d f t.1. r potential, or other resources such as SO I er I IZe f h ]"b h b fbi gases and heat. A ter t e 1 rary searc was
com lust 1 Gewen Turner would perform a bench-study of
comp e e, . f · 1 1 t
b . d" estion o vanous sa mon samp es o anaero IC Ig d 1· d h · 1
d · content an qua 1ty an eat potentia . etermme gas . h d h b h
Th It f both the literature searc an t e enc -e resu s o d . .I bl t th
d ld be drafte mto reports ava1 a e o e stu ywou
162
seafood industry and other interested parties. This study
assumed that some useful by-products, such as the oils
high in vitamins, had already been extracted . The only
wastes digested would be those that had no other uses .
Turner used ground salmon wastes "donated" by area
canneries. These wastes were placed in 2,000-millimeter
glass flasks and immersed in a water bath to control
digesting temperature and allow the recording of heat
production. Although the water bath was originally to be
kept at 55 degrees centigrade, further literature research
determined that 33 degrees would produce a faster and
more stable digestion.
The two researchers monitored each sample until gas
production ceased, between 30 and 45 days, and then
analyzed both the gas produced and the spent flask
contents.
Conclusions
Roy Timmreck's final report on the literature study is a
comprehensive dissertation on the resources available in
fish wastes. Beginning with a description of the fish
processing industry including types of fish processed,
catch size, and typical fish wastes and waste treatments,
Timmreck then undertakes a thorough discussion of the
fish processing technology and practices including
methods of extracting valuable nutritional and other
beneficial products from the wastes. His report ends with
a list of the available vitamins and minerals in the fish
wastes and a list of all the certified Seafood Operators in
Alaska from 1977 to 1980.
Gwen Turner's report was based on the results of the
anaerobic digestion study. Although digestion was not
complete at the end of the experiment, the study did
provide information on gas content and quality and the
heat potential in fish wastes. The digested products were
also analyzed for fertilizer potential and the results
included in the report. Whereas Timmreck's report dealt
with theoretical potential, Turner's report provided hard
data on the potential resources available in the wastes.
Based on the bench tests conducted on the processed
salmon wastes, the researchers concluded that it is
possible to digest these wastes anaerobically, but that
further experimentation needs to be done to find the
balance that will fully complete the digestion process.
Researchers concluded that the following variables (ex-
plained in detail in the report) must be adjusted or moni-
tored to go beyond the partial digestion achieved in this
project: chemical oxygen demand; nitrogen and phos-
phorus ratios; pH levels; carbonate content of waste-
water; sodium concentrations; and potassium content of
wastes.
Throughout the course of the project, the potential of
the resource was stressed and not the development of a
workable system for developing the resource. Dr. Reid
feels that this is the responsibility of the fish processing
industry; his organization was involved only in identify-
ing the resource potentials. Because the fish processing
industry traditionally works only with processes that
have a fast payback schedule, it is uncertain if the in-
dustry will take advantage of this study.
Funding
U.S. Department of Energy
State of Alaska
$2,795
2,795
163
Grant Recipient
Leroy C. Reid, )r., Ph.D.
1200 West 33rd Avenue
Anchorage, Alaska 99503
Wood gasification studied
by timber mill
The 1980s have brought hard times for Alaska timber
companies and Mitkof Lumber Co., a small sawmill
located on the Wrangell Narrows three miles south of
Petersburg, found its market deteriorating and operating
costs rising.
Like many lumber companies, Mitkof had to look for
ways to remain profitable. Typically, small firms cut
payroll or search for new markets to do this, but in the
current business climate , the workforce was already cut
to the bone and new markets just weren't there . Another
method had to be found.
For every two-by-four cut in the world, there is a pile
of bark and sawdust left behind. This residue either ends
up being dumped, or burned in a giant incinerator. Saw-
mills in California, Oregon, and Washington are con-
verting a portion of this waste into "manufactured" fire-
place logs. Unfortunately in Alaska, there is an abund-
ance of fuel wood and thus a limited market for this type
of product.
Wood gasification was becoming popular with other
wood product companies . This process was a way to
"c hange a liability to an asset by converting waste wood
residue directly into a fuel" that could replace the
211,200 gallons of diesel used every year by the
company. Other small and large scale projects had
164
already proven the technology. The Mother Earth News,
an alternative magazine, outfitted a late model pick-up
truck with a wood gasifier and has traveled cross coun-
try using salvaged waste wood as fuel. They also modi-
fied a small gasoline generator to use wood-gas to gen -
erate electricity. After "a world-wide" search, Ed Lapeyri,
President of Mitkof Lumber Company, and Gerald
Engel, area forester, decided that a wood gasifier may be
part of the answer to Mitkof's problems.
In 1980, Mitkof Lumber Company applied for and was
awarded grants to research and develop a workable
wood-gasification plant. This project would be com-
pleted in three steps, with each step dependent upon the
results of the previous step. The steps would be to :
(1) test the wood wastes to determine fuel content;
(2) test the wood wastes' ability to produce a usable fuel
in a wood gasifier; and (3) develop an operational
gasifier. This was modified soon after receiving the
award to install a full-size wood gasifie r at Mitkof for
electrical power generation.
Data Collection and Testing
In April 1981, Engel and Ken Kilborn , a U.S . Forest
Service employee, determined that the sawmill produces
about 6,800 tons of wood waste each year, calculated by
monitoring 100 typical sawlogs as they were processed.
A wood residue sample was tested in this gasifier
located in Portland, Oregon.
Later that year, a sample of wood residue was shipped to
Hamilton Energy Systems of Portland, Ore., where it
was tested for five hours in a gasifier designed by Franz
Rotter. Although the output of the gasifier was supposed
to run a 175-horsepower Waukesha diesel/generator, the
generator section was inoperative. The gas produced did,
however, run the internal combustion engine with no
load and provided needed momentum to the project.
At the end of the five-hour test, the results showed that
almost 42 percent of the heat value in the wood was con-
verted to a low BTU gas. About 10,700 cubic feet of this
(95 BTUs per cubic foot) gas was produced, or approxi-
mately 26 cubic feet of gas per pound of wood. Further
studies indicated that the quality and amount of gas
could be increased by pelletizing the fuel, recycling the
spent charcoal, and adding a small amount of oil to each
burn. Pelletizing the wood before adding it to the gasifier
would also keep the wood scraps from periodically clog-
ging the feed hopper.
Final analysis of the wood-gasifier by-products indi-
cated that hazardous wastes were present and additional
scrubbing would have to be performed in order to satisfy
environmental requirements. For example, water pro-
duced as a by-product, was highly acidic, black from
soluble tars, and had an awful odor.
However, the test run proved that an acceptable gas
can be generated from the wood residues and that with
some modification a gasifier could be built to overcome
the offensive by-products. Shortly after this stage was
completed, Mitkof was informed by the State of Alaska
Division of Energy and Power Development that an
Anchorage company, Marenco, Inc., also was working
on wood-gasification. In fact, they had an experimental
system in Anchorage. Mitkof agreed to a contract with
the State to install a second generation gasifier manu-
factured by Marenco. Mitkof sent three workers to train
on the completed unit in Anchorage. After three days
of trying to get Marenco's gasifier to work, Mitkof man-
agement decided that a more reliable system would be
needed before installation would be approved. Mitkof
"lost interest at that point; according to Engle, and the
project was dropped.
165
Conclusions
Although the prospects of converting waste wood to a
usable fuel still sound exciting, the "technology isn't up
to snuff~ said Engel. 'Although one of the guys we con-
tacted had recently won a cross country race in a wood-
fired car and is planning a five-megawatt wood-gasifi-
cation plant in Michigan, we aren't large enough to war-
rant a large investment in technological research:' he
said.
The study itself, however, was considered a success. It
exposed those grey areas of the technology that dramat-
ically increase costs when going from experimental units
to full production facilities. For example, the studies in
Oregon indicated that the fuel had to be pelletized prior
to use and that additional environmental protection
devices were needed to process the by products. These
additions raised the price of a working system to almost
that of a large wood-fired steam generator system. With
present market conditions and an uncertain future,
Mitkof decided to maintain its present system of diesel
powered generators and equipment, supplemented by
utility power.
The future for wood-gasifiers is uncertain, even
though the State of Alaska has spent over $1.2 million
in wood gasification development since 1978. Prob-
lems with fuel consistency, dangerous by-products, etc.,
makes this energy source questionable.
Funding
U.S. Department of Energy
State of Alaska
Grant Recipient
Mitkof Lumber Company
P.O. Box89
Petersburg, Alaska 99833
$6,415
6,415
Media and curriculum
projects expand energy
knowledge
While scores of grantees were inventing new applica-
tions for energy technologies, grappling with technical
problems, and getting their equipment on-stream, other
grantees were participating in a statewide series of grants
to spread the word about appropriate technology.
These programs ranged from full-scale video and
audio tape programming production to community
workshops that taught the basics of energy conservation.
Several grants enabled communities to develop their own
energy libraries or resource centers (in addition to a series
of grants awarded individual libraries statewide to
improve their collections; these grants are listed in the
Appendices).
The following is a synopsis of each grantee's media
and educational project under the AT grant program .
Robert Woolf
A textbook outlining the historical origins of appro-
priate technology was developed by Robert Woolf, and
Paul Helmar of Juneau. Woolf received $7,026 from the
U.S. Department of Energy and $39,376 from the state of
Alaska for the project, which he developed while teach-
ing in the v illage of Atmautluak.
The history textbook, a one-semester course, is avail-
able through the Alaska Department of Education's
vocational education office. The state is publishing
so me 1,000 copies of the textbook.
In addition, Woolf designed a model home for class-
room use. The model, two-feet-by-one-foot-by-two-feet ,
helps students learn about the concepts of appropriate
technology. It also is available through the vocational
education office .
Further information may be obtained from Woolf at
749 St. Ann's Ave ., Douglas, AK 99824 .
Southeast Regional Resource Center
The Southeast Regional Resource Center obtained
$35,000 for producing videotapes, slide tapes and lesson
materials on the appropriate technology grants. All that
was completed was a 30-minute videotape on some of
the AT projects. It is available through the State Film
Library under the title "Appropriate Energy Modes:'
167
University of Alaska-Fairbanks,
School of Agriculture
Belle Michelson and Sue Yerian, with the U of As Fair-
banks School of Agriculture, received $7,769 in funding
to create an energy curriculum library at the North Pole
Junior-Senior High School. Multi-media teaching mate-
rials emphasizing northern energy applications were
selected for the library collection. Goals of the program
included demonstrating local appropriate technology
through multi-media education, boosting the amount of
locally available alternative energy literature, and teach-
ing these energy topics in seventh through 12th grade
classes.
For more information, contact Yerian at Box 82114,
College, AK 99708.
Western Media Concepts, Inc.
Western Media Concepts, Inc., a radio production
firm in Anchorage, received a $16,896 grant to research,
edit and produce radio broadcast tapes for various alter-
native energy projects around the state. In all, the com-
pany produced 15 five-minute programs, aired on 10
commercial radio station members of the Alaska Radio
Network. Three documentaries also were produced, as
well as 15 two-minute features . The tapes were offered to
and used by radio stations statewide.
Further information on the radio project may be
obtained from Western Media at P.O. Box 215 , Anchor-
age, AK 99510 .
Northwest Community College
Nome's Northwest Community College used AT grant
funds to improve knowledge of appropriate technology's
benefits in a number of villages in the Northwest Alaska
region , including Unalakleet, Gambell, Savoonga,
Shishmaref, Wales, Teller, Stebbins, Diomede, White
Mountain, Golovin and Nome. The $26,797 project
included workshops, demonstrations, consulting for
residents and accumulation of a collection of books for
the college library and five learning centers throughout
the region.
Further information on the program may be obtained
from the Energy Information Center (Library) at the col-
lege , Pouch 400, Nome, AK 99762 .
Sitka Community College
The Sitka Community College also conducted an
energy outreach program in its region with a grant total-
ing $9,582. Workshops were held in Kake, Angoon,
Petersburg and Wrangell by two instructors. The work-
shops covered lifestyle practices that can reduce energy
consumption; conservation measures suitable for (indi-
vidually audited) homes; applications for renewable
resource energy sources; financing and other programs
available through the state for energy conservation;
federal energy conservation tax credit programs; and
retrofitting methods to improve energy efficiency.
Further information on the program may be obtained
from the college, P.O. Box 1090, Sitka, AK 99835.
Huslia High School
Huslia High School was awarded a $5,579 grant to
develop an Energy Resource (Information) Center in the
school. The collection included books, pamphlets,
reports, video and audio tapes, and films. The school
sought the grant to improve its teaching and educational
resources for the community. The library was available
168
to teachers during the day and to the community during
after-school hours.
Further information on this Yukon-Koyukuk region
project may be obtained from the high school resource
center, Huslia, AK 99746.
Steve Smiley
In addition to his wind generator project in Homer,
appropriate technology advocate Steve Smi)ey con-
ducted a workshop at the Seward Training Center under
a $5,000 grant from the AT program. In the workshop,
Smiley discussed techniques for building and retrofitting
for energy efficiency. He covered costs and benefits of
energy efficiency (such as tax credits, etc.), general
design considerations, specific building techniques,
building materials, and selected hardware.
Further information on the workshops may be obtained
from Smiley at SRA Box 41-C, Homer, AK 99603.
,.
r
I
Glossary
Absorber pipe-The tubing is a solar collector that transfers
the heat collected by the absorber plate to the heat transfer
fluid, either air or liquid, within it.
Appropriate Energections-A quarterly magazine pub-
lished by the State of Alaska, Department of Commerce
and Economic Development, Division of Energy and Power
Development until june, 1983.
BTU-British Thermal Unit. A measurement of heat, or
more specifically, the amount of heat required to raise one
pound of water one degree Fahrenheit when the temperature
of the water is initially at 39.2 degrees.
Clerestory-A window, or windows, placed high on a wall
near the eaves, used for light, heat gain, and ventilation.
Cooperative Extension Service-A cooperative education
program between the University of Alaska and the U.S.
Department of Agriculture. The purpose of this service is to
provide information to Alaskans to help identify and solve
problems in order to improve business, homes, and
communities.
Deadman beams-Long poles or beams buried in the
ground like a dead man to provide strong anchors for
winching or guy wires. Deadman beams are buried at right
angles to the line of pull in order to provide maximum
resistance.
Domestic water supply-Standard household water system
connected either to the municipal water system, a well, or
another source like a cistern collecting rainwater.
Double-glazed thermal window-A double-paned window
that has an air gap between the panes, giving increased
thermal insulating qualities almost double the insulating
value of a single-pane window.
Earth-sheltering-A construction technique which places
all or part of a building under ground level. Although con-
struction materials used in earth-sheltered buildings must
be heavier than for standard above-ground structures,
earth-sheltered homes have the advantage of less air infil-
tration and sometimes decreased heat loss through
the walls.
Float-valve (controlled) alarm-A device used to auto-
matically signal a homeowner when the fluid in a reservoir
falls below a predetermined level.
Gin pole-A tall pole used as a portable derrick fulcrum for
lifting heavy objects.
Heat exchanger-A device that transfers heat from one
fluid to another without the two fluids touching each other.
Both air and water are considered fluids.
Heat exchanger coils-Coils of tubing, usually copper,
within a heat exchanger assembly. As fluid flows through
the heat exchanger coils, the heat is transferred from the
fluid outside the coils to-the liquid inside the heat exchanger
or vice versa. This system is often used to ensure that the
liquid on the outside of the coil does not mix with the liquid
inside the coil (i.e., one fluid may have antifreeze in it and
the other fluid may be drinking water).
171
Heating degree days-A measure of the need for heat,
based on the assumption that when outside temperatures
drop below 65 degrees, the heating system will come on to
keep the house at 70 degrees. Degree Days (DD) are
calculated daily as follows:
65 degrees -average outdoor temp = heating DD
Temperatures above 65 degrees are considered 0 Heating
Degree Days. Over the course of a winter, the total annual
Heating Degree Days are used to compare the severity of
one winter with another.
Parabolic reflector-A bowl-shaped device used to concen-
trate solar or electromagnetic energy by reflecting the
energy to a focal point much smaller than the collector area.
This device produces much higher temperatures at the focal
point than can be obtained with a flat-plate collector.
Passive system-Passive systems involve energy collection,
storage, and distribution by means of natural processes
using a minimal amount of power fans or pumps. Passive
cooling also includes methods to shade the solar collectors
and control ventilation and humidity.
Plastic bubble insulation-A form of insulating material
which sandwiches bubble polyethylene (the same material
used as packing in shipping boxes) between layers of other
materials. This system creates several layers of dead air
space for improved insulating abilities.
Photovoltaic cells-Devices which convert sunlight directly
into electrical energy (also called solar cells). A grouping of
cells may be manufactured as a panel.
R-value-The measure of the ability of a material to resist
heat flow. This term is used to compare the heat-saving
ability of building insulation and other construction materi-
als and represents how many BTUs per hour will pass
through the structure to the outside. The higher the "value"
the better the insulating ability; R-20 is twice as good as
R-10 and R-50 is five times better than R-10. A single-pane
glass is less than R-1 and a common two-by-four wall insu-
lated with fiberglass has an R-13.
Radiant heat system-A heating system that takes advan-
tage of the radiant component of heat transfer. Radiant heat
is composed of electromagnetic waves that travel through
space, demonstrating warmth only when they strike a solid
object, like a wall, or your skin. The warmth felt directly
from the sun or a woodstove is radiant heat.
Reflective mylar-A generic term for polyester film with a
microthin coating of metal applied to one side, usually
aluminum. The metal coating greatly increases the heat
reflectivity of the mylar with only a slight reduction in its
light transmission qualities.
Sola-Roll Systems-(Also known as Solaroll.) A flexible,
black rubber EPDM solar absorption system with six
molded tubes for carrying water or other heat transfer fluid.
Sola-Roll can be used for solar absorption energy systems
or imbedded in concrete for radiant heat appliCations. The
fluid-carrying flat tubing(%" diameter) is an integral part
of the Sola-Roll System. The term applies to the construc-
tion which places six tubes in parallel, then seals them in
flexible, black rubber EPDM material. The end result is a
"flat-tubing" product.
Shotrock-Coarse rubble left over from a blasting opera-
tion and which can be used for thermal mass.
Solar gain-A measure of the amount of BTUs received on
a particular surface over a given period of time.
Solar greenhouse-A greenhouse that is attached to a house
and provides heat storage and heat to the interior of
the home.
Solar water heaters-Domestic water heaters that use the
energy of the sun to heat the water.
"Space Blanket" curtains-Quilted aluminized-mylar cur-
tains that reflect a large portion of the radiant heat striking
them and yet still offer the light transmission reduction of
standard curtains. These curtains are also lightweight and
extremely thin.
TPs-A fabricated Wooden beam which uses a combination
of solid wood and plywood to make a strong, lightweight
building material. TJI is an acronym for truss joist /I, or
!-shaped truss joists and are manufactured by the Truss
Joist Company.
Thermal mass-Building materials that absorb and store
heat. Thermal masses can be brick, shotrock, large contain-
ers of water, adobe, masses of cement, etc.
172
Thermax-An isocyanurate foil covered foam sheathing
(plastic) used to insulate buildings and manufactured by the
Celotex Corporation. Other similar products are called
R-MAX, THERMOFAX, TECHNIFOAM, and HIGH-R.
Thermax is known for its strength, high R-value, and light
weight.
Thermosiphon system-A heating system designed to
exploit the natural tendency of hot fluids to rise and cold
fluids to fall. It can provide heat distribution without the
use of a circulating pump, or fan.
Tracking system-A mechanical system designed to rotate
solar collectors so they receive maximum available solar
energy.
Utility intertie system-The direct connection through a
control box of a wind or hydro electric generation system
with the local utility electric power system. This enables the
homeowner to almost always have electricity either from
the wind or hydro system, or the local utility. Any power
not used by the homeowner may be sold to the electric
utility.
Vapor barriers-A layer of material used to retard the
movement of moisture and air from the warm insulated
wall to the cold side. Because warm air can hold more
moisture than cold air, a vapor pressure will occur in cold
weather on the outside walls and ceilings of a house. The
moisture can be forced through openings and permeable
materials in the walls and ceilings. The moisture may then
condense or freeze in the insulation, reducing the insulating
value and causing moisture or wciter problems which are
sometimes severe. Some common vapor barriers are poly-
ethylene film (Visqueen) and aluminum foil.
APPENDIX A
Appropriate technology grants to libraries, 1980-1982
Grantee Location Amount*
Cooperative Extension Service Anchorage $2,297
West High School Media Center Anchorage 213
Service Hanshew Resources Center Anchorage 390
Anchorage Career Center Anchorage 350
University of Alaska Anchorage 350
Angoon High School Angoon 1,244
Yukon Flats School District Arctic Village 350
BIA Bethel Regional Library Bethel 391
Cantwell Education Association Cantwell 550
Anderson Village Library Clear 350
Cordova Public Schools Cordova 530
Dillingham Public Library Dillingham 553
Dillingham City School District Dillingham 1,685
Eagle Library Eagle 350
Elim Community Library Elim 350
Fairbanks North Star Borough Fairbanks 1,150
University of Alaska, Rasmuson Library Fairbanks 905
Yukon Flats School District Fort Yukon 550
Glennallen School Library Glennallen 350
Copper Valley Community Library Glennallen 350
Haines Borough School District Haines 350
Haines Borough Public Library Haines 198
Tri-Valley School Library Healy 4,472
Homer Public Library Homer 374
Hoonah Schools Library Hoonah 300
Hooper Bay High School Hooper Bay 350
Alaska Conservation Society, Taku Chapter Juneau 350
Juneau Borough Library Juneau 618
Juneau-Douglas High School Juneau 372
Kake High School Library Kake 468
Kenai Junior High School Kenai 284
Kenai Central High School Kenai 319
Kenai Community Library Kenai 1,350
Kenny Lake Community Library Kenny Lake 691
Ketchikan Public Library Ketchikan 350
McQueen School Kivalina 320
A. Holmes Johnson Memorial Library Kodiak 650
Kodiak Island Borough School District Kodiak 450
City of Kotzebue Kotzebue 350
McGrath Community Library McGrath 350
Nenana Public Library Nenana 350
Kegoayah Kozga Library Nome 850
Mat-Su Community College Palmer 1,004
Palmer Public Library Palmer 350
Petersburg High School Petersburg 720
Petersburg Public Library Petersburg 1,050
Port Lions Public Library Port Lions 650
St. Mary's High School St. Mary's 175
Susan B. English School Seldovia 175
Seward High School Library Seward 670
Kettleson Memorial Library Sitka 622
Skagway City School District Skagway 175
Soldotna Public Library Soldotna 350 r
Kenai Peninsula Community College Soldotna 300
Sutton Public Library Sutton 281
Talkeetna Public Library Talkeetna 350
Tanana Community Library Tanana 350
Tenakee Public Library Tenakee 350
Valdez City Schools Valdez 350
Valdez Public Library Valdez 320
Wrangell Public School District Wrangell 350
Irene Ingle Public Library Wrangell 1,300
Yakutat City Schools Yakutat 350
*Most current reported
1\73
APPENDIXB
Appropriate technology edited
videotape project material
The Alaska State Film Library has available for viewing a
number of AT project films, most compiled as news reports by
the television media. These projects are listed below.
KTOO-TV
Petersburg Ram
Pt. Baker
Port Armstrong
Thayer Lake
Thayer lake
Ken Cassell Hydro
KIMO-TV
Dallas Solar, Fairbanks
Don Chaney/Mike Baumgartner
Port Armstrong Hydroelectric
McGrath Greenhouse
H. jack Coutts
john Collette
KYUK-TV
Hooper Bay Wind-3 parts
june, 1983
June, 1983
june, 1983
September, 1982
September, 1982
September, 1982
june, 1983
May, june, 1983
June, 1983
May, 1983
june, 1983
june, 1983
May, 1982
Alaska Review #46 ':Alternative Energy: Alternatives for
Alaskans" 29,14, 1982
':Appropriate Energy Modes" 27:30, 1982
"Alternative Energy in Alaska: Everett Drashner's Homestead"
1981
"The Great Alaskan Warm-up" 29,30, 1984
("Retrofit" and "Sunspace" segments)
II
174
APPENDIXC
Grant awards returned
or not accepted
Dan Denslow, Ambler,
Wind Powered Freezer $ 3,500
Tom Miller, Kodiak,
Insulating Shutter 675
Walt Cunningham, Bare Island,
Alcohol Production 2,750
Ricardo Quiroz, Anchorage,
Wood-Heat Systems 8,000
City of Tununak,
Energy Conservation Workshops 4,414
Joann Schoonover, Anchorage,
Rainwater System 15,000
Charles Vowell, Anchorage,
Wind-Powered Heat Pump 8,200
Kodiak Community College, Ahkiok,
Energy-Efficient Home Building 6,260
St. Mary's School District, St. Mary's
Greenhouse 25,540
Alice Campbell, Fairbanks,
Compost-Heated Greenhouse 290
Alas-Can Energy Expo 80, Anchorage,
High School Energy Fair 2,000
William Major, Glennallen,
Solar Collector 4,200
Lower Kuskokwim Coast Corporation, Kipnuk,
Earth-Sheltered Office Building 50,000
Kodiak Mental Health, Kodiak,
Greywater Heat Recovery 19,153
City of Dillingham, Dillingham,
" Wind Monitoring Equipment 10,000
Matanuska Electric Association, Inc., Palmer,
Wind Monitoring Equipment 1,458
Gary Nowobielski, McKinley Station,
Hydraulic Ram 1,115
175
APPENDIXD
Grant projects terminated
before completion
Craig H.F. Anderson, Palmer,
Solar Collector
Nome Veterinary Hospital, Nome,
Solar Thermal Storage
Arctic Technical Services, Inc., Kotzebue,
Solar System
William Arterburn, Willow,
Air to Air Heat Exchanger
Hughes Village Council, Hughes
Alternative Energy Study
Sandra Tahbone, Nome,
Sod House
James Keck, Fairbanks,
Passive Solar
William Hightower, Moose Pass,
Methane Digester
Patrick Yourkowski, Homer,
Wood-Heat and Storage System
John Hodge, Fairbanks,
Hydrate Energy Storage System
George Bennett, Fairbanks,
Energy Efficient Garage/Shop
Kodiak Winds, Kodiak,
Wind Monitoring System
Dean Jarosh, Takotna,
Micro-Hydro System
$ 400
2,576
24,900
2,162
3,000
1,266
313
1,922
3,081
183
7,860
8,251
2,710
(
l
176